05000270/LER-1979-005-03, /03L-0:on 790924,rod Block Gaseous Radiation Monitors Were Inoperable When Containment Isolation Valve on Monitor Return Line Failed Closed.Caused by Hole in Operator Diaphragm.Diaphragm Replaced

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/03L-0:on 790924,rod Block Gaseous Radiation Monitors Were Inoperable When Containment Isolation Valve on Monitor Return Line Failed Closed.Caused by Hole in Operator Diaphragm.Diaphragm Replaced
ML19253B694
Person / Time
Site: Oconee Duke Energy icon.png
Issue date: 10/10/1979
From: Lewis S
DUKE POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML16148A259 List:
References
LER-79-005-03L-02, LER-79-5-3L-2, NUDOCS 7910170247
Download: ML19253B694 (1)


LER-1979-005, /03L-0:on 790924,rod Block Gaseous Radiation Monitors Were Inoperable When Containment Isolation Valve on Monitor Return Line Failed Closed.Caused by Hole in Operator Diaphragm.Diaphragm Replaced
Event date:
Report date:
2701979005R03 - NRC Website

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IThe RB gaseous radiation monitors were rendered inoperable when a containment l o.:

,,,,, isolation valve on the monitors' return line failed closed. The valve was l repaired and the monitors were returned to service well within the times g

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other means for detecting RCS leakage were available. Therefore, this incident, ser

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, safety of the public were not endangered.

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iio i The valve failed due to a hole in its operator dic.phraga, which is believed

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. Jhe valve was tested to verify operability. The preventive maintenance pro-pg gram will be revised to review ES valves to identify those with diaphragms ineeding replacement.

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