ML19211A282

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LER 79-110/03L-0:on 791112,while Testing HPI Pump 1-1 in Mode 5,pump Failed to Start.Caused by Improperly Terminated Lug in Breaker Control Wiring.Lead Properly Terminated & Reinstalled
ML19211A282
Person / Time
Site: Davis Besse Cleveland Electric icon.png
Issue date: 12/11/1979
From: Naylor R
TOLEDO EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML19211A277 List:
References
LER-79-110-03L, LER-79-110-3L, NUDOCS 7912170309
Download: ML19211A282 (2)


Text

i U. S. NUCLEAR REGULATORY COMMISSION NRC FORlW3GG (7 77) .,

LICENSEE EVENT REPORT CONTROL BLOCK: l l l l l l l (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 6 f5Til 10 IH ID IB IS 11 l@l el o -l ol LICENSE Of NI rl Pi -I ol 3I@l4 25 26 1LICENSE l1 l1TYPE l1l@l JO l l@

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) 8 9 LICENSEE CODE CON'T o i SO R$ l L j@l 0 l 5 l 0 l- l0 l 3l 468l 669@l llEVENT 1] DATE 1l 2l 7l 9@l1 74 75 l 2REPORT l1 l1 l 7 l980l@

DATE 7 8 60 64 OOCKET NUYBER EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h 1012 ] l On 11/12/79 while testing High Pressure Injection (HPI) Pump 1-1, it failed to start. l in the control circuit wiring. l l o l3 l l This lead to the identification of a factory defect o 4 l The unit was in Mode 5, and HPI Pump 1-2 was operable during the period that HPI 1-1 loisj was inoperable. There was no danger to the health and safety of the public or to o o l station personnel. HPI l-2 was operable during the period that HPI 1-1 was inopera- l o 7 ble and capable of supplying water to the core in the event of a safety features l l

Io 1e 1 l actuation. (NP-33-79-127) ,

80 SU8 DE SU E lo!91 C DE CCDE SU8C E l S j F lg lB lg lB lg l Cj Kl Tj Bl Rl Klg ]g COMPONENT CODE 20 g

12 13 18 19 7 8 9 10 11 R EVislON SEQUEN TI AL OCCURRENCE REPORT CODE TYPE N REPORT NO.

LE R/RO _ EVENT YEAR O sgic; a a 17 19 l l-l l1 l1 l0 l y l0l3l ] l_]

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33 34 3 dh J6 3l1 NI Nl Ol40 OllY lh di Wh l3Ag 42 4 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS i o l The cause was due to an improperly terminated lug in the breaker control wiring which; The condition was aggravated by modification work being l 11 11 1 ] caused a bad connection.

Under MWO 79-3522, th9 l1 I2l l done for the arc suppression for the breaker control circuits.

HP1 Pump 1-1 was returned to operabi- [

)il3) Llead was properly terminated and reinstalled.

_ li 141 l lity at 1327 hours0.0154 days <br />0.369 hours <br />0.00219 weeks <br />5.049235e-4 months <br /> on 11/13/79. 80 7 8 9 oTHER STATUS IS O RY DISCOVERY DESCRIPTION ST S NPOAER

[ R l_D_j@ l0l0l0l@] NA l l C [gl Test af ter modification l ACTIVITY CON TE NT LOCATION OF RELEASE RELEASED OF hELEASE AMOUN r OF ACTIVITY l NA l l

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PERsONNEt ExPOsMES NUMBER TYPE DESCRIPTION NA l L'_LUl0101Ol@lZl@l PERSONNE L INJU IES NUVBEn D ESC rip TION j l i o elel@l i a NA OSS OF OR D AGE TO FACILITY g TYPE DESCRIPTION

~ W l Zl@l 7 8 9 to NA NRC USE ONLY ISSUE DESCRIPTION 79121 70307 l ll lllllll llj 7

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[_Nhl 10 NA 68 69 80 5 Richard W. Naylor PHONE: 419-259-5397 {

DVR 79-1 ,6 NAME OF PREPARER

3

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TOLEDO EDISON COMPANY DAVIS-BESSE NUCLEAR POWER STATION UNIT OIE SUPPLDENTAL INFORMATION FOR LER NP-33-79-127_

DATE OF EVENT: November 12, 1979 FACILITY: Davis-Besse Unit 1 IDENTIFICATION OF OCCURRENCE: High Pressure Injection Pump 1-1 failed to start dur-ing special testing Conditions Prior to Occurrence: The unit was in Mode 5, with Power (MNT) = 0, and Load (Gross MWE) = 0.

Description of Occurrence: On November 12, 1979 while testing High Pressure Injection (HPI) Pump 1-1 af ter a modification for surge suppression in the cubicle, HPI Pump 1-1 failed to start. Maintenance personnel stopped the test and commenced trouble-shooting. This lead to the identification of a factory def ect in the control circuit wiring. A lead had been improperly stripped prior to the lug being crLaped, thus the lead was insulated rather than the wire being crimped in the termination lug.

The unit was in bbde 5, and HPI Pump 1-2 was operable during the period that HPI l-1 was inoperable.

Designation of Apparent Cause of Occurrence: The cause of the occurrence was due to an improperly terminated lug in the breaker control wiring which caused a bad connec-tion. The lug was crimped to the lead insulation rather than the wire. This was due to improper insulation removal when the cabinet was manufactured. The' condition was aggravated by the modification work which caused wires in that area to be moved which caused the discontinuity in that circuit. This modification work was being done for the arc suppression for the breaker control circuits.

Analysis of Occurrence: There was no danger to the health and safety of the public or to station personnel. HPI 1-2 was operable during the period that HPI l-1 was inoperable and capable of supplying water to the core in the event of a safety features actuation.

Corrective Action: Under Maintenance Work Order 79-3522, the lead was properly ter-minated and reinstalled. The breaker was cycled several times and placed back to the i original position and the pump started. Following the~ work, all testing for the arc suppression was completed, and the unit returned to operability at 1327 hours0.0154 days <br />0.369 hours <br />0.00219 weeks <br />5.049235e-4 months <br /> on November 13, 1979. Wiring within the cabinet was inspected, and no other improperly crimped wires were found.

Failure Data: No previously similar occurrences have been identified or reported.

LER #79-110 1592 230