ML19256A930
| ML19256A930 | |
| Person / Time | |
|---|---|
| Site: | Brunswick |
| Issue date: | 01/02/1979 |
| From: | Willis E CAROLINA POWER & LIGHT CO. |
| To: | |
| Shared Package | |
| ML19256A927 | List: |
| References | |
| NUDOCS 7901170153 | |
| Download: ML19256A930 (8) | |
Text
i APP T.'D I 7 2 A '/ E l A'3E 'l A I L t ?'J'"9 LE'/3 L aCC"ET
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,a CATE 01/02/7 C1 PL3TT) ";Y EULIS
'"I LLI 3 TELEPHLT'E 915-457-6711 xCE..r.iG 7; J.W AVG. JAIL ( P C '.'.'E R L E V E L DA/
A'!C. tM ILY P J"'E9 LEVIL
("ME-riET)
( ' C 'F-d ET )
1 563.
17 318.
2 273.
10 4 95.
3 276.
19 a1J.
4 al6 27 465.
o 599 21 a11 6
51I.
22 457 7
546.
23
?76.
o 601.
24 26a.
y 294 25 279 10 294 25 265.
Il 594.
27 2c9.
I2 6l1 2a M..
Ia 6la.
29 339 14 629.
3) 305.
Ib 643.
31 135.
10 270.
1.16 - a 7901170153
- PER ATI.13 JAYA ?9Cdr DCC::ET iO. 040-0320 DATE GI/02/7s C0!?LETED 3Y EULIR MILLI 3 TELEPHO"E 9l+-457-671I le ATIi G 5iATUS l
I.
i!I 1 IA iE: Ri? U:iS'/:IC:( U'!IT I I 'JCTE S I
- 2. '< d e J u i l.! J P E 7 I C D : DECE ME7 7d I
I J. LICdfiSEJ TridL!AL PTIER (.M ): 2435 I
I 4
14,.dPlaic R ATIdG (GR OSS Tc'E ) : c67.0 I
I
- 3. uuSIG.i dLECT7ICAL RATI'!G (.'IE T 1 /2 ) : 621.3 I
I S.
stAX uEPEilDABLE CAPACITY ( GROSS..t '!E ) : 315.0 I I
7.
iAX UEPEliUABLE CAPACITY (tIET M'tlE): 790.0 a.
IF CHA' LUES OCCUR Ii! CAPACITY RATI!!GS (ITE IS 3 THRU 7) SIIICE LAST REPORT, JI/d RJASONS:
9 PT.d? L.i /EL TO '! HIC.i dESToICTED IF A:l/ ('TET.i E): ':0ME 17.
ta.,5U.!S FOR 1ESTRICTID'r IF A?!Y:
THIS Yo TO CU"UL
...CJTH DATE ATIVE II. HOURS I:i REPORTItiG PdRIOD 744.0 o760.7 15697.0
- 12..lJ:'Ud7 0F HOURS REACTOR LI AS CoITICAL 744.0 7850.6 12310.6 Ia. REACia:? RESE.~2VE SHUTDOTI HOURS 0.0 n.0 1627.I i4
.1JUHS Je EP A f0R O'l LI?iE 744.0 7627.6 11549.d in. U.ll f ?dS3RVE SHUTDOTi HOURS 0.0
'.0 1.0
- 15. J iLSS fHEP?*AL
- !ERGY GESIERATED ( r!H )
1035903.6 16036295.1 239271.91.1 II. v tCSS ELECTRICAL d:iEdGY GE'IERATEv ( ""-! )
337730.0 53092dl.0 7931277.7 la.
!ET ELECTPICI AL E.iElJY GE':ER ATED ("":H) 323556.0 5122 bN. o 753359a.0 I /.
U.. I t SE7 VICE FACTur:
100.0 37.I 73.5
- 27. v.IIT AVAILABILITY FACTOR 10u.1 a7.I 73.6 21 U~iIT CA?ACIT( FACT 07 ( US I LIG MDC '!ET) 55.0 74.0 51.6
- 23. J.llt~ FORCED JUTAGE
.~2 ATE 0.0 9.1 23.5 24 S.iUTv0'!i;S SCiiEDULED JVER 'IEXT 6.10HTH3 (TYPE. DATE, A"D DU?\\TIJT OF E\\CH)-
Refueling 79,01,13 1656.0 hours0 days <br />0 hours <br />0 weeks <br />0 months <br /> D.
Ir 6tiUT30""! AT Eild JF 7EP07T PERIOD, iSTIIATED DrTE 0.2 STA~'T UP :
O/ 7/ n
- 23. J l[iS [i IEST STA[U3 ( P '? I O7 TO CU.HdR[C[ \\L G?E7 ATIC':) : FORC iST 2 C'-iE I VED IITIAL CdITICALIT/
I'!ITIAL ELECT 7ICITY CJ.:.!ER ICI AL OPE:2 ATIC'i l.15 - 9
APPENDIX DOCKET NO.
050-0325 UNIT Brunswick No. 1 DATE January 3, 1979 COMPLETED BY Eulis A. Willis BRUNSWICK NO. 1 Brunswick Unit No. I was available and producing 100% of the time for the reporting period.
The unit capacity factor for the same period was limited to 55% per the dispatchers request for fuel conservation in preparation for the upccming refueling outage (see Operating Data Report Item No. 24).
Brunswick Unit No. I has 154 PRR fuel assemblies in its storage pool.
Brunswick Unit No.1 also has 144 ERR fuel assemblies in its storage pool.
i APPEJUIX P AVE? AGE ' JAIL / PU'WP L'! VEL r"JC"ET l0. H1-0324 ij::IT SPU?:3'4ICT T!IT ?
DATE 91/02/79 Co.'.:PLET2D 3Y EULI; "!ILLI 5 TELEPiiG'!E V 1/-457-67'I JbCE. '.P ER 75 DAt A V '3. DAILY Ptr:ER LE/EL JAf WU. D AILY PG' EP L: VEL
( ;.'4E. NET )
(..t'"E-T ET )
I 230.
17 762.
2 420.
IJ 777.
3 3 't -
I ')
774 4
5
?.
2]
- 769, a
681.
21 765 0
767.
2?
764 7
770.
23 763.
o 776.
24 765.
/
53d.
25 762.
10 501.
26 759.
II 703.
27 759 12 79c.
23 749.
13 796.
29 749 I+
79 0.
30 735.
la 707.
31 603.
16 7e l.
1.15 - 3
OPERATIil3 UATt 7E? ORT n 0CET lC. H1-0324 DATE nl/02/79 Col'PLETEP 9f EULI S "'ILLIS TELEPHO'IE 91v-457-679I JPERATIt!G 5TATUS 1.
U '!I T.lA!.i E BRUT:SWICX UIIIT 2 I :lGTES I
2.
WEPORTIilG PERIOD: DECE'iBER 7d I
I
I 4
?JAl'EPLATE RATIf!G (GROSS '.P'E): d67.0 I
I
- 5. DESIG:1 ELECTRICAL RATItiG ( ?i E T.1'/!E ) : d21.0 I
I
- 5...t AX ud?E.lDABLE C APACITY (GROSS i'.E): 115.0 I I
7 MX DEPE.'lDA3LE CAPACITY (.'iET ir, E ) : 790.0 J.
IF CliA.lGES OCCUR I.P i C AP AC I TY R ATI.!GS (ITE'!S 3 THkU 7 ) SI' ICE LAST REP 07T, UIVE 7EAS0iid:
1 PO't.=R LE /EL To '> HICri HEST 7ICTED IF AN( ( 'IET 1"'E ) : "O'!E
- 10. iiEA30'IS FOR RESTI?ICTIO'I IF AIY:
THIS Y? TO CU'UL "0:ITH D ', T E ATIVE
- 11. riOU.?S Ii! REPORTING PERIOD 7d4.0 0763.1
?7721.0
- 12..iJ:.iBER OF HOURS REACTCR 7'AS CPITICAL 742.3 7321.3 1923J.2 IJ. REACTOR RESERVE SHUTD0'N HOURS 0.0 6.0 0.0 14 riJU.5 JE:IER ATOR O'l LIs!E 737.0 7922.0 1d129.0 Ia. J
? 'ESERVE SHUTDOf! 90JRS 0.0
'O 0.0 l1 JRG3S fri3RMAL c,iERG( GE'!E?ATEJ (..MH )
15doda1.4 14 72012.t. i 32447634.3 1~.
JRCSS ELECTRICAL Et!ERGY GE'!ER AfEu ' 4"9 )
540035.0 4967317.1 in816327.n J.
U:lli SERVICE FACTOR 99.1 d0.2 53.4
.? O. U'IIT AVAILABILITY FACTOR 99.I do.2 55.4
%.3 47.4
a
.5
- 23. JIIf FORCED QUTAGE RATE 0.9 a.7 15.1 24 5:iUTD.T::.15 SCHECULED GVER lEXT 5 JiiTHS (TYPE. DATE, A'!D DU;'ATIOi 0F EACH)*
Refuelingr79,02,18 1488.0 hours0 days <br />0 hours <br />0 weeks <br />0 months <br />
V 3/ 0 2a. J.iI f 5 I.! TESr STATUS (PRIOR TO COT'.ERICIiL OPE'ATIO:!): Fnm \\ST AC'.E I '/ E 0 I.llflAL CPITICALITY IIITIAL ELECTRICITY
=---
CO..iERICIAL OPERATtGN 1.li - 9
n 050-0324 UNIT SilUTDOWNS AND POWER REDUCrlONS DOCKET NO.
UNIT N AME Brunswick No. 2 DATE T,no,ry 1979 REPORT MONT11 December 1978 COMPLETED BY Eulis A. Willis TELEl'IlONE 457-6701 (919)
~.
E c
.!?
3
$ $2 Licensee E r,
{*3 Cause & Coracetive No.
Date 3
3g d
js&
Event gy A6 tion to go jE 5
y 5 ;2 Report #
mU H
o Prevent Recurrence e
v 6
033 781201 F
7.0 G
3 N/A CH Instru Reactor scram on low vessel level.
An I&C Tech was working a work re-quest on the steam flow recorder (C32-R006), which was pegged high.
When lead to recorder was lifted, the 3-element level control loop was opened. The feed pump level control ran the feed pumps back, causing the vessel level to drop to the scram set-point. A meeting was held by plant management with the technicians in-volved to review the scram and deter-mine measures to prevent recurrence.
The details of the scram will be re-viewed with all 1&C Technicians in training sessions.
I 2
3 4
F: Forced Reason:
Method:
Ex!nbit G - Instructions S: Scheduled A Equipment Failure (Explain) 1-Manual for Preparation of Data B-Maintenance of Test 2 Manual Scram.
Ent > Sheets for Licensee C Refueling 3 Automatic Scram.
Esent ReporI(LER) FileINURLG-D Regulatory Restriction 4 Other (Explain) 0161) 150perator Training & License Examination F Adnunistrative 5
G Operational Essor (Explain)
Estabit I-Same Source P3/77)
Il-Other (Explain)
CAUSE & CORRECTIVE ACTION TO PREVENT RECURRENCE (cont'd)
Feasibility of installing Zener diodes in some plant current loops will be investigated. The diodes would allow current to bypass an instrument when the loop is broken at the instrument. This is a carryover from a November outage.
APPENDIX DOCKET NO.
050-0324 UNIT Brunswick No. 2 DATE January 3, 1979 COMPLETED BY Eulis A. Willis BRUNSWICK NO. 2 Monthly availability for Brunswick Unit No. 2 was 99.1% with only one major power interruption for the entira month.
December 1: A technician error on 11-30-78 caused a reactor scram which lasted 7.0 hours0 days <br />0 hours <br />0 weeks <br />0 months <br /> into this reporting period.
The capacity factor for the month was 89%. For further 2xplanation of the outage,see the unit shutdown and power reduction log (Appendix D) for the month of December. Brunswick Unit No. I has no spent fuel in its pool at this time.