LER-1979-053, /03L-0:on 791024,total Primary Coolant Oxidants Exceeded 10 Parts Per Million.Caused by off-gassing of Oxidants Due to Reaction of Moisture W/Core Graphite.Power Decreased to Initiate Maint Shutdown |
| Event date: |
|
|---|
| Report date: |
|
|---|
| 2671979053R03 - NRC Website |
|
text
.
REPORT DATE:
November 1% 1979 REPORTABLE OCCURRENCE 79-53 ISSUE O OCCURRENCE DAIE:
Octob er 24, 1979 Page 1 of 4 FORT ST. VRAIN NUCLEAR GENERATING STATION PUBLIC SERVICE COMEANY OF COLORADO 16805 WELD COUNTY ROAD 191/2 PLATTEVILLE, COLCRADO 80651 REPORT NO. 50-267/ 79-5 3/03-L-0 Final IDENTIFICATON OF OCCURRENCE:
At approximately 1730 hours0.02 days <br />0.481 hours <br />0.00286 weeks <br />6.58265e-4 months <br /> on October 24, 1979, with average core outlet temperature greater than 1,200*F, total primary coolant oxidants (the sum of water, carbon dioxide, and carbon conoxide) exceeded ten parts per million.
This constitutes operation in a degraded mode of LCO 4.2.10 and is reportable per Fort St. Vrain Technical Specification AC 7.5.2(b)2.
EVENT
DESCRIPTION
On October 24, 1979, with total orimary coolant oxidants at less than 10 parts per million reactor power was being increased in preparation for approved fluctu-ation testing. At approximately 1600 hours0.0185 days <br />0.444 hours <br />0.00265 weeks <br />6.088e-4 months <br /> average core outlet temperature exceeded 1,200*F.
The total of primary coolant oxidants at that time was approxi-mately 7.5 parts per million. Following the reactor power increase to approxi-mately 60%, primary coolant oxidants began to follow an upward trend. At approxi-mately 1730 hours0.02 days <br />0.481 hours <br />0.00286 weeks <br />6.58265e-4 months <br />, primary coolant oxidant levels exceeded ten parts per million (reference Figure 1, point 1). During the period of fluctuation testing, average core outlet temperature remained above 1,200*F and total oxidants continued to increase.
Fluctuation testing was completed at 2230 hours0.0258 days <br />0.619 hours <br />0.00369 weeks <br />8.48515e-4 months <br /> on October 25, 1979, and an orderly shutdewn was initiated for plant =sintenance.
Core outlet temperature was less than 1,200*F by 0600 hours0.00694 days <br />0.167 hours <br />9.920635e-4 weeks <br />2.283e-4 months <br /> on October 26, 1979, (reference Figure 1, point 2) and to further LCO 4.2.10 degraded mode operation occurred.
CAUSE
DESCRIPTION:
The increase in total oxidants is due in part to off-gassing of carbon =enoxide and carbon dioxide as residual primary coolant moisture reacted with the core graphie.e at increased temperatures.
1A72 246 f
7012040h'
REPORTABLE OCCURRENCE 79-53 ISSUE O Page 2 of 4 CORRECIIVE ACTION:
Following completion of fluctuation testing at approximately 2230 hours0.0258 days <br />0.619 hours <br />0.00369 weeks <br />8.48515e-4 months <br /> on Octo-ber 25,1979, orderly reactor shutdown was initiated.
Core outlet temperature was less than 1,200
- F. by approximately 0600 hours0.00694 days <br />0.167 hours <br />9.920635e-4 weeks <br />2.283e-4 months <br /> on October 26, 1979, and no further degr'aded mode operation was observed.
No further corrective action is anticipated or required.
1A72 A7
FIGURE 1: AVERAGE CORE OUTLET TEMPERATURE VERSUS PRIMARY COOLANT OXIDANTS 1350-40
~
38 CORE OUTLET TEMPERATURE 36 34
- - 32 a
~
1300 30
- - 28 TOTAL OXIDANTS
~
26
^
[
24 m
22 H
x 1
cb y
1250-20 e
m E
18 5 C
x 5
C c
- - 16 E
0 H
- - 14 s
Ex 12 1200 '
10 8
6 4
2 1150 0
0000 0000 0000 0000 10/24 0/25 10/26 10/27 D*9 0
T 9
g
,j, DATE/ TIME a
REPORTABLE OCCURRENCE 79-53 ISSUE O Page 4 of 4 Prepared by:
'r 4 2M Cathy (C[ H1'rsch T
Techni'chl Services TechniciXn
/
///
c ///
/; su Reviewed by:
- 7. W. gahm' kechnical Services Supervisor Reviewed by:
Frank M. Mathie Operations Manager Approved by:
7}7m Don Warembourg
/
Manager, Nuclear Production 1472 ;49 O
NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSIUN (7*77 T LICENSEE EVENT REPORT CONTROL BLOCK: l l
l l
l l lh (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 6
@ lC l0 l F l S l V l 1 l@l 0 l 0 l-l 0 l 0 l 0 l 0 l 0 l-l0 l 0 l@l 4l ll 1l2 l 0 l@l l
l@
7 8 9 LICENSEE CODE 14 15 LICENSE NUM8ER 25 26 LICENSE TYPE JO 57 CAT 58 CON'T ERC lL @l0l5l0l0 0 l 2 l 6 l 7 @l 1 ' O l 2 l 4 l 7 l 9 l@l 1 l 1 11 l 9 l 7 9l@
"T o
1 7
8 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT OESCRIPTION AND PROSABLE CONSEQUENCES h o
2 l At approximatelv 1730 hours0.02 days <br />0.481 hours <br />0.00286 weeks <br />6.58265e-4 months <br /> on October 24. 1979. with averace core outlet temperature 1 o a j greater than 1,200*F, total primary coolant oxidants exceeded 10 parts per million.
l l This is operation in a degraded mode of LCO 4.2.10 and is reportable per Technical o
4 o
s l Specification AC 7.5.2(b) 2.
No affect on public health and safety.
Similar occur-l o e l rences reported in RO's 77-36, 78-12, 78-18, 78-37, 78-39, 79-01, 79-02, 79-24, 79-30,1 oi7 land 79-45.
I l
o a
80 7
8 9 E
CODE SL8C E COMPONENT CODE SUSCODE SU
.3 E l C l 8 l@ [J_j@
Zl@
Z IZ l Z l ZI Zl ZI@ LZ_j@ l Z i @
o 9
7 8
9 10 11 12
'J 18 19 20 SEQUENTI#6 OCCURRENCE REPORT REVISION LE R'RO EVENT YE A R R EPORT P.O.
CODE TYPE N O.
@ yu RE 7 l9 l l-l l0 l513 l l/l l 01 3 l lL l-l 0l
,_ 21 22 23 24 26 27 28 29 10 31 32 K N A O
Q PL NT MET HOURS 22 58 1 POR B.
SUPPLI E MANUFAC RER IXl@lZl@
lZl@
l Z l@
l 0 10 l 0 l 0 lY l@
l Nl@
l Zl@
lZ Z l Z l Z [@
33 34 35 36 31 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h l Cause. of occurrence was off-aassing of oxidants due to reaction of moisture with core '
i o
W graphite. When power was decreased to initiate maintenance shutdown _, no further de-l graded mode operation occurred.
l 7
1 3
l I
l I
i A
7 8 9 80 SA
% POWER OTNER STATUS DIS O RY DISCOVERY DESCRIPTION Xl@ l0 l 6 l 0 l@l N/A l
l Z l@l Personnel Observation l
i s
ACTIVITY CO TENT RELEASED OF RELEASE AMOUNT OF ACTIVITY LOCATION OF RELEASE
@ l d@l N/A l
l N/A l
1 16 7
8 9 10 11 44 45 80 PERSONNEL EXPOSUR ES NUM8ER TYPE
DESCRIPTION
1i7 [_0l0l0l@lZl@lN/A l
(
PERSONNP RIES NUM8ER L FURIPT1CN l 0] 0 l Ol@i N/ A 1
a 7
8 9 11 12 30 LOSS OF OR OAMAGE TO FACILITY
"@i iTI' ~
QqLuf V$3M i
="
i i
e 7
8 9 10 30 e
DE CRIPTION ISSUSEL 81 N/A l
llllllIll{l llj 2
o NAME CF PREPARER PHONE:
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000267/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000267/LER-1979-001-03, /03L-0 on 790102:total Primary Coolant Oxidant Concentration Exceeded 10 Vol Ppm While Core Average Outlet Temp Was Greater than 1200 F.Caused by Low Temp Absorber Heatup,Releasing Oxidant to Primary Coolant | /03L-0 on 790102:total Primary Coolant Oxidant Concentration Exceeded 10 Vol Ppm While Core Average Outlet Temp Was Greater than 1200 F.Caused by Low Temp Absorber Heatup,Releasing Oxidant to Primary Coolant | | | 05000267/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000267/LER-1979-002-03, /03L-0 on 790127:operation in Degraded Mode Resulted from Repairs to Seat of Buffer Helium Purge Valve. Bypass of Buffer Helium Dryer Caused by Leakage Past Valve Seat Insert of Velan Model P-33876-N/78R Valve | /03L-0 on 790127:operation in Degraded Mode Resulted from Repairs to Seat of Buffer Helium Purge Valve. Bypass of Buffer Helium Dryer Caused by Leakage Past Valve Seat Insert of Velan Model P-33876-N/78R Valve | | | 05000267/LER-1979-004-03, /03L-0 on 790203:during Normal Operation,Cooling Tower Blowdown Exceeded Limit But Was Not Reported.Caused by Incorrect Completion of Surveillance Forms.Forms Changed & Personnel Instructed | /03L-0 on 790203:during Normal Operation,Cooling Tower Blowdown Exceeded Limit But Was Not Reported.Caused by Incorrect Completion of Surveillance Forms.Forms Changed & Personnel Instructed | | | 05000267/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000267/LER-1979-005-03, /03L-0 on 790209:during Semiannual Loss of Outside Electrical Power Test,Output Circuit Breaker Did Not Close.Cause Unknown.Breaker Replaced W/Equivalent Spare | /03L-0 on 790209:during Semiannual Loss of Outside Electrical Power Test,Output Circuit Breaker Did Not Close.Cause Unknown.Breaker Replaced W/Equivalent Spare | | | 05000267/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000267/LER-1979-013, Forwards RO 50-267/79-13/03-L-O & LER 79-013/03L-0 | Forwards RO 50-267/79-13/03-L-O & LER 79-013/03L-0 | | | 05000267/LER-1979-013-03, /03L-0 on 790412:during Test of Snubbers Many Found Inoperable Due to Unacceptable Lockup & Bleed Characteristics.Caused by Setpoint Drift,Dirty Oil & Clogged Valves.All Snubbers Repaired & Adjusted | /03L-0 on 790412:during Test of Snubbers Many Found Inoperable Due to Unacceptable Lockup & Bleed Characteristics.Caused by Setpoint Drift,Dirty Oil & Clogged Valves.All Snubbers Repaired & Adjusted | | | 05000267/LER-1979-015, Forwards LER 79-015/03L-0 | Forwards LER 79-015/03L-0 | | | 05000267/LER-1979-015-03, /03L-0 on 790507:during Routine Surveillance Testing,Setpoint of Pcrv Rupture Disc M-11702 Found to Be 826 Psig.Caused by Calibr Drift.Disc Recalbr | /03L-0 on 790507:during Routine Surveillance Testing,Setpoint of Pcrv Rupture Disc M-11702 Found to Be 826 Psig.Caused by Calibr Drift.Disc Recalbr | | | 05000267/LER-1979-016, Forwards LER 79-016/01T-0 | Forwards LER 79-016/01T-0 | | | 05000267/LER-1979-016-01, /01T-0 on 790521:punch Gap of Pcrv Rupture Disc M-11702 Found Out of Tolerance W/Vendor Specs.Caused by Undocumented Change of Punch Gap Specs.Tolerances Returned to Original Specs | /01T-0 on 790521:punch Gap of Pcrv Rupture Disc M-11702 Found Out of Tolerance W/Vendor Specs.Caused by Undocumented Change of Punch Gap Specs.Tolerances Returned to Original Specs | | | 05000267/LER-1979-017, Forwards LER 79-017/01T-0 | Forwards LER 79-017/01T-0 | | | 05000267/LER-1979-017-01, /01T-0 on 790626:fault Current Trip Occurred, Causing Reactor Scram & Interrupted Reactor Cooling.Caused by Water Spray in Switchgear,Resulting in Short Circuit Due to Voltage Perturbation | /01T-0 on 790626:fault Current Trip Occurred, Causing Reactor Scram & Interrupted Reactor Cooling.Caused by Water Spray in Switchgear,Resulting in Short Circuit Due to Voltage Perturbation | | | 05000267/LER-1979-018, Forwards LER 79-018/03L-0 | Forwards LER 79-018/03L-0 | | | 05000267/LER-1979-018-03, /03L-0 on 790630:one motor-operated Butterfly Valve Found Inoperable by Remote Manual Control.Cause Is Unknown.Cause & Corrective Action to Be Reported in Future Suppl | /03L-0 on 790630:one motor-operated Butterfly Valve Found Inoperable by Remote Manual Control.Cause Is Unknown.Cause & Corrective Action to Be Reported in Future Suppl | | | 05000267/LER-1979-019-03, /03L-0 on 790711:during Normal Operation,Weekly Functional Test of Area Radiation Monitors Not Performed for 1 Wk.Caused by Misfiling of Card for Surveillance Test. Computer Readout Will Be Used as Cross Check on Card Sys | /03L-0 on 790711:during Normal Operation,Weekly Functional Test of Area Radiation Monitors Not Performed for 1 Wk.Caused by Misfiling of Card for Surveillance Test. Computer Readout Will Be Used as Cross Check on Card Sys | | | 05000267/LER-1979-020-03, /03L-0 on 790717:during Normal Plant Operation, Engine Failed to Start.Caused by Failure of Emergency Diesel Temp Switch C.Switch Replaced | /03L-0 on 790717:during Normal Plant Operation, Engine Failed to Start.Caused by Failure of Emergency Diesel Temp Switch C.Switch Replaced | | | 05000267/LER-1979-021-03, /03L-1 on 790720:during Review of Surveillance Tests,Discovered That Halon Fire Suppression Sys Surveillance Test for Second Quarter Not Performed.Caused by Inadequate Control & Direction Re Refueling Work Load | /03L-1 on 790720:during Review of Surveillance Tests,Discovered That Halon Fire Suppression Sys Surveillance Test for Second Quarter Not Performed.Caused by Inadequate Control & Direction Re Refueling Work Load | | | 05000267/LER-1979-021, Forwards LER 79-021/03L-0 | Forwards LER 79-021/03L-0 | | | 05000267/LER-1979-022-03, /03L-0 on 790720:lack of Aquatic Macroinvertebrate Sample Collection.Caused by Oversight of Field Sampling Personnel Employed by Contract Agent.Agent Indicated Program Was Resumed & Will Continue Biweekly | /03L-0 on 790720:lack of Aquatic Macroinvertebrate Sample Collection.Caused by Oversight of Field Sampling Personnel Employed by Contract Agent.Agent Indicated Program Was Resumed & Will Continue Biweekly | | | 05000267/LER-1979-023-03, /03L-0 on 790727:while Performing Normal Surveillance,Fixed Feedwater Low Flow Switch Found Inoperable. Caused by Component Failure from Normal Wear. Module Was Repaired,Reinstalled & Retested Satisfactorily | /03L-0 on 790727:while Performing Normal Surveillance,Fixed Feedwater Low Flow Switch Found Inoperable. Caused by Component Failure from Normal Wear. Module Was Repaired,Reinstalled & Retested Satisfactorily | | | 05000267/LER-1979-024, Forwards LER 79-024/03L-0 | Forwards LER 79-024/03L-0 | | | 05000267/LER-1979-024-03, /03L-0:on 790804,on Three Occasions Between 790804-16,total Primary Coolant Oxidants Exceeded 10 Ppm W/Core Average Outlet Temp Greater than 1,200 F.Caused by Dryer Bypass Resulting in Water Ingress to Core | /03L-0:on 790804,on Three Occasions Between 790804-16,total Primary Coolant Oxidants Exceeded 10 Ppm W/Core Average Outlet Temp Greater than 1,200 F.Caused by Dryer Bypass Resulting in Water Ingress to Core | | | 05000267/LER-1979-025-03, /03X-0:on 790806,during Steady State Operation at 45% Thermal Power,Emergency Diesel Generator a Found in Degraded Mode, & B Engine Also Declutched.Caused by Relay Failure Due to Normal End of Life.Relay Replaced | /03X-0:on 790806,during Steady State Operation at 45% Thermal Power,Emergency Diesel Generator a Found in Degraded Mode, & B Engine Also Declutched.Caused by Relay Failure Due to Normal End of Life.Relay Replaced | | | 05000267/LER-1979-026-03, /03L-0:on 790807,bearing Water Makeup Pump P-2105 Removed from Svc to Perform Line Repair W/Reactor at 65% Power.Caused by Hole in Recirculation Line of Pump,Requiring Removal from Svc.Line Repaired.Pump Returned to Svc | /03L-0:on 790807,bearing Water Makeup Pump P-2105 Removed from Svc to Perform Line Repair W/Reactor at 65% Power.Caused by Hole in Recirculation Line of Pump,Requiring Removal from Svc.Line Repaired.Pump Returned to Svc | | | 05000267/LER-1979-027-01, /01T-0:on 790817,noted That Recent Pipe Hanger Installation Power Operated Relief Valve Cooling Water Lines Would Have Prevented Proper Installation of Pipe Spools. Caused by Pipe Ends Changing Alignment | /01T-0:on 790817,noted That Recent Pipe Hanger Installation Power Operated Relief Valve Cooling Water Lines Would Have Prevented Proper Installation of Pipe Spools. Caused by Pipe Ends Changing Alignment | | | 05000267/LER-1979-028-01, Plant Personnel Inadvertently Grounded Instrument Panel I-36,blowing Panel Fuses & Causing Voltage Perturbation on Bus 2.Caused by Personnel Error.Ground Corrected | Plant Personnel Inadvertently Grounded Instrument Panel I-36,blowing Panel Fuses & Causing Voltage Perturbation on Bus 2.Caused by Personnel Error.Ground Corrected | | | 05000267/LER-1979-029-03, /03L-0:on 790819,during Plant Startup,B Instrument Air Compressor Became Inoperable.Caused by Failure of Discharge Feather Valve.All Discharge Valves on Compressor Replaced & C Air Compressor Returned to Svc | /03L-0:on 790819,during Plant Startup,B Instrument Air Compressor Became Inoperable.Caused by Failure of Discharge Feather Valve.All Discharge Valves on Compressor Replaced & C Air Compressor Returned to Svc | | | 05000267/LER-1979-029, Forwards LER 79-029/03L-0 | Forwards LER 79-029/03L-0 | | | 05000267/LER-1979-030, Forwards LER 79-030/03L-0 | Forwards LER 79-030/03L-0 | | | 05000267/LER-1979-030-03, /03L-0:on 790821,primary Coolant Oxidants Exceeded Limiting Condition for Operation.Caused by Offline Helium Dryer Drying Out Operations & Extended Regeneration Period. Core Outlet Temps Reduced Whenever Oxidant Limits Excee | /03L-0:on 790821,primary Coolant Oxidants Exceeded Limiting Condition for Operation.Caused by Offline Helium Dryer Drying Out Operations & Extended Regeneration Period. Core Outlet Temps Reduced Whenever Oxidant Limits Exceeded | | | 05000267/LER-1979-031-03, /03L-0:on 790821 & 0830,plant Operated W/Reactor Dewpoint Outside Tech Spec Limits.Caused by Helium Dryer Bypass,Due to Faulty Time Delay Relay.No Cause for 790821 Event.Relay Replaced & Tested | /03L-0:on 790821 & 0830,plant Operated W/Reactor Dewpoint Outside Tech Spec Limits.Caused by Helium Dryer Bypass,Due to Faulty Time Delay Relay.No Cause for 790821 Event.Relay Replaced & Tested | | | 05000267/LER-1979-031, Forwards LER 79-031/03L-0 | Forwards LER 79-031/03L-0 | | | 05000267/LER-1979-032, Forwards LER 79-032/03X-1 | Forwards LER 79-032/03X-1 | | | 05000267/LER-1979-032-03, During Testing,Four of 12 Helium Circulator Seal Malfunction Pressure Differential Switch Units Would Not Trip.Caused by Dirt Accumulation in Electrical Switches.Switches Replaced | During Testing,Four of 12 Helium Circulator Seal Malfunction Pressure Differential Switch Units Would Not Trip.Caused by Dirt Accumulation in Electrical Switches.Switches Replaced | | | 05000267/LER-1979-033, Forwards LER 79-033/03L-0 | Forwards LER 79-033/03L-0 | | | 05000267/LER-1979-033-03, /03L-0:on 790828,unauthorized Release Made from 1A Gas Waste Surge Tank.Caused by Wrong Valve Lineup.Valve Checkoff Sheets Revised to Require Operator Initials for Each Valve.Personnel Admonished | /03L-0:on 790828,unauthorized Release Made from 1A Gas Waste Surge Tank.Caused by Wrong Valve Lineup.Valve Checkoff Sheets Revised to Require Operator Initials for Each Valve.Personnel Admonished | | | 05000267/LER-1979-034-03, /03L-0:on 790830,while Operating at 36% Thermal Power,Emergency Diesel Generator Day Tanks Did Not Have 500 Gallons of Fuel Oil as Required Per Tech Specs.Caused by Inoperable High Level Switch Which Controls Pump Operations | /03L-0:on 790830,while Operating at 36% Thermal Power,Emergency Diesel Generator Day Tanks Did Not Have 500 Gallons of Fuel Oil as Required Per Tech Specs.Caused by Inoperable High Level Switch Which Controls Pump Operations | | | 05000267/LER-1979-034, Forwards LER 79-034/03L-0 | Forwards LER 79-034/03L-0 | | | 05000267/LER-1979-035-01, /01X-1:on 790831,field Audit & Preliminary Engineering Analysis of Random Sample of as-built safety-related Piping Drawings Showed Several Hangers W/Inconsistencies.Caused by Design Inconsistencies | /01X-1:on 790831,field Audit & Preliminary Engineering Analysis of Random Sample of as-built safety-related Piping Drawings Showed Several Hangers W/Inconsistencies.Caused by Design Inconsistencies | | | 05000267/LER-1979-036-03, /03L-0:on 790910,cold Reheat Snubber CRS-262 Inoperable W/Reactor in Shutdown Condition.Caused by Missing Pin That Kept Snubber from Being Properly Attached to Pipe. New Pin Fabricated & Installed.Snubber Returned to Svc | /03L-0:on 790910,cold Reheat Snubber CRS-262 Inoperable W/Reactor in Shutdown Condition.Caused by Missing Pin That Kept Snubber from Being Properly Attached to Pipe. New Pin Fabricated & Installed.Snubber Returned to Svc | | | 05000267/LER-1979-037, Forwards LER 79-037/03L-0 | Forwards LER 79-037/03L-0 | | | 05000267/LER-1979-037-03, /03L-0:on 790919,during Normal Operation,Liquid Radwaste Release Was Made in Noncompliance W/Limiting Conditions for Operation.Caused by Operator Failure to Reset Flow Switch to New Required Flow Rate.Operators Admonished | /03L-0:on 790919,during Normal Operation,Liquid Radwaste Release Was Made in Noncompliance W/Limiting Conditions for Operation.Caused by Operator Failure to Reset Flow Switch to New Required Flow Rate.Operators Admonished | | | 05000267/LER-1979-038-03, /03L-0:on 790921,analytical Sys Primary Coolant Moisture Monitor ME-9307 Became Inoperable W/Reactor at Less than 2% Power.Caused by Burned Out Thermal Electric Heater/Cooler & Two Faulty Relays.Head & Relays Replaced | /03L-0:on 790921,analytical Sys Primary Coolant Moisture Monitor ME-9307 Became Inoperable W/Reactor at Less than 2% Power.Caused by Burned Out Thermal Electric Heater/Cooler & Two Faulty Relays.Head & Relays Replaced | | | 05000267/LER-1979-038, Forwards LER 79-038/03L-0 | Forwards LER 79-038/03L-0 | | | 05000267/LER-1979-039-03, /03L-0:on 790924,authorized Liquid Waste Release Was Made,Requiring Raising Setpoints on Liquid Waste Activity Monitors Above Normal.Caused by Failure to Return Monitors to Normal Setpoints Prior to Starting Release | /03L-0:on 790924,authorized Liquid Waste Release Was Made,Requiring Raising Setpoints on Liquid Waste Activity Monitors Above Normal.Caused by Failure to Return Monitors to Normal Setpoints Prior to Starting Release | | | 05000267/LER-1979-040-03, Ler 79-040/03L-0:on 791001,two Snubbers Required During Power Operation Found Inoperable.Caused by Oil Reservoir Leak in HRS-194 & Loose Lock Nut on HOS-29.Reservoir Refilled & Lock Nut Tightened | Ler 79-040/03L-0:on 791001,two Snubbers Required During Power Operation Found Inoperable.Caused by Oil Reservoir Leak in HRS-194 & Loose Lock Nut on HOS-29.Reservoir Refilled & Lock Nut Tightened | |
|