ML19257A956
| ML19257A956 | |
| Person / Time | |
|---|---|
| Site: | Marble Hill |
| Issue date: | 12/28/1979 |
| From: | James Keppler NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
| To: | Shields S PSI ENERGY, INC. A/K/A PUBLIC SERVICE CO. OF INDIANA |
| References | |
| NUDOCS 8001090494 | |
| Download: ML19257A956 (1) | |
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UNITED STATES 8'3,'
NUCLEAR REGULATORY COMMISSION o
E REGION lli e
o IJ 799 ROOSEVELT ROAD
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GLEN ELLYN, ILLINOIS 60137 o
DEC 2 81979 Docket No. 50-546 Docket No. 50-547 Public Service of Indiana ATTN:
Mr. S. W. Shields Vice President - EleLtric System 1000 East Main Street Plainfield, IN 46168 Gentlemen:
TIis Information Notice is provided as an early notification of a possibly siacificant matter.
It is expected that recipients will review the Inf ormation for possible applicability to their facilities.
No specific action or response is requested at this time.
If NRC ? valuations so indicate, further licensee actions may be requested or required.
If you have questions regarding this matter, please contact the Director of the appropriate NRC Regional Office.
Sincerely,
[/ James G. Keppler Director Enclosure IE Information Notice No. 79-37 cc w/ encl:
Mr. Steve J. Brewer, Nuclear Safety and Licensing Supervisor Central Files Director, NRR/DPM Director, NRR/ DOR PDR i030 058 Local PDR NSIC TIC LeBoeuf, Lamb, Leiby & MacRae Mr. Dave Martin, Office of the Attorney General Mr. John R. Galloway, Staff Director, Environment, Energy, and Natural Resources Subcommittee 8 0 010 90 4-7t
UNITED STATES ISIN5 NO.-
6870 NUCLEAR REGULATORY COMMISSION Accession No.-
0FFICE OF INSPECTION AND ENFORCEMENT 7910250525 WASHINGTON, D.C.
20555 December 28, 1979 IE Information Notice No. 79-37 CRACKING IN LOW PRESSURE TURBINE DISCS Description of Circumstances:
An anonymous letter was received by the Director of the Office of Inspection and Enforcement, on November 17, 1979 which alleged possible violation of Part 10 CFR 50.55e and/or 10 CFR 21 Regulations concerning reportability of recently discovered stress corrosion cracking in Westinghouse 1800 rpm low pressure turbine discs.
Westinghouse had made a presentation on the turbine disc cracking to electric utility executives on October 30, 1979.
Telephone discussions between the NRC staff and Westinghouse's Turbine Division on November 20, 1979 established that cracking, attributed to stress corrosion phenomena, had been found in the keyway areas of several LP turbine discs at operating plants and that inservice inspection techniques (i.e., in situ ultra-sonic examination) for crack detection have been developed and are being imple-mented in the field.
The Office of Inspection and Enforcement was also notified on November 20, 1979 that during the current overhaul of Commonwealth Edi. son's Zion Unit 1 LP turbine, ultrasonic examination revealed embedded cracks located on the inlet side on the disc bore area where no cracks had been previously observed.
Ultrasonic measurements indicate this disc bore cracking is of greater depth than the keyway cracks found to date.
According to Westinghouse, these bore cracks have been metallurgically examined and preliminary findings show them not to be typical of classical stress corrosion cracking observed in the keyways.
The probable cracking mechanism and impact on disc integrity is being further evaluated by Westinghouse.
A meeting was held on December 17, 1979 between the NRC staff, Westinghouse and utility representatives to discuss the disc cracking problem, repair alter-natives, turbine missile evaluation, inspection techniques and plant inspection priorities.
In response to the staffs' request, Westinghouse provided the staff an updated report on December 21, 1979 regarding the current field inspection program that included a list of nuclear power plants already inspected, recom-mended inspection schedules and pertinent information related to LP turbines where cracks have been observed.
Inspections to date have identified turbine disc cracks at Surry Unit 2, Point Beach Unit 2, Palisades, Indian Point Unit 3 and Zion Unit 1.
All units except Poi the plants return to power.
Point Bea with a small crack in the No. 2 disc o Westinghouse indicated that the observ DUPLICATE DOCUMENT during 28 additional months of turbine the turbine inspection results and ana Entire document previously entered into system under:
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