ML19241B537
| ML19241B537 | |
| Person / Time | |
|---|---|
| Site: | Oconee |
| Issue date: | 05/30/1979 |
| From: | Parker W DUKE POWER CO. |
| To: | James O'Reilly NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| References | |
| NUDOCS 7907180883 | |
| Download: ML19241B537 (2) | |
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DuIin POWEIZ COMPANY, f
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May 30, 1979
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i Mr. James P. O'Reilly, Director U. $. Nuclear Regulatory Commission Regfon II 101 Marietta Street, Suite 3100 Atlantn, Georgia 30302 Re:
RII:JPO 50-269 50-270 50-287
Dear Mr. O'Reilly:
With regard to your letter of March 30, 1979 and my letter of May 2, 1979, please find attached Duke Powar Company's response to IE 'Bulletin 79-04 for Oconee Nuclear Station.
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William O. Parker, Jr.
RLG:ses Attachment cc:
U. S. Nuclear Regulatory Commission Office of Inspection and Enforcement Division of Reactor Construction Inspection Washington, D. C.
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DUKE POWER COMPANY OCONEE NUCLEAR STATION Response to IE Bulletin 79-04 Duke Power Company has reviewed all Seismic Category I piping sysyees and has 1500 psi Velan check valves were installed in thei-inch dis-3 determined that charge line of each high pressure injection (HPI) pump of each Ocypee unit.
- c. these lines.
An.3ncorrectvalveweightwasusedinthepipinganalysis A teanalysis of the affected HPI piping has been initiated to determine if additional supports or restraints are required.
The computer code SUPERPIPE is being utilized in this analysis.
A report will be submitted upon completion of this analysis, which is expected to be completed by June 29, 1979.
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