ML19210A796
| ML19210A796 | |
| Person / Time | |
|---|---|
| Site: | Crane |
| Issue date: | 10/03/1977 |
| From: | Potts W METROPOLITAN EDISON CO. |
| To: | |
| Shared Package | |
| ML19210A795 | List: |
| References | |
| NUDOCS 7910310681 | |
| Download: ML19210A796 (5) | |
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/..liA( M l'A l 1,Y titil t* l t usti 1,x DOCKET No. 50-289 IMI-l UNIT DATE octcber 3.1977 CCMPIETED BY W. E. Potts TEL. NO. 215 020-3601, Ext. 11h MCNTH September DAY AVERAGE DAILY PCWER LEVEL (We-Net)
DAY AVERAGE DAILY PCWER Ir/EL(We-ht '
-21 1
755 21 750 22
-19 2
-23 75h 23 3
h 759 2h ho 13 753 25 5
hh 6
750 26 189 759 27 7
760 28 699 8
70 783 9
29 780 755 30 10 762 11 31 767 12 758 13 733 1h 275 15 137 16
-15 17
-17 18 15m]
077
-23 19
-23 20 7910810 h/
UNIT SHiJ1'uG.I. 3 kid POvut at..~,, t h..
IStARY:
y On 9/15/77 at 2300 power (T. Unit I ran at 100% power for the first 15 days of +he month.
, reduced to 50% for main condenser tube cleaning. On 9/16/77 at 14:15 high condactivity DOCKET !!O.
1 On u detected in the secondary side of the steam generator and the unit was shut down.On 9/2 6/77 at 1
'18/TT at 1200 an H.C. pump motor malfunctioned thus extending the outage.
blem.
while starting up the main turbine the turbine tripped due to a generator ground pro 9/27/77 the unit was placed back on lirie and ran at 1005 power for the remainder of the month.
DATE Octnt...
3114 i
C mPLETED BY ]. E. Pott:
TEL. NO. 215-REPORT M0flT!I September METilW OF SIIUTTING DOWN TYPE TIIE REACTW OR F-FORCED DURATIffl 0.
DATE S-SCllEDULED (11001C)
REASON (1)
REDUCING POWER (2)
COMMEN'IU Reduced power to 505 for main condense - c.
B 1
9/15/TT S
!!igh conductivity in secondary side of 3:ct 1
9/16/77 F
261.0 G, A the initial reason for outage. The cu yt 6
to a R.C. pump motor malfuncticn. The cut-further due to a main turbine trip reeu'_ i:
ground problem.
O (1) REASGl:
(2l A-EQUIPMENT FAIIURE (EXPIAIN)
B-MAI!3T. OR TEST C
C-REFUELING w
D-REGUIATORY RESTRICTICN E-OPERATOR TRAINING A'D CD O
LICFNSE EXAMI!!ATIC':i CO F-ADMINSTRATIVE G-OPERATIOt!AL ERROR (EPIAIU)
Il-OrilER (EXPIAIN) l
sg
- 1~.
REP WTING PEHIOD:
- 11. 77, niwu Tg[it nicI[
'h
, T(. Omo GROSS HOURS IN REP GTING PERICD:
720 2.
CURPINTLY AU"'HCRIZED POTER LEVEL IWt 2535 MAX. DEFEND. CAPACITY (bide-Net)
I9I 3.
DESIGN ELECTRICAL RATING (!Ge-net) 819 k.
POWER EVEL TO WHICH RESTRICTED (IF /diY):
N/A 5
REASCNS FOR PISTRICTIONS (IF /di!):
THIS CU!!UIATIVE MCUTH YR-TO-DATE TO DATE 5.
NUMBER CF HCUPS REACTOR WAS CRITICAL 513.2 5002.5 2085h.3 6..
REACTOR RESERVE SHUTDOWN HOURS 67.3 230 838.5 7.
HOURS GENEPATCR CH-LINE..
h59.0 h888.h 20396.8 8.
UNIT RESERVE SHUTDOWN HOURS......
0 0
0 9
GECSS THERMAL ENERGY GENERATED (INH)
. 109755h 12122978 '
h9880853 10.
GRCSS EECTRICAL E'IERGY GENEPATED (!GH).
3hhhh3 30726ho 166h5h27 11.
NET EECTRICAL ENERGY GENER;GED (M4H)..
316088 3720878 15575838 12.
REACTOR SERVICE FACTOR 71.35 76.h5
'7.25 13.
REACTOR AVAILABILITY FACTOR..
83.h%
79.05 80.35 14 UNIT SERVICE FACTOR,
63.8%
'7h.6%
75.5%
15 UNIT AVAILABILITY FACTOR 63.8%
Th.6%
75.55
- 16. UNIT CAPACITY FACTCR (USING MDC) 55.h5 71.7%
72.8%
"17.
UNIT CAPACITY FACTOR (USING DESIGN MWe-net) 53. 4 60.h5 70.h5 18.
FORCED OUTAGE RATE........................ 36.3%
5.1%
6.1%
19 SHUTDOiNS SCHEDULED TO BEGIN IN NEXT 6 MCUTHS (STATE TYPE, DATE AND DURA *ICN OF EACH):
Refueling. March 18, 1978, 6 weeks 20 IF SHUTDCWN AT END CF REPCRT PERICD, ESTIMATED DATE CF STARTJP:
UNITS IN TEST STA"TJS (PEIG TO COMMERCIAL OPEPATIC3): NOT APPLICA3LE 21 1%9 099