ML19224C587
| ML19224C587 | |
| Person / Time | |
|---|---|
| Site: | FitzPatrick |
| Issue date: | 05/29/1979 |
| From: | Grier B NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | Leonard J POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK |
| References | |
| NUDOCS 7907030049 | |
| Download: ML19224C587 (1) | |
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[g UNITED STATES
! }M.[ d, efi NUCLEAR REGULATORY COMMISSION j
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KING OF PRUSSI A, PENNSYLV AN6A 1930G May 29, 1979 Docket No. 50-333 Power Authority of the State of New York James A. FitzPatrick Nuclear Power Plant ATTN:
Mr. J. D. Leonard Resident Manager P. O. Box 41 Lycoming, New York 13093 Gentlemen:
This Infornation Notice is provided as an early notificatior of a possibly significant matter.
It is expected that recipients will review the information for possible applicability to their faci ties.
No specific act@on or response is requested at this time.
If further NRC evaluations so indicate, an IE Cir-cular or Bulletin will be issued to recommend or request specific licensee actions.
If you have questions regarding this matter, please contact the Di.ector of the appropriate NRC Regional Office.
Sincerely,
/ h m.-
Boyce H. Grier Director
Enclosures:
1.
IE Information Notice No. 79-13 w/ enclosures 2.
List of Information ;lotices Issued in 1979 cc w/encls:
George T. Berry, Executive Director P. W. Ljon, Manager - Nuclear Operations A. Klausmann, Director, Quality Assurance M. C. Cosgrove, Quality Assurance Supervisor J. F. Davis, Chairman, Safety Review Ccmmittee L. R. Bennett, Assistant General. Manager - General Counsel G. M. Wilverding, Licensing Supervisor 272 309 790703009'?
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UNITED STATES NUCLEAR REGULATORY COMMISSION OFFICE OF INSPECTION AND ENFORCEMENT WASHINGTON, D.C.
20555 IE Information Notice No. 79-13 Date: May 29, 1979 Page 1 of 4 INDICATION OF LOW WATER LEVEL IN THE OYSTER CREEK REACTOR Sumary A loss of feedwater transient at the Oyster Creek facility on May 2, 1979, resulted in a significant reduction in water inventory within the reactor core shroud area as measured by one set of water level instrumen'.s (triple low level),
while the remaining level instrum its, sensing from the reactor annulus area indicated water levels above any protective feature setpoint (Figure 1). The water level within the ccre shroud area was reduced below the " triple low level" setpoint of 4-feet, 8-inches above the top of the fuel.
Subsequent analysis by the licensee has determined that the minimea collapsed water level (solid, without steam voids) over the top of the fuel was 1 to 1-1/2 feet.
Coolant sample analyses and offgas release rates indicate that no fuel damage occurred.
General Oyster Creek is a non-jet pump BWR with licensed power of 1930 MWt.
The plant was first made critical May 3, 1969.
Status Before Transient Operating at near full power with the main parameters at levels as follows:
1895 MWt power level 79" Yarway (13'4' over top of fuel) reactor water level 1020 p 7.1x10gigreactorpressure
- /hr feed flow 14.8x104 gpm recirculation flow rate (4 pumps) 12 psid core op Equipment Out of Service (00S)
"D" recirc pump 005 due to seal coole -
"B" startup transformer 00S for inspe DUPLICATE DOCUMENT l-3IU Entire document previously entered into system under:
~J9dfd[p ((d No. of pages:
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