05000267/LER-1979-024-03, /03L-0:on 790804,on Three Occasions Between 790804-16,total Primary Coolant Oxidants Exceeded 10 Ppm W/Core Average Outlet Temp Greater than 1,200 F.Caused by Dryer Bypass Resulting in Water Ingress to Core

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/03L-0:on 790804,on Three Occasions Between 790804-16,total Primary Coolant Oxidants Exceeded 10 Ppm W/Core Average Outlet Temp Greater than 1,200 F.Caused by Dryer Bypass Resulting in Water Ingress to Core
ML19253A578
Person / Time
Site: Fort Saint Vrain Xcel Energy icon.png
Issue date: 08/31/1979
From: Gahm J
PUBLIC SERVICE CO. OF COLORADO
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19253A577 List:
References
LER-79-024-03L, LER-79-24-3L, NUDOCS 7909100359
Download: ML19253A578 (1)


LER-1979-024, /03L-0:on 790804,on Three Occasions Between 790804-16,total Primary Coolant Oxidants Exceeded 10 Ppm W/Core Average Outlet Temp Greater than 1,200 F.Caused by Dryer Bypass Resulting in Water Ingress to Core
Event date:
Report date:
2671979024R03 - NRC Website

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60 61 COCKET NUM8ER 68 69 EVENT DATE 74 75 HEPoRT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEOUENCES h l Cn three occasions during the period August 4, 19 79, through August 16, 1979, total I

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primary coolant oxidants (sum of water, carbon monoxide, and carbon dioxide) ex-l o

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