LER-1979-045, Forwards LER 79-045/03L-0 |
| Event date: |
|
|---|
| Report date: |
|
|---|
| 2671979045R00 - NRC Website |
|
text
-
- - N' pubne service companylatteville, Colorado oe cenomde 16805 Weld County Road 191/2, 80651
.3 L_
./
November 7,1979 Fort St. Vrain Unit No. 1 P-79266 Mr. Karl V. Seyfrit, Director Nuclear Regulatory Cor: mission Region IV Office of Inspection and Enforcement 611 Ryan Plaza Drive Suite 1000 Arlington, Texas 76012 REF:
Facility Operating License No. DPR-34 Docket No. 50-267
Dear Mr. Seyfrit:
Enclosed please find a copy of Reportable Occurrence Report No. 50-267/79-45/03-L-0, Final, submitted per the requirements of Technical Specification AC 7.5.2(b)2.
Also, please find ' inclosed one copy of the Licensee Event Report for Reportable Occurrence Report No. 50-26 7/79-45/0} L-0.
Very truly yours, bW Don Warembourg Manager, Nuclear roduction DW/alk cc: Director, MIPC
,.7,,9 2, /. 1 y
%\\
i 7 911140 el VO 3
REPORT DATE:
November 7,1979 REPORTABLE OCCURRENCE 79-45 I
ISSUE O OCCURRENCE DATE:
October 8,1979 Page 1 of 5 FORT ST. VRAIN NUCLEAR GENERATING STATION PUBLIC SERVICE COMPANY OF COLORADO 16805 WELD COUNTY ROAD 19 1/2 PLAITEVILLE, COLORADO 80651 REPORT No. 50-267/ 79-45/03-L-0 Final IDENTIFICATION OF OCCURRENCE:
On four occasions between October 8,1979, and October 15, 1979, total primary coolant oxidants (the sum of water, carbon monoxide, and carbon dioxide) ex-ceeded 10 parts per million with average core outlet temperature greater than 1,200*F.
These occurrences constitute operation in a degraded mode permitted by LCO 4.2.10, and are reportable per Fort S t. Vrain Technical Specification AC 7.5.2(b)2.
EVENT
DESCRIPTION
At 1400 hours0.0162 days <br />0.389 hours <br />0.00231 weeks <br />5.327e-4 months <br /> on October 8,1979, the plant was operating at approximately 38* ther=al power and 120 MWe with an average core outlet temperature less than 1,200*F and total primary coolant oxidants greater than 10 ppm. A de-cision was made to increase reactor power in an attempt to facilitate mois-ture removal and between October 8,1979, and October 15, 1979, degraded mode operations allowed by LCO 4.2.10 occurred on four occasions, as described be-low.
1.
At approximately 1430 hours0.0166 days <br />0.397 hours <br />0.00236 weeks <br />5.44115e-4 months <br /> on October 8,1979, average core outlet tem-perature exceeded 1,200*F for the first time sin e return to power on September 15, 1979. Reference Figure 1, point 1 At that time, the total primary coolant oxidant level was approximately 15.7 ppm. As reac-ter power and core outlet temperature were increased to facilitate mois-ture removal, primary coolant oxidant levels increased as moisture was allowed to outgas from the graphite in the core. A maximum primary coolant oxidant level of 24.0 ppm was reached at 0000 hourt on October 9,1979, with corres onding core outlet temperature of 1,320*F (reference Figure 1, point
).
Total oxidant levels began a decreasing trend, with aver-age core let temperature holding steady.
At 0800 hours0.00926 days <br />0.222 hours <br />0.00132 weeks <br />3.044e-4 months <br /> on October 9,1979, it was decided to decrease reactor power to hold average core outlet temperature below 1,200*F until oxidant levels reachedavaluelessthan10 ppm (referenceFigure1, point (3)).
9 272 f9 hho W e/
REPORTABLE OCCURRENCE 79-45 ISSUE O Page 2 of 5 EVENT DESCRIPTION (continued):
2.
Because total oxidants had been less than 10 ppm since approximately 2300 hours0.0266 days <br />0.639 hours <br />0.0038 weeks <br />8.7515e-4 months <br /> October 9,1979, reactor power was increased at 1340 hours0.0155 days <br />0.372 hours <br />0.00222 weeks <br />5.0987e-4 months <br /> on Octo-b er 10, 19 79. By 1400 hours0.0162 days <br />0.389 hours <br />0.00231 weeks <br />5.327e-4 months <br />, average core outlet temperature was greater than 1,200*F.
As core outlet temperature was increased, the small amount of moisture remaining in the core was allowed to react with the graphite, resulting in increased primary coolant oxidant levels. At approximately 1700 hours0.0197 days <br />0.472 hours <br />0.00281 weeks <br />6.4685e-4 months <br /> on October 10, 1979, the plant again entered o ration under a degraded mode of LCO 4.2.10 (reference Figure 1, point 4 ).
Following an initial increase due to the rise in core outlet temperature, oxidant levels decreased to less th 10 ppm at 0700 hours0.0081 days <br />0.194 hours <br />0.00116 weeks <br />2.6635e-4 months <br /> on October 11, 1979 (reference Figure 1, point
).
3.
A small increase in moisture resulted in total primary coolant oxidants again exceeding 10 ppe at 1000 hours0.0116 days <br />0.278 hours <br />0.00165 weeks <br />3.805e-4 months <br /> on October 11, 1979, (reference Figure 1, point (})).
Af ter degraded mode operation of approximately 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />, sufficient mois-ture cleanup occurred that total pr mary coolant oxidants dropped below 10 ppm (reference Figure 1, point 7 ).
4 Total primary coolant oxidants remained at less than 10 ppm until 1400 hours0.0162 days <br />0.389 hours <br />0.00231 weeks <br />5.327e-4 months <br /> on October 13, 1979. Beginning at 0000 hours0 days <br />0 hours <br />0 weeks <br />0 months <br /> on October 13, 1979, carbon monoxide began increasing, and this eventually brought the total of primary coolant oxidants to greater than 10 ppm. Followin short period of degraded mode operation (reference Figure 1, point S
), total oxidants dropped below 10 ppm and no further degraded mode operation was observed.
CAUSE
DESCRIPTION:
'leasons for the LCO 4.2.10 degraded mode operation referenced in this report are as follows:
1.
At approximately 0400 hours0.00463 days <br />0.111 hours <br />6.613757e-4 weeks <br />1.522e-4 months <br /> on October 8,1979, a temporary loss of liquid nitrogen to the low temperature absorber resulted in an increase in total oxidants due primarily to carbon monoxide.
Following a peak at approxi-mately 0800 hours0.00926 days <br />0.222 hours <br />0.00132 weeks <br />3.044e-4 months <br /> carbon monoxide levels decreased. At 1345 hours0.0156 days <br />0.374 hours <br />0.00222 weeks <br />5.117725e-4 months <br />, a de-cision was made to increase reactor power to facilitate removal of mois-ture remaining in the core following a dryer bypass due to cross tower leakage on October 5,1979. This increase in temperature resulted in increased oxidant levels.
2.
The degraded mode operation referenced in item 2 of the event description was the result of an increase in core outlet temperature which allowed moisture to react with the core graphite, resulting in increased carbon monoxide and carbon dioxide values.
3.
Degraded mode operation described in item nu=ber 3 was a result of a small increase in moisture level.
'7'9 273
REPORTABLE OCCURRENCE 79-45 I
ISSUE O Page 3 of 5
CAUSE
DESCRIPTION (continued):
/
4.
The degraded mode operation noted in item 4 of the event description was due to a small, gradual increase in carbon monoxide. Ne explanation trace-able to plant operation is available for this brief period of degraded mode op era tion.
CORRECTIVE ACTION:
Corrective action for the occurrences noted in this report is as follows:
1.
Reactor power was reduced on October 9,1979, to achieve an average core outlet temperature less than 1,200*F until pri=ary coolant oxidants were brought within the limits of LCO 4.2.10.
2, 3, and 4.
No specific corrective action was taken for the degraded mode operation referenced in itecs 2, 3, and 4.
Sufficient pri=ary coolant cleanup occurred in each case to return pri=ary coolant oxidants to less
. than 10 ppm.
No further corrective action is anticipated or required.
9 274
lu. YUK 1ABLt ULGUKKENCE /9-4)
FIGURE 1 ISSUE O Page 4 ef 5 AVERAGE CORE OUILET TEMPERATURE VERSUS PRIFARY COOLANT OXIDANTS 1350 -
O-
- - 24 AVERAGE CORE OLT-LET TE!!PERATURE
_ 22
=!
E
'+
z
- - b 1300 20 1
- - 18 9
=
- - 16 mt E.
1250 -
d 14 i-TOTAL OXIDANTS 16 i
E 2=;
1200
?;@
~'
t'
-- 10
.m
- - 8 D
's Al T
6 1150 0000 0000 0000 0000 0000 0000 0000 0000 10/8 10/9 10/10 10/11 10/12 10/13 10/14 10/ 15 DATE/ TIME
REPORTABLE OCCURRENCE 79-45 I
ISStE o Page 5 of 5
, b]No>d Prepared by:
o-Cathy C./ Collard Technical Services Technician Reviewed by:
./
p a Services Supervisor g
Reviewed by:
Frank M. Mathie Operations Manager Approved by:
Md Manager, Nuclear Product [ ion Don Warembourg
' "9 276
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000267/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000267/LER-1979-001-03, /03L-0 on 790102:total Primary Coolant Oxidant Concentration Exceeded 10 Vol Ppm While Core Average Outlet Temp Was Greater than 1200 F.Caused by Low Temp Absorber Heatup,Releasing Oxidant to Primary Coolant | /03L-0 on 790102:total Primary Coolant Oxidant Concentration Exceeded 10 Vol Ppm While Core Average Outlet Temp Was Greater than 1200 F.Caused by Low Temp Absorber Heatup,Releasing Oxidant to Primary Coolant | | | 05000267/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000267/LER-1979-002-03, /03L-0 on 790127:operation in Degraded Mode Resulted from Repairs to Seat of Buffer Helium Purge Valve. Bypass of Buffer Helium Dryer Caused by Leakage Past Valve Seat Insert of Velan Model P-33876-N/78R Valve | /03L-0 on 790127:operation in Degraded Mode Resulted from Repairs to Seat of Buffer Helium Purge Valve. Bypass of Buffer Helium Dryer Caused by Leakage Past Valve Seat Insert of Velan Model P-33876-N/78R Valve | | | 05000267/LER-1979-004-03, /03L-0 on 790203:during Normal Operation,Cooling Tower Blowdown Exceeded Limit But Was Not Reported.Caused by Incorrect Completion of Surveillance Forms.Forms Changed & Personnel Instructed | /03L-0 on 790203:during Normal Operation,Cooling Tower Blowdown Exceeded Limit But Was Not Reported.Caused by Incorrect Completion of Surveillance Forms.Forms Changed & Personnel Instructed | | | 05000267/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000267/LER-1979-005-03, /03L-0 on 790209:during Semiannual Loss of Outside Electrical Power Test,Output Circuit Breaker Did Not Close.Cause Unknown.Breaker Replaced W/Equivalent Spare | /03L-0 on 790209:during Semiannual Loss of Outside Electrical Power Test,Output Circuit Breaker Did Not Close.Cause Unknown.Breaker Replaced W/Equivalent Spare | | | 05000267/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000267/LER-1979-013, Forwards RO 50-267/79-13/03-L-O & LER 79-013/03L-0 | Forwards RO 50-267/79-13/03-L-O & LER 79-013/03L-0 | | | 05000267/LER-1979-013-03, /03L-0 on 790412:during Test of Snubbers Many Found Inoperable Due to Unacceptable Lockup & Bleed Characteristics.Caused by Setpoint Drift,Dirty Oil & Clogged Valves.All Snubbers Repaired & Adjusted | /03L-0 on 790412:during Test of Snubbers Many Found Inoperable Due to Unacceptable Lockup & Bleed Characteristics.Caused by Setpoint Drift,Dirty Oil & Clogged Valves.All Snubbers Repaired & Adjusted | | | 05000267/LER-1979-015, Forwards LER 79-015/03L-0 | Forwards LER 79-015/03L-0 | | | 05000267/LER-1979-015-03, /03L-0 on 790507:during Routine Surveillance Testing,Setpoint of Pcrv Rupture Disc M-11702 Found to Be 826 Psig.Caused by Calibr Drift.Disc Recalbr | /03L-0 on 790507:during Routine Surveillance Testing,Setpoint of Pcrv Rupture Disc M-11702 Found to Be 826 Psig.Caused by Calibr Drift.Disc Recalbr | | | 05000267/LER-1979-016, Forwards LER 79-016/01T-0 | Forwards LER 79-016/01T-0 | | | 05000267/LER-1979-016-01, /01T-0 on 790521:punch Gap of Pcrv Rupture Disc M-11702 Found Out of Tolerance W/Vendor Specs.Caused by Undocumented Change of Punch Gap Specs.Tolerances Returned to Original Specs | /01T-0 on 790521:punch Gap of Pcrv Rupture Disc M-11702 Found Out of Tolerance W/Vendor Specs.Caused by Undocumented Change of Punch Gap Specs.Tolerances Returned to Original Specs | | | 05000267/LER-1979-017, Forwards LER 79-017/01T-0 | Forwards LER 79-017/01T-0 | | | 05000267/LER-1979-017-01, /01T-0 on 790626:fault Current Trip Occurred, Causing Reactor Scram & Interrupted Reactor Cooling.Caused by Water Spray in Switchgear,Resulting in Short Circuit Due to Voltage Perturbation | /01T-0 on 790626:fault Current Trip Occurred, Causing Reactor Scram & Interrupted Reactor Cooling.Caused by Water Spray in Switchgear,Resulting in Short Circuit Due to Voltage Perturbation | | | 05000267/LER-1979-018, Forwards LER 79-018/03L-0 | Forwards LER 79-018/03L-0 | | | 05000267/LER-1979-018-03, /03L-0 on 790630:one motor-operated Butterfly Valve Found Inoperable by Remote Manual Control.Cause Is Unknown.Cause & Corrective Action to Be Reported in Future Suppl | /03L-0 on 790630:one motor-operated Butterfly Valve Found Inoperable by Remote Manual Control.Cause Is Unknown.Cause & Corrective Action to Be Reported in Future Suppl | | | 05000267/LER-1979-019-03, /03L-0 on 790711:during Normal Operation,Weekly Functional Test of Area Radiation Monitors Not Performed for 1 Wk.Caused by Misfiling of Card for Surveillance Test. Computer Readout Will Be Used as Cross Check on Card Sys | /03L-0 on 790711:during Normal Operation,Weekly Functional Test of Area Radiation Monitors Not Performed for 1 Wk.Caused by Misfiling of Card for Surveillance Test. Computer Readout Will Be Used as Cross Check on Card Sys | | | 05000267/LER-1979-020-03, /03L-0 on 790717:during Normal Plant Operation, Engine Failed to Start.Caused by Failure of Emergency Diesel Temp Switch C.Switch Replaced | /03L-0 on 790717:during Normal Plant Operation, Engine Failed to Start.Caused by Failure of Emergency Diesel Temp Switch C.Switch Replaced | | | 05000267/LER-1979-021-03, /03L-1 on 790720:during Review of Surveillance Tests,Discovered That Halon Fire Suppression Sys Surveillance Test for Second Quarter Not Performed.Caused by Inadequate Control & Direction Re Refueling Work Load | /03L-1 on 790720:during Review of Surveillance Tests,Discovered That Halon Fire Suppression Sys Surveillance Test for Second Quarter Not Performed.Caused by Inadequate Control & Direction Re Refueling Work Load | | | 05000267/LER-1979-021, Forwards LER 79-021/03L-0 | Forwards LER 79-021/03L-0 | | | 05000267/LER-1979-022-03, /03L-0 on 790720:lack of Aquatic Macroinvertebrate Sample Collection.Caused by Oversight of Field Sampling Personnel Employed by Contract Agent.Agent Indicated Program Was Resumed & Will Continue Biweekly | /03L-0 on 790720:lack of Aquatic Macroinvertebrate Sample Collection.Caused by Oversight of Field Sampling Personnel Employed by Contract Agent.Agent Indicated Program Was Resumed & Will Continue Biweekly | | | 05000267/LER-1979-023-03, /03L-0 on 790727:while Performing Normal Surveillance,Fixed Feedwater Low Flow Switch Found Inoperable. Caused by Component Failure from Normal Wear. Module Was Repaired,Reinstalled & Retested Satisfactorily | /03L-0 on 790727:while Performing Normal Surveillance,Fixed Feedwater Low Flow Switch Found Inoperable. Caused by Component Failure from Normal Wear. Module Was Repaired,Reinstalled & Retested Satisfactorily | | | 05000267/LER-1979-024, Forwards LER 79-024/03L-0 | Forwards LER 79-024/03L-0 | | | 05000267/LER-1979-024-03, /03L-0:on 790804,on Three Occasions Between 790804-16,total Primary Coolant Oxidants Exceeded 10 Ppm W/Core Average Outlet Temp Greater than 1,200 F.Caused by Dryer Bypass Resulting in Water Ingress to Core | /03L-0:on 790804,on Three Occasions Between 790804-16,total Primary Coolant Oxidants Exceeded 10 Ppm W/Core Average Outlet Temp Greater than 1,200 F.Caused by Dryer Bypass Resulting in Water Ingress to Core | | | 05000267/LER-1979-025-03, /03X-0:on 790806,during Steady State Operation at 45% Thermal Power,Emergency Diesel Generator a Found in Degraded Mode, & B Engine Also Declutched.Caused by Relay Failure Due to Normal End of Life.Relay Replaced | /03X-0:on 790806,during Steady State Operation at 45% Thermal Power,Emergency Diesel Generator a Found in Degraded Mode, & B Engine Also Declutched.Caused by Relay Failure Due to Normal End of Life.Relay Replaced | | | 05000267/LER-1979-026-03, /03L-0:on 790807,bearing Water Makeup Pump P-2105 Removed from Svc to Perform Line Repair W/Reactor at 65% Power.Caused by Hole in Recirculation Line of Pump,Requiring Removal from Svc.Line Repaired.Pump Returned to Svc | /03L-0:on 790807,bearing Water Makeup Pump P-2105 Removed from Svc to Perform Line Repair W/Reactor at 65% Power.Caused by Hole in Recirculation Line of Pump,Requiring Removal from Svc.Line Repaired.Pump Returned to Svc | | | 05000267/LER-1979-027-01, /01T-0:on 790817,noted That Recent Pipe Hanger Installation Power Operated Relief Valve Cooling Water Lines Would Have Prevented Proper Installation of Pipe Spools. Caused by Pipe Ends Changing Alignment | /01T-0:on 790817,noted That Recent Pipe Hanger Installation Power Operated Relief Valve Cooling Water Lines Would Have Prevented Proper Installation of Pipe Spools. Caused by Pipe Ends Changing Alignment | | | 05000267/LER-1979-028-01, Plant Personnel Inadvertently Grounded Instrument Panel I-36,blowing Panel Fuses & Causing Voltage Perturbation on Bus 2.Caused by Personnel Error.Ground Corrected | Plant Personnel Inadvertently Grounded Instrument Panel I-36,blowing Panel Fuses & Causing Voltage Perturbation on Bus 2.Caused by Personnel Error.Ground Corrected | | | 05000267/LER-1979-029-03, /03L-0:on 790819,during Plant Startup,B Instrument Air Compressor Became Inoperable.Caused by Failure of Discharge Feather Valve.All Discharge Valves on Compressor Replaced & C Air Compressor Returned to Svc | /03L-0:on 790819,during Plant Startup,B Instrument Air Compressor Became Inoperable.Caused by Failure of Discharge Feather Valve.All Discharge Valves on Compressor Replaced & C Air Compressor Returned to Svc | | | 05000267/LER-1979-029, Forwards LER 79-029/03L-0 | Forwards LER 79-029/03L-0 | | | 05000267/LER-1979-030, Forwards LER 79-030/03L-0 | Forwards LER 79-030/03L-0 | | | 05000267/LER-1979-030-03, /03L-0:on 790821,primary Coolant Oxidants Exceeded Limiting Condition for Operation.Caused by Offline Helium Dryer Drying Out Operations & Extended Regeneration Period. Core Outlet Temps Reduced Whenever Oxidant Limits Excee | /03L-0:on 790821,primary Coolant Oxidants Exceeded Limiting Condition for Operation.Caused by Offline Helium Dryer Drying Out Operations & Extended Regeneration Period. Core Outlet Temps Reduced Whenever Oxidant Limits Exceeded | | | 05000267/LER-1979-031-03, /03L-0:on 790821 & 0830,plant Operated W/Reactor Dewpoint Outside Tech Spec Limits.Caused by Helium Dryer Bypass,Due to Faulty Time Delay Relay.No Cause for 790821 Event.Relay Replaced & Tested | /03L-0:on 790821 & 0830,plant Operated W/Reactor Dewpoint Outside Tech Spec Limits.Caused by Helium Dryer Bypass,Due to Faulty Time Delay Relay.No Cause for 790821 Event.Relay Replaced & Tested | | | 05000267/LER-1979-031, Forwards LER 79-031/03L-0 | Forwards LER 79-031/03L-0 | | | 05000267/LER-1979-032, Forwards LER 79-032/03X-1 | Forwards LER 79-032/03X-1 | | | 05000267/LER-1979-032-03, During Testing,Four of 12 Helium Circulator Seal Malfunction Pressure Differential Switch Units Would Not Trip.Caused by Dirt Accumulation in Electrical Switches.Switches Replaced | During Testing,Four of 12 Helium Circulator Seal Malfunction Pressure Differential Switch Units Would Not Trip.Caused by Dirt Accumulation in Electrical Switches.Switches Replaced | | | 05000267/LER-1979-033, Forwards LER 79-033/03L-0 | Forwards LER 79-033/03L-0 | | | 05000267/LER-1979-033-03, /03L-0:on 790828,unauthorized Release Made from 1A Gas Waste Surge Tank.Caused by Wrong Valve Lineup.Valve Checkoff Sheets Revised to Require Operator Initials for Each Valve.Personnel Admonished | /03L-0:on 790828,unauthorized Release Made from 1A Gas Waste Surge Tank.Caused by Wrong Valve Lineup.Valve Checkoff Sheets Revised to Require Operator Initials for Each Valve.Personnel Admonished | | | 05000267/LER-1979-034-03, /03L-0:on 790830,while Operating at 36% Thermal Power,Emergency Diesel Generator Day Tanks Did Not Have 500 Gallons of Fuel Oil as Required Per Tech Specs.Caused by Inoperable High Level Switch Which Controls Pump Operations | /03L-0:on 790830,while Operating at 36% Thermal Power,Emergency Diesel Generator Day Tanks Did Not Have 500 Gallons of Fuel Oil as Required Per Tech Specs.Caused by Inoperable High Level Switch Which Controls Pump Operations | | | 05000267/LER-1979-034, Forwards LER 79-034/03L-0 | Forwards LER 79-034/03L-0 | | | 05000267/LER-1979-035-01, /01X-1:on 790831,field Audit & Preliminary Engineering Analysis of Random Sample of as-built safety-related Piping Drawings Showed Several Hangers W/Inconsistencies.Caused by Design Inconsistencies | /01X-1:on 790831,field Audit & Preliminary Engineering Analysis of Random Sample of as-built safety-related Piping Drawings Showed Several Hangers W/Inconsistencies.Caused by Design Inconsistencies | | | 05000267/LER-1979-036-03, /03L-0:on 790910,cold Reheat Snubber CRS-262 Inoperable W/Reactor in Shutdown Condition.Caused by Missing Pin That Kept Snubber from Being Properly Attached to Pipe. New Pin Fabricated & Installed.Snubber Returned to Svc | /03L-0:on 790910,cold Reheat Snubber CRS-262 Inoperable W/Reactor in Shutdown Condition.Caused by Missing Pin That Kept Snubber from Being Properly Attached to Pipe. New Pin Fabricated & Installed.Snubber Returned to Svc | | | 05000267/LER-1979-037, Forwards LER 79-037/03L-0 | Forwards LER 79-037/03L-0 | | | 05000267/LER-1979-037-03, /03L-0:on 790919,during Normal Operation,Liquid Radwaste Release Was Made in Noncompliance W/Limiting Conditions for Operation.Caused by Operator Failure to Reset Flow Switch to New Required Flow Rate.Operators Admonished | /03L-0:on 790919,during Normal Operation,Liquid Radwaste Release Was Made in Noncompliance W/Limiting Conditions for Operation.Caused by Operator Failure to Reset Flow Switch to New Required Flow Rate.Operators Admonished | | | 05000267/LER-1979-038-03, /03L-0:on 790921,analytical Sys Primary Coolant Moisture Monitor ME-9307 Became Inoperable W/Reactor at Less than 2% Power.Caused by Burned Out Thermal Electric Heater/Cooler & Two Faulty Relays.Head & Relays Replaced | /03L-0:on 790921,analytical Sys Primary Coolant Moisture Monitor ME-9307 Became Inoperable W/Reactor at Less than 2% Power.Caused by Burned Out Thermal Electric Heater/Cooler & Two Faulty Relays.Head & Relays Replaced | | | 05000267/LER-1979-038, Forwards LER 79-038/03L-0 | Forwards LER 79-038/03L-0 | | | 05000267/LER-1979-039-03, /03L-0:on 790924,authorized Liquid Waste Release Was Made,Requiring Raising Setpoints on Liquid Waste Activity Monitors Above Normal.Caused by Failure to Return Monitors to Normal Setpoints Prior to Starting Release | /03L-0:on 790924,authorized Liquid Waste Release Was Made,Requiring Raising Setpoints on Liquid Waste Activity Monitors Above Normal.Caused by Failure to Return Monitors to Normal Setpoints Prior to Starting Release | | | 05000267/LER-1979-040-03, Ler 79-040/03L-0:on 791001,two Snubbers Required During Power Operation Found Inoperable.Caused by Oil Reservoir Leak in HRS-194 & Loose Lock Nut on HOS-29.Reservoir Refilled & Lock Nut Tightened | Ler 79-040/03L-0:on 791001,two Snubbers Required During Power Operation Found Inoperable.Caused by Oil Reservoir Leak in HRS-194 & Loose Lock Nut on HOS-29.Reservoir Refilled & Lock Nut Tightened | |
|