RO 77-045:on 770916,found That Loss of Air Supply to Containment Bldg Purge Isolation Valves Will Result in Depressurization of Seal Rings.Caused by Valves Not Being Provided W/Redundant Supply to Maintain Seal Ring PressureML19249F014 |
Person / Time |
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Site: |
Palisades |
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Issue date: |
09/30/1979 |
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From: |
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.) |
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To: |
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References |
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NUDOCS 7910030538 |
Download: ML19249F014 (1) |
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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO
MONTHYEARML18054B0561989-10-23023 October 1989 Special Rept 89-TS2-00:on 890314,control Room Operators Identified That One Channel of Reactor Vessel Level Monitoring Sys Recorder Was Indicating Lower than Would Be Expected.Caused by Open Circuit within Thermocouple Heater ML20024E2531983-08-0202 August 1983 Telecopy Ro:On 830801,during Outage of Safety Injection Tank T-82D,safety Injection Tank T-82A Became Inoperable Due to Low Level.Simultaneous Outage of Tanks Lasted 4 Minutes. Tank T-82A Restored to Operability ML20024A6611983-06-13013 June 1983 Telecopy Ro:On 830610,safety Injection Tank C (T-82C) Became Inoperable Due to Low Level Resulting from Sampling. Caused by Lifting of Relief Valve.Low Level Switch Cleared ML20028E2351983-01-13013 January 1983 Ro:On 830112,safety Injection Tank T-82B Inoperable for Greater than 1 H.Addl Safety Injection Tank Appeared to Be Inoperable on Three Separate Occasions.Power Reduction Begun & Continued Until One Tank Restored ML20049H6851982-02-23023 February 1982 Ro:On 820203,SIRW Tank Level Determined Below Specified Limit.Evaluation of Event Rept Indicates That Apparent Low Level Resulted from Level Instruments Out of Calibr. Condition Not Reportable ML20039B0411981-12-11011 December 1981 Telecopy Mesage of Ro:On 811211,steam Leak Occurred Inside Containment Bldg.Cause Not Stated.Normal Cooldown Procedures in Progress ML18046A5641981-04-0101 April 1981 Ro:On 810331,safety Injection Tanks T81A & T81D Showed Levels Lower than Permitted by Tech Spec 3.3.1.B.Cause Not Stated.Level in T81A Was Restored in Approx 1 Minute ML18044A4201980-01-0909 January 1980 Ro:On 800109,pipe & Pipe Support Stress Analyses,Performed in Accordance W/Ie Bulletin 79-14,identified Several Lines Not Meeting FSAR Acceptance Criteria ML19208B8051979-09-30030 September 1979 Corrected Copy of RO 77-045:on 770916,found That Loss of Air Supply to Containment Bldg Purge Isolation Valves Will Result in Depressurization of Seal Bladders.Caused by Valves Not Being Provided W/Redundant Air Supply ML19249F0141979-09-30030 September 1979 RO 77-045:on 770916,found That Loss of Air Supply to Containment Bldg Purge Isolation Valves Will Result in Depressurization of Seal Rings.Caused by Valves Not Being Provided W/Redundant Supply to Maintain Seal Ring Pressure ML19208B8141977-12-16016 December 1977 RO 77-058:on 771125,during Normal Steady Operation,Bus R Became de-energized Causing Complete Loss of Offsite Power & Resulting in Loss of Main Condenser Cooling Water.Cause Unknown ML19208B8111977-10-18018 October 1977 RO 77-47:on 770924,during Electrical Storm,Bus R Was de-energized Causing Complete Loss of Offsite Power & Resulting in Loss of Main Condenser Cooling Water & Plant Trip.Cause Unknown.Tech Spec Change Will Be Made ML19208B8021977-05-0404 May 1977 RO 77-023:on 770419,waste Gas Decay Tank Lost 10 Psig While Isolated,Violating Tech Specs.Cause Unstated 1989-10-23
[Table view] Category:LER)
MONTHYEARML18054B0561989-10-23023 October 1989 Special Rept 89-TS2-00:on 890314,control Room Operators Identified That One Channel of Reactor Vessel Level Monitoring Sys Recorder Was Indicating Lower than Would Be Expected.Caused by Open Circuit within Thermocouple Heater ML20024E2531983-08-0202 August 1983 Telecopy Ro:On 830801,during Outage of Safety Injection Tank T-82D,safety Injection Tank T-82A Became Inoperable Due to Low Level.Simultaneous Outage of Tanks Lasted 4 Minutes. Tank T-82A Restored to Operability ML20024A6611983-06-13013 June 1983 Telecopy Ro:On 830610,safety Injection Tank C (T-82C) Became Inoperable Due to Low Level Resulting from Sampling. Caused by Lifting of Relief Valve.Low Level Switch Cleared ML20028E2351983-01-13013 January 1983 Ro:On 830112,safety Injection Tank T-82B Inoperable for Greater than 1 H.Addl Safety Injection Tank Appeared to Be Inoperable on Three Separate Occasions.Power Reduction Begun & Continued Until One Tank Restored ML20049H6851982-02-23023 February 1982 Ro:On 820203,SIRW Tank Level Determined Below Specified Limit.Evaluation of Event Rept Indicates That Apparent Low Level Resulted from Level Instruments Out of Calibr. Condition Not Reportable ML20039B0411981-12-11011 December 1981 Telecopy Mesage of Ro:On 811211,steam Leak Occurred Inside Containment Bldg.Cause Not Stated.Normal Cooldown Procedures in Progress ML18046A5641981-04-0101 April 1981 Ro:On 810331,safety Injection Tanks T81A & T81D Showed Levels Lower than Permitted by Tech Spec 3.3.1.B.Cause Not Stated.Level in T81A Was Restored in Approx 1 Minute ML18044A4201980-01-0909 January 1980 Ro:On 800109,pipe & Pipe Support Stress Analyses,Performed in Accordance W/Ie Bulletin 79-14,identified Several Lines Not Meeting FSAR Acceptance Criteria ML19208B8051979-09-30030 September 1979 Corrected Copy of RO 77-045:on 770916,found That Loss of Air Supply to Containment Bldg Purge Isolation Valves Will Result in Depressurization of Seal Bladders.Caused by Valves Not Being Provided W/Redundant Air Supply ML19249F0141979-09-30030 September 1979 RO 77-045:on 770916,found That Loss of Air Supply to Containment Bldg Purge Isolation Valves Will Result in Depressurization of Seal Rings.Caused by Valves Not Being Provided W/Redundant Supply to Maintain Seal Ring Pressure ML19208B8141977-12-16016 December 1977 RO 77-058:on 771125,during Normal Steady Operation,Bus R Became de-energized Causing Complete Loss of Offsite Power & Resulting in Loss of Main Condenser Cooling Water.Cause Unknown ML19208B8111977-10-18018 October 1977 RO 77-47:on 770924,during Electrical Storm,Bus R Was de-energized Causing Complete Loss of Offsite Power & Resulting in Loss of Main Condenser Cooling Water & Plant Trip.Cause Unknown.Tech Spec Change Will Be Made ML19208B8021977-05-0404 May 1977 RO 77-023:on 770419,waste Gas Decay Tank Lost 10 Psig While Isolated,Violating Tech Specs.Cause Unstated 1989-10-23
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18066A6901999-11-0101 November 1999 Rev 5 to Palisades Nuclear Plant Colr. ML18066A6761999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Palisades Nuclear Plant ML18066A6271999-09-0202 September 1999 LER 98-011-01:on 981217,inadequate Lube Oil Collection Sys for Primary Coolant Pumps Was Noted.Caused by Design Change Not Containing Appropriate Level of Rigor.Exemption from 10CFR50,App R Was Requested.With 990902 Ltr ML18066A6351999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Palisades Nuclear Plant ML18066A6771999-08-31031 August 1999 Operating Data Rept Page of MOR for Aug 1999 for Palisades Nuclear Plant ML18066A6221999-08-20020 August 1999 LER 99-002-00:on 990722,TS Surveillance Was Not Completed within Specified Frequency.Caused by Failure to Incorporate Revised Frequency Into Surveillance Schedule in Timely Manner.Verified Implementation.With 990820 Ltr ML18066A6061999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Palisades Nuclear Plant.With 990803 Ltr ML18066A5201999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Palisades Nuclear Plant.With 990702 Ltr ML18066A4841999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Palisades Nuclear Plant.With 990603 Ltr ML18066A6371999-04-30030 April 1999 Revised Monthly Operating Rept for Apr 1999 for Palisades Nuclear Plant ML18068A5941999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Palisades Nuclear Plant.With 990503 Ltr ML18066A4161999-04-0101 April 1999 Rev 4 to COLR, for Palisades Nuclear Plant ML18066A4501999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Palisades Nuclear Plant.With 990402 Ltr ML18066A4671999-03-31031 March 1999 Rev 0 to SIR-99-032, Flaw Tolerance & Leakage Evaluation Spent Fuel Pool Heat Exchanger E-53B Nozzle Palisades Nuclear Plant. ML18068A5351999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Palisades Nuclear Plant.With 990302 Ltr ML18066A3931999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Palisades Nuclear Plant.With 990202 Ltr ML18066A3781999-01-20020 January 1999 LER 98-013-00:on 981222,safeguards Transfer Tap Changer Failure Caused Inadvertant DG Start.Caused by Failed Motor Contactor.Contactor Was Replaced.With 990120 Ltr ML20206F6131998-12-31031 December 1998 1998 Consumers Energy Co Annual Rept. with ML18066A3651998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Palisades Nuclear Plant.With 990105 Ltr ML18066A3421998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Palisades Nuclear Plant.With 981202 Ltr ML18066A3301998-11-11011 November 1998 Part 21 Rept Re Potential Safety Hazard Associated with Wrist Pin Assemblies for FM-Alco 251 Engines at Palisades Nuclear Power Plant.Caused by Insufficient Friction Fit Between Pin & Sleeve.Supplier of Pin Will No Longer Be Used ML18068A4921998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Palisades Nuclear Plant.With 981103 Ltr ML18068A4851998-10-29029 October 1998 LER 97-011-01:on 971012,starting of Primary Coolant Pump with SG Temps Greater than Cold Leg Temps Occurred.Caused by Inadequate Procedures & Operator Decision.Sop Used for Starting Primary Coolant Pump Enhanced ML18066A3181998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Palisades Nuclear Plant ML18066A2901998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Palisades Nuclear Power Plant.With 980903 Ltr ML18066A3191998-08-31031 August 1998 Revised Monthly Operating Rept Data for Aug 1998 for Palisades Nuclear Plant ML18066A2831998-08-18018 August 1998 LER 98-010-00:on 980721,reactor Manually Tripped.Caused by Failure of Coupling Which Drives Feedwater Pump Main Lube Oil Pump.Main Lube Oil Pump Coupling & Associated Components Replaced & Satisfactorily Tested ML18066A2771998-08-13013 August 1998 Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency ML20237E0301998-07-31031 July 1998 ISI Rept 3-3 ML18066A2701998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Palisades Nuclear Plant.W/980803 Ltr ML18066A2311998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Palisades Nuclear Plant ML18066A2261998-06-30030 June 1998 LER 98-009-00:on 980531,small Pinhole Leak Found on One of Welds,During Leak Test Following Replacement of Pcs Sample Isolation Valves.Caused by Welder Error.Leaking Welds Repaired ML18066A3061998-06-18018 June 1998 SG Tube Inservice Insp. ML20249C4951998-06-17017 June 1998 Rev 1 to EA-GEJ-98-01, Palisades Cycle 14 Disposition of Events Review ML18066A1781998-06-0909 June 1998 LER 98-008-00:on 980511,noted That Procedure Did Not Fully Satisfy Requirement to Test High Startup Rate Trip Function. Caused by Misunderstanding of Testing Requirements.Revised TS Surveillance Test Procedure & Reviewed Other Procedures ML18066A1711998-06-0101 June 1998 Part 21 Rept Re Impact of RELAP4 Excessive Variability on Palisades Large Break LOCA ECCS Results.Change in PCT Between Cycle 13 & Cycle 14 Does Not Constitute Significant Change Per 10CFR50.46 ML18066A1741998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Palisades Nuclear Plant.W/980601 Ltr ML18066A2321998-05-31031 May 1998 Revised MOR for May 1998 for Palisades Nuclear Plant ML18068A4701998-05-31031 May 1998 Annual Rept of Changes in ECCS Models Per 10CFR50.46. ML18065B2451998-05-13013 May 1998 LER 98-007-00:on 980413,HPIS Sys Was Noted Inoperable During TS Surveillance Test.Caused by Performance of Flawed Procedure.Operators & Engineers Will Be Trained to Improve Operational Decision Making Through Resources & Knowledge ML18066A2331998-04-30030 April 1998 Revised MOR for Apr 1998 for Palisades Nuclear Plant ML18068A3461998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Palisades Nuclear Plant.W/980501 Ltr ML18066A3411998-04-22022 April 1998 Rev 0 to EMF-98-013, Palisades Cycle 14:Disposition & Analysis of SRP Chapter 15 Events. ML18065B2071998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Palisades Nuclear Plant.W/980403 Ltr ML20217C2741998-03-31031 March 1998 Independent Review - Is Consumers Energy Method (W Method) of Determining Palisades Nuclear Plant Best Estimate Fluence by Combining Transport Calculation & Dosimetry Measurements Technically Sound & Does It Meet Intent of Pts ML18066A2341998-03-31031 March 1998 Revised MOR for Mar 1998 for Palisades Nuclear Plant ML18068A3041998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Palisades Nuclear Plant.W/980302 Ltr ML18066A2351998-02-28028 February 1998 Revised MOR for Feb 1998 for Palisades Nuclear Plant ML18065B1641998-02-0505 February 1998 Rev 0 to Regression Analysis for Containment Prestressing Sys at 25th Year Surveillance. ML18067A8211998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Palisades Nuclear Plant.W/980203 Ltr 1999-09-30
[Table view] |
Text
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CORRECTD UCENSEE EVENT REPORT Palisades CONTROL BLOCK:l l l l l l l (pLEASE PRINT ALL REQUIRED INFORMATION) 1 6 UCENSEE UCENSE EVENT NAME UCENSE NUMSER TYPE TYPE loE 7 89 xlrl?IAlLl1l 14 lGl0l-l0l0l0l0l0l-l0l0l 15 25 l h l 1 l1l1l1l 26 30 l 0 l 1l 31 32 mEponT aEpenT TYPE SQURCE CCCXET NUMBER EVENT CATE AEPCRT DATE 01 CCNT l
- l lT l lLl l 0l 5 l 0l-l 0 l 2 l 5 l 5l l0! 9l1l6l7l7 l 0 l 912 l 9l 7l 7 7 8 57 58 59 60 61 68 69 74 75 80 EVENT CESCRIPTION Ql 7 89 Investigation has revealed that loss of the air supply to the antain=ent building 80 l
Ql 7 89 purge isolation valtes (CV-1803, -1805, -1806, -1807, -1813 ant. -181h) vill result 80 l
hl in decressurizatien of thh s6rinesDeh eculd cause _ ss of containment intec ityl o5 "his failure node had not cea . in the FSAR. Seal tressures are beine 7 89 80 6 l Checked once per shift to verify operability of seal ri*ng air Sunply. (ER-77-Oh5) l 7 89 pseat corrected 80 SYsitM CAUSE COMpOMNT COMACNENT CoCa CecE CCupoNENT CCat supptan um;rACrunca votATioN 07 l Sl Dl W lVl Al LlVl Ej Xl l Al lCl5l8l7 [p_j 7 89 10 11 12 17 43 44 47 48 CAUSE CESCRIPTION gl The valves (Continental Equip / Type 9220) are not provided with a redundant air l 7 89 80 C9 l surply to naintain seal ring pressure.
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A redundant air source will be provided as l 7 89 80
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ufTwoo cF 80 STA'US % POWEA CTHER STATUS OtSCOVERY CISCOVERY CESCAlPTICN 11 l1l 0l 0l l N/A l d45 N/A l 7 8 9 10 12 13 44 48 80 CCRTENT RELEASE 0 AMOUNT CF ACTlVfTY LCCATCN CF RELEASE 12 d CFdRELEASE N/3 l l l N/a l 7 8 9 10 11 44 45 80 PERSONNEL EXPOSURES NUMBER TYPE CESCAIPT1CN 3 l0l O! 0l l Zl l N/A l 7 89 11 12 13 , eo PERSONNEL INJUA;ES CESCATpT10N D.: 0
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ao FR02A3LE CONSEO.UETCES h; l 15 l N/A J 'J L U ~' 'l ' [ [ . /, (d) / /
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