ML19254F906

From kanterella
Jump to navigation Jump to search
LER 79-046/03L-0:on 791011,noted That Sequence of Manual Switching of Primary Coolant Low Level Dew Point Moisture Monitors Can Result in Degraded Mode of Limiting Conditions for Operation.Sys Operating Procedure Revised
ML19254F906
Person / Time
Site: Fort Saint Vrain Xcel Energy icon.png
Issue date: 11/09/1979
From: Gahm J
PUBLIC SERVICE CO. OF COLORADO
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19254F895 List:
References
LER-79-046-03L, LER-79-46-3L, NUDOCS 7911190386
Download: ML19254F906 (1)


Text

NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION nm LICENSEE EVENT REPORT CONTROL BLOCK: l l l l l l l (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 6 MlC 7 8 9 l6lF l S l V I 1 l@l L CENSEE CODE 14 0 l 0 l - l 0 lLICENSE 15 0 l 0NUMBER l 0 l 0 l- l 0 l 025l@l26 4 l1LICENSE l 1 l:TYPEl 0JOl@l57 CAT l l@

58 CON'T 0 "' "

?

1 8

5OuRC l60L l@l61 0 l 5 lDOCKET 0 l 0NUM8ER l 0 l 2 l 6 l687 @l 69 1 lEVENT 011DATE l1 l 7 l 749 l@l111 75 l 0 DATE REPORT l 9 l 7 l809 l@

EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h O 2 lOn October 11, 1979, it was determined that due to procedural inadequacies, a parti- l 0 3 l cular sequence of manual switching of the primary coolant low level dew point moisture l o 4 l monitors could have resulted in a degraded mode of LCO 4.4.1. This is reportable per l o s i Fort St. Vrain Technical Specification AC 7.5.2(b)3. l 0 6 l l 0l7 l l 0 8 l 7 8 9 80 SYSTEM CAUSE CAUSE COMP. VALVE CODE CODE SUSCODE COMPONENT CODE SUSCODE SU8 CODE l0 7

9 8

l Il Bl@ W@ l Z l@ lIIJlN lS lT lR lU @ l Il@ l Zl@

9 10 11 12 18 19 20

,,, SEQUENTI AL OCCURRENCE REPORT REVISION LER RO EVENTYEAR REPORT NO. CODE TYPE N O.

O17 RE u l7 l9 l l-l l0 416l l/l l 01 3 l lLl l-l l0 l 21 22 23 24 26 27 28 29 30 31 32 AK N AC ON O PL NT E HOURS S8 i FOR 8. SUPPLI MANUFACTURER lGl@lZl@

33 34 lZl@

35 lZl@

36 l0 l0 0 l0 l 3/ 40 lY 41 l@ Nl@

42 lN 43 l@ y l0 l6 3j@

44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h i o l An approved field change notice (FCN 3738B) made the automatic trip on moisture l i i l monitor system failure a manual action and revised the logic to allow individual [

, 7 l moisture monitors to be tripped (rather than disabling by pairs) . However, if the

, 3 l correct switching sequence was not followed it was possible to lock out a moisture l 3 4 l monitor inadvertently. The system oeprating procedure was revised to prevent this  ;

7 8 p 9f m occurring. No further corr ivgggign is anticipated or required. 80 STATUS  % POWER OTHER STATUS DISCOVERY DISCOVERY CESCRIPTION 1 5 l El@ l 0 l 6 0 l@l N/A l Al@l Instrument Personnel Observation ACTIVITY CO TENT RELEASED OF RELEASE AMOUNT OF ACTIVITY LOCATION OF RELEASE 1 6

[_Z) h @l N/A l l N/A l 7 8 9 10 11 44 45 80 PERSONNEL EXPOSURES NUMBER TYPE CESCRIPTION 1 7 10]0l0l@lZl@lN/A l PERSONNEL INJURIES NUMBER DESCRIPTION 1 a l0l0l0l@lN/A _ . l LOSS OF OR O AGE TO FACILITY Q TYPE DESCRIPTION  %/

1 9 l Zl@l10 N/A 7 8 9 80 l Nl N/A

@ {h)))hb , N S NLY 2 o ISSUED @l DESCRIPTION/ , l llllllllllll l}

7 8 9 to 68 69 30 5

~

NAME OF PREPARER C PHONE: