ML19210A796

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Monthly Operating Rept for Sept 1977
ML19210A796
Person / Time
Site: Crane Constellation icon.png
Issue date: 10/03/1977
From: Potts W
METROPOLITAN EDISON CO.
To:
Shared Package
ML19210A795 List:
References
NUDOCS 7910310681
Download: ML19210A796 (5)


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/..liA( M l'A l 1,Y titil t* l t usti 1,x DOCKET No. 50-289 IMI-l UNIT DATE octcber 3.1977 CCMPIETED BY W. E. Potts TEL. NO. 215 020-3601, Ext. 11h MCNTH September DAY AVERAGE DAILY PCWER LEVEL (We-Net)

DAY AVERAGE DAILY PCWER Ir/EL(We-ht '

-21 1

755 21 750 22

-19 2

-23 75h 23 3

h 759 2h ho 13 753 25 5

hh 6

750 26 189 759 27 7

760 28 699 8

70 783 9

29 780 755 30 10 762 11 31 767 12 758 13 733 1h 275 15 137 16

-15 17

-17 18 15m]

077

-23 19

-23 20 7910810 h/

UNIT SHiJ1'uG.I. 3 kid POvut at..~,, t h..

IStARY:

y On 9/15/77 at 2300 power (T. Unit I ran at 100% power for the first 15 days of +he month.

, reduced to 50% for main condenser tube cleaning. On 9/16/77 at 14:15 high condactivity DOCKET !!O.

1 On u detected in the secondary side of the steam generator and the unit was shut down.On 9/2 6/77 at 1

'18/TT at 1200 an H.C. pump motor malfunctioned thus extending the outage.

blem.

while starting up the main turbine the turbine tripped due to a generator ground pro 9/27/77 the unit was placed back on lirie and ran at 1005 power for the remainder of the month.

DATE Octnt...

3114 i

C mPLETED BY ]. E. Pott:

TEL. NO. 215-REPORT M0flT!I September METilW OF SIIUTTING DOWN TYPE TIIE REACTW OR F-FORCED DURATIffl 0.

DATE S-SCllEDULED (11001C)

REASON (1)

REDUCING POWER (2)

COMMEN'IU Reduced power to 505 for main condense - c.

B 1

9/15/TT S

!!igh conductivity in secondary side of 3:ct 1

9/16/77 F

261.0 G, A the initial reason for outage. The cu yt 6

to a R.C. pump motor malfuncticn. The cut-further due to a main turbine trip reeu'_ i:

ground problem.

O (1) REASGl:

(2l A-EQUIPMENT FAIIURE (EXPIAIN)

B-MAI!3T. OR TEST C

C-REFUELING w

D-REGUIATORY RESTRICTICN E-OPERATOR TRAINING A'D CD O

LICFNSE EXAMI!!ATIC':i CO F-ADMINSTRATIVE G-OPERATIOt!AL ERROR (EPIAIU)

Il-OrilER (EXPIAIN) l

sg

1~.

REP WTING PEHIOD:

11. 77, niwu Tg[it nicI[

'h

, T(. Omo GROSS HOURS IN REP GTING PERICD:

720 2.

CURPINTLY AU"'HCRIZED POTER LEVEL IWt 2535 MAX. DEFEND. CAPACITY (bide-Net)

I9I 3.

DESIGN ELECTRICAL RATING (!Ge-net) 819 k.

POWER EVEL TO WHICH RESTRICTED (IF /diY):

N/A 5

REASCNS FOR PISTRICTIONS (IF /di!):

THIS CU!!UIATIVE MCUTH YR-TO-DATE TO DATE 5.

NUMBER CF HCUPS REACTOR WAS CRITICAL 513.2 5002.5 2085h.3 6..

REACTOR RESERVE SHUTDOWN HOURS 67.3 230 838.5 7.

HOURS GENEPATCR CH-LINE..

h59.0 h888.h 20396.8 8.

UNIT RESERVE SHUTDOWN HOURS......

0 0

0 9

GECSS THERMAL ENERGY GENERATED (INH)

. 109755h 12122978 '

h9880853 10.

GRCSS EECTRICAL E'IERGY GENEPATED (!GH).

3hhhh3 30726ho 166h5h27 11.

NET EECTRICAL ENERGY GENER;GED (M4H)..

316088 3720878 15575838 12.

REACTOR SERVICE FACTOR 71.35 76.h5

'7.25 13.

REACTOR AVAILABILITY FACTOR..

83.h%

79.05 80.35 14 UNIT SERVICE FACTOR,

63.8%

'7h.6%

75.5%

15 UNIT AVAILABILITY FACTOR 63.8%

Th.6%

75.55

16. UNIT CAPACITY FACTCR (USING MDC) 55.h5 71.7%

72.8%

"17.

UNIT CAPACITY FACTOR (USING DESIGN MWe-net) 53. 4 60.h5 70.h5 18.

FORCED OUTAGE RATE........................ 36.3%

5.1%

6.1%

19 SHUTDOiNS SCHEDULED TO BEGIN IN NEXT 6 MCUTHS (STATE TYPE, DATE AND DURA *ICN OF EACH):

Refueling. March 18, 1978, 6 weeks 20 IF SHUTDCWN AT END CF REPCRT PERICD, ESTIMATED DATE CF STARTJP:

UNITS IN TEST STA"TJS (PEIG TO COMMERCIAL OPEPATIC3): NOT APPLICA3LE 21 1%9 099