ML19257C373
| ML19257C373 | |
| Person / Time | |
|---|---|
| Site: | La Crosse File:Dairyland Power Cooperative icon.png |
| Issue date: | 01/11/1980 |
| From: | James Keppler NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
| To: | Linder F DAIRYLAND POWER COOPERATIVE |
| References | |
| NUDOCS 8001280501 | |
| Download: ML19257C373 (1) | |
Text
/
'o UNITED STATES g
NUCLEAR REGULATORY COMMISSION o
5 REGION 111 b[
0, 799 ROOSEVELT ROAD o
GLEN ELLYN, ILLINOIS 60137 Docket No. 50-409 NAh111300 Dairyland Power Cooperative ATTN:
Mr. F. W. Linder General Manager 2615 East Avenue - South La Crosse, WI 54601 Gentlemen:
Enclosed is IE Bulletin No. 80-01 which requires action by you with regard to your BWR power reactor facility with an operating license.
Should you have questions regarding this Bulletin or the actions required of you, please contact this office.
Sincerely,
~
James G. Keppler Director
Enclosure:
IE Bulletin No. 80-01 cc w/ encl:
Mr. R. E. Shimshak, Plant Superintendent Central Files Director, NRR/DPM Qirector, NRR/ DOR PDR Local PDR NSIC TIC Mr. John J. Duffy, Chief Boiler Inspector, Department of Industry, Labor and Human Relations 1819 247 6001280 FO/
UNITED STATES SSINS No.:
6870 NUCLEAR REGULATORY COMMISSION Accessions No.:
OFFICE OF INSPECTION AND ENFORCEMENT 7912190652 WASHINGTON, D.C. 20555 January 11, 1980 IE Pulletin No. 80-01 OPERABILITY OF ADS VALVE PNEUMATIC SUPPLY On January 10, 1980, the NRC was informed by Philadelphia Electric Company that engineering evaluation for Peach Bottom 2 and 3 has disclosed that the Automatic Depressurization System (ADS) pneumatic supply (either nitrogen or air) may not be operable for all possible events because of a combination of misapplication of check valve, a lack of leak testing of the accumulator system backing up each ADS valve operator and questions about the continued operability of the pneumatic supply in a seismic event.
Attached is a simplified schematic of the pneumatic supply. The check valve nearest to the accumulator is a PAL, three quarter inch, stainless steel, socket welded check valve with a hard seat (valve identification-B-1376 on the upper flange).
Plant information at Peach Bottom shows substantial supports for the pneumatic supply inside the drywell, but seismic qualification has not been verified.
The licensee has stated that the pneumatic supply is not seismically qualified outside the drywell.
Unit 2 was shutdown on 1/10/80 because of questions of ADS operability and Unit 3 has been provided a seismically qualified nitrogen supply at the containment penetration pending confirmation of seismic qualification of piping inside Unit 2 containment.
The licensee is changing their valve to one with a soft seat to reduce leakage.
Actions to be taken by Licensees of GE BWR facilities with an operating license which use a pneumatic operator for ADS function:
1.
Determine if your facility has installed hard-seat check valves to isolate the ADS accumlator system from the pneumatic supply system.
2.
Determine if periodic leak tests have been performed on your ADS accumulator systems to assure emergency pneumatic supply for the FSAR-required number and duration of valve operations.
3.
Review seismic qualifications of the ADS pneumatic supply system:
(a) from accumulator system isolation check valve to ADS valve operator, (b) from isolation valve outside containment up to ADS accumulator check valve.
4.
Based upon determination of item DUPLICATE DOCUMENT of the ADS for the conditions un including a seismic event.
If o Entire document previously to appropriate Technical Specifi entered into system under:
ANO Y
1819 248 No. or gases: