05000267/LER-1979-051-03, /03L-0:on 791017,at 5% Power,Sys 21 Loop 1 Surge Tank Level Decreased to Low Level Setpoint,Tripping Loop 1 Bearing Water Pumps & Making Circulators Inoperable.Caused by Procedural Inadequacy & Operator Error

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/03L-0:on 791017,at 5% Power,Sys 21 Loop 1 Surge Tank Level Decreased to Low Level Setpoint,Tripping Loop 1 Bearing Water Pumps & Making Circulators Inoperable.Caused by Procedural Inadequacy & Operator Error
ML19210E329
Person / Time
Site: Fort Saint Vrain Xcel Energy icon.png
Issue date: 11/16/1979
From: Gahm J
PUBLIC SERVICE CO. OF COLORADO
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19210E328 List:
References
LER-79-051-03L, LER-79-51-3L, NUDOCS 7912040341
Download: ML19210E329 (1)


LER-1979-051, /03L-0:on 791017,at 5% Power,Sys 21 Loop 1 Surge Tank Level Decreased to Low Level Setpoint,Tripping Loop 1 Bearing Water Pumps & Making Circulators Inoperable.Caused by Procedural Inadequacy & Operator Error
Event date:
Report date:
2671979051R03 - NRC Website

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60 61 DOCKET NUM8ER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h

['o'TTl l on october 17, 1979, while operating at 5% reactor power, System 21 Loop 1 surge tank o

o a l level decreased to the low level trip setpoint which tripped the Loop 1 bearing water l l pumps, making Loop 1 circulators inoperable per Fort St. Vrain Technical Specification l o

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