ML19209C209

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Forwards IE Circular 79-20, Failure of Gte Sylvania Relay, Type PM Bulletin 7305,Catalog 5U12-11-AC w/120 Volt Ac Coil. No Action Required
ML19209C209
Person / Time
Site: Trojan File:Portland General Electric icon.png
Issue date: 09/24/1979
From: Engelken R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To: Goodwin C
PORTLAND GENERAL ELECTRIC CO.
References
NUDOCS 7910120204
Download: ML19209C209 (1)


Text

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September 24, 1979 Docket tio. 50-344 Portland General Electric Company 121 S. W. Salmon Street Portland, Oregon 97204 Attention: Mr. Charles Goodwin, Jr.

Assistant Vice President Gentlemen:

The enclosed IE Circular tio. 79-20 is forwarded to you for information.

ilo written response is required.

Should you have any questions related to your understanding of this matter, please contact this office.

Sincerely,

/EvrL,.al-R. H. Engelken Director

Enclosures:

1.

IE Circular tio. 79-20 2.

List of IE Circulars Issued in the Last Six Months cc w/ enclosures:

C. P. Yundt, PGE F. C. Gaidos, PGE d

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6' Accession tlo.: 7908220118 SSINS No.: 6830 UNITED STATES NUCLEAR REGULATORY COMMISSION OFFICE OF INSPECTI0fl AND ENFORCEMENT WASHINGTON, D.C.

20555 September 24, 1979 IE Circular No. 79-20 FAILURE OF GTE StLvnhin RELM, TYPE FM obLLETIN 7^2G5, CATALOG 5U12-11-AC UITH A 120V AC COIL Description of Circumstances:

During inspection of relays in the Engineered Safeguards Actuation System at Metropolitan Edison Three Mile Island Nuclear Station Unit #1, relay 62X2B/RCIA failed to drop out when the coil was deenergized. The failed relay would not prevent component starting but would have reduced the 2 of 3 coincidence logic to 2 of 2, affecting Decay Heat Closed Cooling Pump A and ?!uclear Services Closed Cooling Pump A or B.

The cause for failure was attributed to a notch in the armature operating rod. The notch occurs where the rod vibrates against the magnet assembly due to coil hum. A review of the history of this component indicates that similar relays failad during 1977 through 1979 at least one of which was attributed to notching. An inspection of forty-eight (48) relays by this licensee indicated that twenty-five (25) of the relays had detectable notches ranging from 0.001 to 0.003 inches deep.

Reconmended Actions for Licensees' Consideration:

1.

Ensure that all GTE Sylvania Relays Type PM Bulletin 7305, with a 120V AC Coil used in or affecting the operation of safety-related equipment are examined to ensure that the arnature operating rod is not notched and is operating freely.

2.

Relays found with detectable notches on the operating rod should be corrected.

If correction cannot be accomplished then administrative controls should be initiated to assure demonstrated operation until the relay condition is corrected.

No written response to this Circular is required.

If you require additional information regarding this subject, contact the Director of the appropriate NRC Regional Office.

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IE Circular No. 79-20 Enclosure Septenber 24, 1979 Page 1 of 2' LISTING OF IE CIRCULARS ISSUED IN LAST SIX MONTHS Circular Subject Date of Issued to No.

Issue 79-03 Inadequate Guard Traini g-2/23/79 All Holders of Qualification and Falsified and applicants

' 24 'rr "accrd:

for S;ecial Nuclear Material Licenses in Safeguards Group I 79-04 Loose Locking Nut On 3/16/79 All Holders of Linitorque Valve Reactor OLs or cps Operators 79-05 Moisture Leakage In 3/20/79 All Holders of Stranded Wire Conductors Reactor OLs or cps 79-06 Failure to Use Syringe 4/19/79 All Holders of and Bottle Shields in Medical Licensees Nuclear Medicine except teletherapy licensees 79-07 Unexpected Speed Increase 5/2/79 All Holders of of Reactor Recirculation BWR OL's or CP's MG Set Resulted in Reactor Power Increase 79-08 Attempted Extortion - Low 5/18/79 All Fuel Facilities Enriched Uranium Licensed by NRC 79-09 Occurrences of Split or 6/22/79 All Materials Punctured Regulator Diaphragms Priority I, Fuel In Certain Self Contained Cycle and Operating Breathing Apparatus Reactor Licensees 79-10 Pipefittings Manufactured 6/2o/79 All Power Reactor from Unacceptable Material Licensees with a CP and/or OL 79-11 Design / Construction 6/27/79 All Applicants Interface Problem for, and Holders of Power Reactor cps 1144 063

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  • IE Circular No. 79-20 Enclosure September 24, 1979 Page 2 of 2 LISTING 0F IE CIRCULARS ISSUED IN LAST SIX MONTHS Circular Subject Date of Issued to No.

Issued 79-12 Potential Diesel Generator 6/28/79 All Power Reactors Turbech? ger Dreblem Goerating Facilities ano all Utilities having a CP 79-13 Replacement of Diesel 7/10/79 All Power Reactor Fire Pump Starting Operating Facilities Contactors and all Utilities having a CP 79-14 Unauthorized Procurement and 7/13/79 All Medical Licensees Distribution of XE-133 except Teletheraphy Medical Licensees and to all Radiopharmaceu-tical Suppliers 79-15 Bursting of High Pressure Hose 8/8/79 All Materials Priority I, and Malfunction of Relief Fuel Cycle and Operating Valve "0" Ring in Certain Self-Power Reactor Licensees Contained Breathing Apparatus 79-16 Excessive Radiation Exposures 8/16/79 All Radiography To Menbers Of The General Public Licensees And A Radiographer 79-17 Contact Problem in SB-12 8/14/79 All Power Reactor Switches on General Electric Licensees with a CP Company Metalclad Circuit and/or OL Breakers 79-18 Proper Installation of 9/10/79 All Holders of a Target Rock Safety-Relief Power Reactor OL Valves or CP 79-19 Loose Locking Devices on 9/13/79 All Power Reactor Ingersoll-Rand Pumps Operating facilities and all utilities having a CP 1144 064