ML19256B413

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Forwards IE Circular 79-07, Unexpected Speed Increase of Reactor Motor Generator Set Resulted in Reactor Power Increase. No Written Response Required
ML19256B413
Person / Time
Site: Millstone 
Issue date: 05/02/1979
From: Grier B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To: Counsil W
NORTHEAST NUCLEAR ENERGY CO.
References
NUDOCS 7906130164
Download: ML19256B413 (1)


Text

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May 2,1979 Docket No. 50-245 Northeast Nuclear Energy Company ATTN: Mr. W. G. Counsil Vice President - Nuclear Engineering and Operations P. O. Box 270 Hartford, Connecticut 06101 Gentlemen:

The enclosed IE Circular No. 79-07 is forwarded to you for in-fonna tion.

flo written response is required.

Should you have any questions related to your understanding of this matter, please contact this office.

Sincerely, f

d}'.

~

Boyce H. Grier

' Director

Enclosures:

1.

IE Circular No. 79-07 2.

List of IE Circulars Issued in Last Twelve fionths cc w/encls:

J. F. Opeka, Station Superintendent D. G. Diedrick, Manager of Quality Assurance J. R. Himmelwright, Licensing Safeguards Engineer A. Z. Roisman, Natural Resources Defense Council 7006130/fy.T

UNITED STATES NUCLEAR REGULATORY COMMISSION OFFICE OF INSPECTION AND ENFORCEMENT WASHINGTON, D.C.

20555 IE Circular No. 79-07 Date:

May 2, 1979 Page 1 of 3 UNEXPECTED SPEED INCREASE OF REACTOR RECIRCULATION MG SET RESULTED IN REACTOR POWER INCREASE Description of Circumstances:

On November 24, 1978, an unexpected rapid speed increase was experienced on the 'B' Reactor Recirculation MG set (RRMG) at the Cooper Nuclear Station.

Prior to the event, the RRMG set had been inadvertently tripped during the performance of routine maintenance.

Upon restart, the MG set would not respond to a speed increase signal.

Licensee personnel com-menced trouble shooting this problem in accordance with the instructions in the manufacturer's technical manual.

One step of these instructions suggested removing the fuse from the Bailey scoop tube actuator circuit (a blown fuse would de-energize the actuator and not permit the scoop tube to move).

When the terminal panel cover was removed, licensee personnel noted two fuses instead of one as shown on the vendor drawings.

When licensee personnel removed the second fuse to verify fuse integrity, a rapid speed increase of the MG set occurred.

This increase was terminated by replacement of the fuse or tripping of the MG set by the control room operator (both actions took place almost simultaneously).

The input signal to the scoop tube actuator is received from the speed controller via a function generator.

This signal is a scoop tube posi-tion demand signal.

As the actuator drives the scoop tube in or out of the fluid coupler, a position followup signal is generated to null the input signal and stop scoop tube motion at the required position.

The vendor's drawings of the scoop tube actuator circuit showed only one fuse in the circuit.

The licensee contacted the vendor regarding the second fuse and was informed that this fuse had been added as a change in the initial circuit design to provide protection for certain elec-tronic components in this circ '

the position 'ollowup circuit.

in a loss of the nulling signa to the maximum speed position.

DUPLICATE DOCUMENT Entire document previously entered into system under:

ANO 74 0 5 / 9-D +9 7 No. of pages:

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