ML19207B258

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IE Insp Rept 50-348/79-22 on 790604-05.No Noncompliance Noted.Major Areas Inspected:Licensed Operators Requalification Training Program,Nonlicensed Personnel Training & Licensee Response to IE Bulletin 79-06A
ML19207B258
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 06/25/1979
From: Ford E, Ruhlman W, Taylor P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML19207B252 List:
References
50-348-79-22, NUDOCS 7908230683
Download: ML19207B258 (4)


See also: IR 05000348/1979022

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Report No. 50-348/79-22

Licensee: Alabama Power Company

600 North 18th Street

,

Birmingham, Alabama

35202

Facility Name:

Farley Unit 1

Docket No. 50-348

License No. NPF-2

Inspection at Fat ey ite near Dothan, Alabama

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Inspectors:

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P. 4.. Taylor

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Date Signed

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E. J. Ford

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Date Signed-

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Approved by: / [ jT.

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W. A. Ruhlman, Acting Section Chief, RONS Branch

DE e Signed

SUMMARY

Inspection on June 4-5, 1979

Areas Inspected

This routine, announced inspection involved 34 inspector-hours onsite in the

areas of licensed peratort, requalification training p-ogram; train.ng and

retraining programs - nonlicensed personnel and licens . response to IE Bulletin

79-06A in areas of training.

Results

Of the 3 areas inspected, no appare..t items of noncompliance or deviations were

identified.

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DETAILS

1.

Persons Contacted

Licensee Employees

  • W.

G. Hairston, Plant Manager

D. C. Poole, Operations Superintendent

  • R. D. Hill, Plant Quality Assurance Engineer
  • L.

S. Williams, Training Supervisor

T. Horne, Training Instructor

Other licensee employees contacted included technicians, operators, and

mechanics.

  • Attended exit interview

2.

Exit Interview

The inspection scope and findings were summarized on June 5, 1979, with

those persons indicated in Paragraph 1 above.

Licens?e Action on Previous Inspection F.ndings

.4. .

%pected.

4.

Unresolved Items

Unresolved items were not identified during this inspection.

5.

Training and Retraining Programs; Non-licensed Plant Personnel

References:

a)

AP-45, Training Plan, Rev. 2, dated 3/78

a.

Review Conducted

There were no changes made to the licensee's training procedures since

the last inspection.

This area was reviewed with respect to maintain-

ing the implementation of the licensee's commitments for:

1)

General employee training for new employees

2)

General employee retraining

3)

Tecporary employee training

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4)

On the-job training for:

auxiliary /craf tsmen; technicians;

QA/QC personnel; and technical staff

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The inspector reviewed training records for two individuals in each

category above to verify that the described training program was

p-ovided. The inspector interviewed one employee from each category

above to verify that the individual actually received the training

which was documented in the training records.

Within the areas reviewed, no items of noncompliance or deviations

were identified, one open item was found as documented in Paragraph

5.b below.

b.

Failure to Provide Security Training

While reviewing licensee training records the inspector noted that

records for several individuals showed no participation in security

training as required by reference (a).

The inspector had determined

that the licensee had identified this area and corrective action is in

progress with a completion date of October 1, 1979.

This item will remain open and will be inspected at a future inspection

(348/79-22-01).

6.

Requalification Training

References:

a)

Training Plan, Revision 2, dated 3/78

There were no changes made to the licensee's requalification program

,ince the last inspection. This area was reviewed with respect to

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maintaining the implementation of tbe accepted requalification train-

ing program. The inspector reviewed:

the licensee's prepared schedule

for conducting lectures; the licensee's prepared lesson plan or equiva-

lent for three lecture topics; and the licensee's inclusion in the

requalification program of deficient areas identified by evaluation of

the most recent annual examinations.

The inspector determined which

licensed operators:

failed all or portions of the annual examinations;

received unsatisfactory performance evaluations,

or did not perform

licensed duties for a period four months or longer.

The inspector

verified the completion of r

apriate follow through action for each

of these individuals.

The raspector reviewed the training records for

NRC licensed Reactor Operators and Senior Reactor Operators to verify

that they included:

copies of annual written examinations and the

individual responses, documentation of attendance at all required

lectures, documentation of the required control manic lations, the

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results of performance evaluations, documentation of required addi-

tionally traicing to satisfy deficient performance, documentation of

cc,pletion of required procedure reviews and/or self-study.

Addition-

ally, the inspector interviewed (5) operators to verify that the

training records reflect the actual training received.

Within the areas reviewed no ie. ems of noncompliance or deviation were

identified.

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7.

Licensee Response to IE Bulletin 79-06A

a.

heview Conducted

The inspectors conducted a review of licensee actions to verify the

effectiveness of operator training conducted in response to IE Bulletta

79-06A. The inspectors reviewed:

ewergency procedures related to a

small break LOCA; management controls implemented to incorporate plant

modifications into the operator training and requalification proFrams;

management controls implemented to incorporate the operational knowledge

gained from the Three Mile Island incident into the operator training

and requalification programs; management controls implemented to

increase the standard of operator knowledge required in the area of

plant transient responses; management controls implemented to assess

the effectiveness of the training conducted, including, but not limited

to, auditing of training presentations, examination content, and

examination grading. The inspectors interviewed (2) reactor operators,

(3) senior reactor operators, to establish the operators' subjective

evaluations of the effectiveness of training received in conjunction

with incidents at the same or other facilities.

Within the areas reviewed no items of noncompliance or deviation were

identified.

b.

Inadequate Operator Training

With respect to operator training conducted in recponse to IE Bulletin

79-06A, the licensee committed to conduct a corporate QA audit on

training presented in response to IE Bulletin 79-06A. This audit

would be complet'ed by June 15, 1979. This item aill remain open and

inspected at a future date (349/79-22-02).

The licensee stated that training in response to IE Bulletin 79-06A is

being incorporated in the license <

perators' requalification program

and that changes will be made as ,ilant procedures are revised end

plant modifications are implemented.

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