ML19210C430

From kanterella
Jump to navigation Jump to search
LER 79-045/03L-0:on 791008,primary Coolant Oxidants Exceeded 10 Parts Per Million W/Average Core Outlet Temp Greater than 1,200 F.Caused by Residual Moisture Outgasing Due to Dryer Bypass.Load Decreased & No Corrective Action Required
ML19210C430
Person / Time
Site: Fort Saint Vrain Xcel Energy icon.png
Issue date: 11/07/1979
From: Gahm J
PUBLIC SERVICE CO. OF COLORADO
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19210C429 List:
References
LER-79-045-03L, LER-79-45-3L, NUDOCS 7911140241
Download: ML19210C430 (6)


Text

NRC FpRM 366 w. a. mucLean neuvem un e cumnissaiva (7 77) ~

LICENSEE EVENT REPORT CONTROL BLOCK: l l l l l l lh (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) [

t 0 0 1 8 9 lCl0 l F l S l V l 141 l@l 15 0 l 0 l- I O LICENSE l0 l 0 lNvu6la 0l0l IO I O25 l@l4 26 l1LICENSE Il l2 ITYPE O_l@lK I

57 CAT 58 l@

LICENSEE CODE CON'T 7

0 '

8

$o Re lLl@l0l51010l0l2l6l7 @l1l010181719 l@l1l110l7l7l9l@

60 61 DOCKET NUM8ER 68 69 EVENT DATE 74 75 REPORT CATE 80 EVENT DESCRIPTION AND PRCB ABLE CONSEQUENCES h o 2 l On four occasions between October 8.1979. and October 15. 1979. oricarv coolant o,ci- I o 3 l dants (sum of water, carbon dioxide, and carbon mo toxide) exceeded 10 carts per I o i4 l million with average core outlet tecperature greater than 1,200*F. This is operation l io 5 l under a degraded mode permitted by LCO 4.2.10 and is reportable per Technical Specifi-l.

o is l cation AC 7.5.2(b)2. No affect on public health or safety. Similar occurrences re- l 0l7 l ported in RO 77-36, 78-12, 78-18, 78-37, 78-39, 79-01, 79-02, 79-24, and 79-30. l o18 l 80 7 8 9 SYSTEM CAUSE CAUSE COVP. VALVF CCDE CODE SU80CCE COMPONENT CODE SUSCCCE SUBOLDE 7

oi.

8 I C l 3 l@ lx l@ Lzl@ l z l 21 z i z I z i z l@ l z @ LzJ @

9 10 11 12 13 18 19 20

_ SEQUENTIAL OCCURRENCE REPORT REVISION EVENT vE AR RE80RT NO. COCE TYPE NO.

LER 20

@ RE l 7l 9 l-l l 0l 4l 5l l/l l 0l 3 l lL l l--J l0l

,_ 21 22 23 24 26 27 28 29 30 31 32 T K N A ON ON P NT VETH MOURS SS I 50 8. SUP8 LIE MANUFAC RER LLJ@l zi@ la l@ zl@ I ol ni ni n LY.J@ lu_J@ l43z l@ Iz z1 z zl@

33 34 35 36 31 40 41 42 u 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS 1 0 Cause of first occurren ce wn_s eas4 8 t*1 m i e *n -a nnq,= ein g d ,n +n , , -a ,.4 n ,,e a -, a

  • 1.,,._

_ l 4 - --a , e n e 31 i i loass. Load was decreased to -ef,r da T rn 14 -4 *e - rn- neko- n c ~, -- o- - o e i 2 l core outlet temperature and/or moir ture levels were the cause of dnerndad ~nda neo-e-1 3 l tion. No specific corrective action was reauired. I i 4 l l 7 8 9 80 STA  % POWER OTHER STATUS dis O RY DISCOVERY DESCRIPTION 1 s lE l@ l 0l 3l 8l@l N/A l l A l@l Personnel Observation l ACTIVITY Co TENT AMOUNT OF ACTIVITY LOCATION OF RELEASE 7

1 I6 RELEASE 8 9 W 10 @D OF RELEASE lZl@lN/A 11 44 l l N/A 45 80 l

PERSONNEL EXPOSURES NUMBER TYPE O

  • SCRIPT 10N 1 7 l 0 l 0 l 0 l@l Z l@l N/A l PERSONNE L INJU IES NUMBER DESCRIPTION

[

7 1 a 8 9 10l0 0l@lN/A 11 12 80 l

LOSS OF OR DAMAGE TJ FACluTY TYPE DESCRIPTION _./

y lZl@l N/A ) g[ll.J Y (_Bd Y.l4 7 8 9 10 80 PUBLICITY NRC USE ONLY 2 o lNl l N/A DESCRIPTION fSSUED@ ]

68 69 l l l l l l l l l 1 IM80 &

7 8 9 10

~

~ *

  • NAME OF PREPARER PHONE: