ML19249E746

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Forwards IE Bulletin 79-13,Revision 1, Cracking in Feedwater Sys Piping. No Action Required
ML19249E746
Person / Time
Site: Waterford Entergy icon.png
Issue date: 08/30/1979
From: Seyfrit K
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To: Aswell D
LOUISIANA POWER & LIGHT CO.
References
NUDOCS 7910020326
Download: ML19249E746 (1)


Text

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9 August 30, 1979 In Reply Refer To:

RIV Docket No.

50-382/IE Bulletin No. 79-13, Revision 1 Louisiana Power and Light Co.

ATTN:

Mr. D. L. Aswell Vice President of Power Production 142 Delarcade Street New Orleans, Louisiana 70174 Gentlemen:

IE Bulletin 79-13 was originally sent to you for action on June 27, 1979.

The enclosed IE Bulletin 79-13, Revision 1 is forwarded to you for information.

No written renponse is required. This Revision is being dispatched for action to the additional Utilit.ies, listed in Enclosure 3, who are applicants for operating licenses.

If you desire additional information regarding this matter, please contact this office.

Sincerely, Q(f

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r1 V. S yfrit' Director

Enclosures:

1.

IE Bulletia No. 79-13, Revision 1 2.

List of IE Bulletins Issued in Last Six Months 3.

Designated Applicants for Operating Licr.nses

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  • 03 p 91 p

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UNITED STATES NUCLEAR REGULATORY COMMISSION OFFICE OF INSPECTION AND ENFORCEMENT WASHINGTON, D.C.

20555 IE Bulletin No. 79-13 Revision 1 Date: August 30, 1979 Page 1 of 4 CRACKING IN FEEDWATER SYSTEM PIPING Description of Circumstances:

On May 20, 1979, Indiana and Michigan Power Company notified the NRC of cracking in two feedwater lines at their D. C. Cook Unit 2 facility. The cracking was discovered following a shutdown on May 19 to investigate leakage inside containment.

Leaking circumferential cracks were identified in the 16-inch feedwater elbows adjacent to two steam generator nozzle elbow welds.

Subsequent radiogr:phic examination revealed crack indications in all eight steam generator feedwater lines at this location on both Units 1 and 2.

On May 25, 1979, a letter was sent to all PWR licensees by the Office of Nuclear Reactor Regulation which informed licensees of the D. C. Cook failures and requested specific information on feedwater system design, fabrication, inspection and operating histories.

To further explore the generic nature of the cracking problem, the Office of Inspection and Enforcement requested licensees of PWR plants in current outages to immediately conduct volumetric examination of certain feedwater piping welds.

As a result of these actions, several other licensees with Westinghouse steam generators reported crack indications.

Southern California Edison reported on June 5, 1979, that radiographic examination revealed indications of cracking in feedwater nozzle-to-piping welds on two of three steam generators of San Gnofre Unit 1.

On June 15, 1979, Carolina Power and Light reported that radiography showed crack indications in similar locations at their H. B.

Robinson Unit 2.

Duquesne Power and Light confirmed on June 18, 1979, that radiography has shown cracking in their Beaver Valley Unit 1 feedwater piping to vessel nozzle weld.

Public Service Electric and Gas Company reported on June 20 1979, that Salem Unit I also has crack indications. Wisconsin Public Service Company decided on June 20, 1979, to cut out a feedwater nozzle-to pipe weld which contained questionable indication, for metal.'urgical examination.

As of June 22, 1979, and since May 25, 1979, seven other PWR facilities have inspected the feedwater nozzle-to-pipe welds without finding cracking indications.

fng. h 4 A ol m A-M M s - v; The feedwater nozzle-to pipe configuraHnne a

are shown on the attached Figures 1 ke

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weld joint detail showing the princi DUPLICATE DOCUMENT Onofre are shown on the attached Figi Entire document previously entered into system under:

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DESIGNATED APPLICANTS FOR OPERATING

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LICENSES Salem 2 North Anna 2 Diablo Canyon 1 & 2 Sequoyah 1 McGuire. 1 San Onofre 2 Summer Watts Bar 1 & 2 4.

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