ML19224C653
| ML19224C653 | |
| Person / Time | |
|---|---|
| Site: | Fort Calhoun |
| Issue date: | 06/07/1979 |
| From: | Seyfrit K NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV) |
| To: | Short T OMAHA PUBLIC POWER DISTRICT |
| References | |
| NUDOCS 7907060020 | |
| Download: ML19224C653 (1) | |
Text
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UNITED STATES PDR:HQ NUCLEAR 9EGULATORY COMMISSION ra 3,
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REGION IV E
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ARLINGTON, TEX AS 76012
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June 7, 1979 fucket No.
50-285 Omaha Public Power District ATTN:
T. E. Short, Assistant General Manager 1623 Harney Street Omaha, Nebraska 68102 Gentlemen:
This Information Notice is provided as an early notification of a possibly significant matter. It is expected that recipients vill review the information for possible applicability to their facilities.
No specific action or response is requested at this tiue.
If further URC evaluations so indicate, an IE Circular, Bulletin, or NRR Generic Letter will be issued to recommend or request specific licensee actions.
If you have questions regarding this matter, please contact the Director of the appropriate NRC Regional Office.
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Karl V. Sey it Director
Enclosures:
1.
IE Information Notice No. 79-15 2.
List of IE Information Notices Issued in 1979 cc:
R. L. Andrews, Manager Fort Calhoun Station Post Office Box 98 Fort Calhoun, Nebraska 68102 o n,-
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,j 79070000 26
UNITED STATES NUCLEAR REGULATORY C0fLMISSION OFFICE OF INSPECTION AND ENFORCEMENT WASHINGTON, D.C.
20555 IE Information Notice No.'79-15 Date: June 7, 1979 Page 1 of 3 DEFICIENT PROCEDURES Summary On June 2, 1979, at Arkansas Nuclear One - Unit 1, while observing conditions in the control room, an NRC inspector discovered an operational deficiency that could have rerulted in
,e eme;gncy fee nter system remaining isolated during subsequent power ope..
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Description of Circumstad es On June 2 while Arkansas Nt -T u See Unit 1 was preparing for startup, an NRC inspector in the coutrot m.c four.d that during a surveillance test of the main feedwater checi ve "es, the controls of the emergency feedwater 8
system were positioned so tnat the syste,could not automatically respond if needed. The NRC inspector found that the test procedure being used by the licensed operators did not include, as it should have, instructions either to bypass the emergency feedwater system or to return it to normal.
The plant operators, without approved procedures covering this aspect of the test, bypassed the controls that would have started the feedwater system automatically. Lacking a procedural requirement to return the system to normal, there was no assurance that emergency feedwater would be provided automatically if needed.
Following the Three Mile Island accident, the NRC required that operators be trained to initiate promptly the emergency feedwater system manually if it does not come on automatically. Thus, while no immediate safety hazard existed at the Arkansas Unit 1 plant because of the improper action, the NRC staff is concerned about the potential safety hazard of leaving the emergency feedwater system in the bypassed condition, about the possibility that other procedures at the Arkansas plant may be deficient and about the fact that the operators deviated from procedures in performing the surveillance test.
Arkansas Power and Light Company has returned the plant to cold shutdown.
The June 2, 1979, NRC Order confirmed the requirement for a cold shutdown until the Commission staff is satisfied with the utility's method of con-trolling the development of operating procedures, the adequacy of existing procedures, and until there is assurance that operators will not deviate from those procedures.
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