Similar Documents at Salem |
---|
Category:Letter
MONTHYEARIR 05000272/20230042024-02-0505 February 2024 Integrated Inspection Report 05000272/2023004 and 05000311/2023004 ML24009A1022024-01-26026 January 2024 Exemption from Select Requirements of 10 CF Part 73 (EPID L-2023-LLE-0045 (Security Notifications, Reports, and Recordkeeping and Suspicious Activity Reporting)) IR 05000272/20234012024-01-22022 January 2024 Material Control and Accounting Program Inspection Report 05000272/2023401 and 05000311/2023401 ML24004A1542024-01-0808 January 2024 Notification of Conduct of a Fire Protection Team Inspection LR-N23-0079, Special Report 23-02-00 Pursuant to the Requirements of Salem Unit 1 Technical Specification 3.3.3.7, Action 10, for the Unit 1 Main Steam Line Rad Monitor Inoperable for Greater than Seven Days2023-12-0707 December 2023 Special Report 23-02-00 Pursuant to the Requirements of Salem Unit 1 Technical Specification 3.3.3.7, Action 10, for the Unit 1 Main Steam Line Rad Monitor Inoperable for Greater than Seven Days ML23270C0072023-11-29029 November 2023 Notice of Proposed Amendment to Decommissioning Trust Agreement LR-N23-0077, Loss of Coolant Accident Peak Cladding Temperature Margin Tracking - Annual Report 2023 & 30 Day Report for Salem Unit 1 Upflow Conversion2023-11-29029 November 2023 Loss of Coolant Accident Peak Cladding Temperature Margin Tracking - Annual Report 2023 & 30 Day Report for Salem Unit 1 Upflow Conversion ML23324A3072023-11-17017 November 2023 Request for Exemption from Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Implementation IR 05000272/20230032023-11-13013 November 2023 Integrated Inspection Report 05000272/2023003 and 05000311/2023003 LR-N23-0072, Core Operating Limits Report Cycle 302023-11-0101 November 2023 Core Operating Limits Report Cycle 30 IR 05000272/20230102023-10-12012 October 2023 Biennial Problem Identification and Resolution Inspection Report O5000272/2023010 and 05000311/2023010 IR 05000272/20234022023-10-12012 October 2023 and Salem Nuclear Generating Station, Units 1 and 2 - Security Baseline Inspection Report 05000354/2023402, 05000272/2023402 and 05000311/2023402 (Cover Letter Only) LR-N23-0045, and Peach Bottom Atomic Power Station, Units 2 and 3 - Notice of Proposed Amendment to Decommissioning Trust Agreement2023-09-0808 September 2023 and Peach Bottom Atomic Power Station, Units 2 and 3 - Notice of Proposed Amendment to Decommissioning Trust Agreement ML23249A2612023-09-0606 September 2023 License Amendment Request to Modify the Salem and Hope Creek Exclusion Area Boundary IR 05000272/20230052023-08-31031 August 2023 Updated Inspection Plan for Salem Nuclear Generating Station, Units 1 and 2 (Reports 05000272/2023005 and 05000311/2023005) ML23233A0762023-08-21021 August 2023 Requalification Program Inspection ML23192A8212023-08-14014 August 2023 and Salem Nuclear Generating Station, Unit Nos. 1 and 2 - Issuance of Amendment Nos. 234, 347, and 329 Revise Technical Specifications to Delete Meteorological Tower Location IR 05000272/20230022023-08-0909 August 2023 Integrated Inspection Report 05000272/2023002 and 05000311/2023002 LR-N23-0055, Special Report 272/23-01-00, Pursuant to the Requirements of Technical Specification 3.3.3.1, Action 23, for the Vent Noble Gas Rad Monitor Inoperable for Greater than Seven Days2023-08-0303 August 2023 Special Report 272/23-01-00, Pursuant to the Requirements of Technical Specification 3.3.3.1, Action 23, for the Vent Noble Gas Rad Monitor Inoperable for Greater than Seven Days IR 05000354/20230022023-08-0303 August 2023 Integrated Inspection Report 05000354/2023002 and Independent Spent Fuel Storage Installation Inspection Report 07200048/2023001 LR-N23-0054, In-Service Inspection Activities2023-07-26026 July 2023 In-Service Inspection Activities LR-N23-0046, Emergency Plan Document Revisions Implemented June 28, 20232023-07-10010 July 2023 Emergency Plan Document Revisions Implemented June 28, 2023 LR-N23-0005, License Amendment Request to Amend Technical Specifications (TS) 6.8.4.f for Permanent Extension of Type a and Type C Leak Rate Test Frequencies2023-06-23023 June 2023 License Amendment Request to Amend Technical Specifications (TS) 6.8.4.f for Permanent Extension of Type a and Type C Leak Rate Test Frequencies ML23139A1472023-06-0505 June 2023 Relief Request Associated with Fourth Interval In-service Inspection Limited Examinations of Weld Coverage ML23096A1842023-05-0909 May 2023 Issuance of Amendment No. 328 Revise and Relocate Reactor Coolant System Pressure and Temperature Limits and Pressurizer Overpressure Protection System Limits to Pressure and Temperature Limits Report IR 05000272/20230012023-05-0303 May 2023 Integrated Inspection Report 05000272/2023001 and 05000311/2023001 ML23081A4662023-05-0202 May 2023 Issuance of Amendment Nos. 346 and 327 Revise Technical Specifications to Extend Allowable Outage Time for Inoperable Emergency Diesel Generator IR 05000272/20233012023-05-0101 May 2023 Initial Operator Licensing Examination Report 05000272/2023301 and 05000311/2023301 LR-N23-0034, 2022 Annual Radiological Environmental Operating Report (AREOR) - Salem Nuclear Generating Station, Unit Nos. 1 and 2 and Hope Creek Generating Station2023-04-27027 April 2023 2022 Annual Radiological Environmental Operating Report (AREOR) - Salem Nuclear Generating Station, Unit Nos. 1 and 2 and Hope Creek Generating Station LR-N23-0035, 2022 Annual Radioactive Effluent Release Report (ARERR)2023-04-27027 April 2023 2022 Annual Radioactive Effluent Release Report (ARERR) LR-N23-0033, Core Operating Limits Report Cycle 272023-04-26026 April 2023 Core Operating Limits Report Cycle 27 LR-N23-0010, License Amendment Request Revision of Technical Specification (TS) to Delete TS Section 5.5 - Meteorological Tower Location2023-04-21021 April 2023 License Amendment Request Revision of Technical Specification (TS) to Delete TS Section 5.5 - Meteorological Tower Location ML23089A0942023-04-17017 April 2023 NRC to PSEG Hope Creek, Transmittal of the National Marine Fisheries Service'S March 24, 2023, Biological Opinion GAR-2020-02842 Concerning Salem and Hope Creek ML23087A1492023-04-17017 April 2023 NRC to PSEG Salem, Transmittal of the National Marine Fisheries Service'S March 24, 2023, Biological Opinion GAR-2020-02842 Concerning Salem and Hope Creek ML23103A3232023-04-13013 April 2023 Submittal of Updated Final Safety Analysis Report, Rev. 26, Summary of Revised Regulatory Commitments for Hope Creek, Summary of Changes to PSEG Nuclear LLC, Quality Assurance Topical Report, NO-AA-10, Rev. 89 ML23095A3682023-04-12012 April 2023 and Salem Nuclear Generating Station, Unit Nos. 1 and 2 - Threshold Determination for Proposed Transfer of Land Ownership LR-N23-0006, Report on Status of Decommissioning Funding for Reactors and Independent Spent Fuel Storage Installations2023-03-24024 March 2023 Report on Status of Decommissioning Funding for Reactors and Independent Spent Fuel Storage Installations ML23086A0912023-03-24024 March 2023 NMFS to NRC, Transmittal of Biological Opinion for Continued Operations of Salem and Hope Creek Nuclear Generating Stations RS-23-049, Constellation Energy Generation, LLC, Report on Status of Decommissioning Funding for Reactors and Independent Spent Fuel Storage Installations2023-03-23023 March 2023 Constellation Energy Generation, LLC, Report on Status of Decommissioning Funding for Reactors and Independent Spent Fuel Storage Installations LR-N23-0019, and Salem Generating Station, Units 1 and 2 - Guarantees of Payment of Deferred Premiums2023-03-21021 March 2023 and Salem Generating Station, Units 1 and 2 - Guarantees of Payment of Deferred Premiums ML23044A1052023-03-13013 March 2023 Issuance of Amendment Nos. 345 and 326 Relocate Technical Specifications Requirements for Reactor Head Vents to Technical Requirements Manual ML23037A9712023-03-0909 March 2023 and Salem Nuclear, Unit Nos. 1 and 2 Issuance of Amendment Nos. 233, 344, and 325 Relocate Technical Specification Staff Qualification Requirements to the PSEG Quality Assurance Topical Report IR 05000272/20230112023-03-0707 March 2023 Comprehensive Engineering Team Inspection Report 05000272/2023011 and 05000311/2023011 IR 05000272/20220062023-03-0101 March 2023 Annual Assessment Letter for Salem Nuclear Generating Station, Units 1 and 2 (Reports 05000272/2022006 and 05000311/2022006) LR-N23-0016, and Salem Generating Station, Units 1 and 2 - Report of Changes, Tests, and Experiments2023-02-28028 February 2023 and Salem Generating Station, Units 1 and 2 - Report of Changes, Tests, and Experiments LR-N23-0012, Annual Property Insurance Status Report2023-02-24024 February 2023 Annual Property Insurance Status Report LR-N23-0014, Stations Submittal of 2022 Annual Report of Fitness for Duty Performance Data Per 10 CFR 26.203(e) and 10 CFR 26.7172023-02-23023 February 2023 Stations Submittal of 2022 Annual Report of Fitness for Duty Performance Data Per 10 CFR 26.203(e) and 10 CFR 26.717 ML23034A1532023-02-0909 February 2023 Operator Licensing Examination Approval ML23019A3482023-02-0202 February 2023 Issuance of Relief Request No. SC-I5R-221 for the Alternative Repair for Service Water System Piping LR-N23-0003, Response to Requests for Additional Information Salem Unit 2 Relief Request S2-I4R-2112023-02-0101 February 2023 Response to Requests for Additional Information Salem Unit 2 Relief Request S2-I4R-211 2024-02-05
[Table view] Category:Written Event Report (30 or 60 day)
MONTHYEARLR-N23-0055, Special Report 272/23-01-00, Pursuant to the Requirements of Technical Specification 3.3.3.1, Action 23, for the Vent Noble Gas Rad Monitor Inoperable for Greater than Seven Days2023-08-0303 August 2023 Special Report 272/23-01-00, Pursuant to the Requirements of Technical Specification 3.3.3.1, Action 23, for the Vent Noble Gas Rad Monitor Inoperable for Greater than Seven Days LR-N21-0083, Loss of Coolant Accident Peak Cladding Temperature Margin Tracking - Annual Report 2021 & 30 Day Report for Salem Unit 2 Upflow Conversion2021-11-24024 November 2021 Loss of Coolant Accident Peak Cladding Temperature Margin Tracking - Annual Report 2021 & 30 Day Report for Salem Unit 2 Upflow Conversion ML0333606682003-11-24024 November 2003 Special Report 03-002 Re Condenser Off Gas Monitor Being Inoperable for Greater than Seven Days ML19031A9121997-02-25025 February 1997 LER 1977-009-01 for Salem Unit 1 No. 12 Containment Fan Coil Unit Inoperable ML19031B1781977-02-25025 February 1977 LER 1977-010-01 for Salem, Unit 1 No. 12 Containment Fan Coil Unit Inoperable ML19031B0621977-02-24024 February 1977 LER 1977-011-01 and LER 1977-013-01 for Salem Unit 1 Industrial Waste Was Discharged from the Treatment Area When the Ph Was Outside the Range of 6~5 to 8.5 ML19031B1791977-02-15015 February 1977 LER 1977-006-01 for Salem Unit 1 #12 Reactor Coolant Flow Channel 1 Inoperable ML19031A9151977-02-15015 February 1977 LER 1977-007-01 for Salem Unit 1 No. 12 Steam Generator Steam Flow Channel II Inoperable ML19031B0631977-02-15015 February 1977 LER 1977-008-01 for Salem Unit 1 No. 13 Steam Generator Steam Flow Channel I Inoperable ML19031A9161977-02-0707 February 1977 LER 1977-004-01 for Salem, Unit 1, #13 Auxiliary Feed Pump Fail to Start ML19031B5731977-02-0101 February 1977 LER 1976-029-01 for Salem Unit 1 Phase III Test Procedure ML19031A8271977-01-31031 January 1977 LER 1977-005-01 for Salem, Unit 1, Hydraulic Line Flange on Nos. 11 and 12 Main Steam Isolation Valves and Subsequent Violation of Technical Specification 3.0.3 ML19031B0641977-01-28028 January 1977 LER 1976-031-01 for Salem, Unit 1, Boron Injection Tank Inoperable ML19031B0651977-01-28028 January 1977 LER 1977-001-01 for Salem, Unit 1, Containment Pressure Protection, Channel II, PT-948C, Inoperable ML19031B0671977-01-28028 January 1977 LER 1977-002-01 for Salem, Unit 1, Pipe Failure on Letdown Vent Line ML19031B5741977-01-28028 January 1977 LER 1976-030-01 for Salem Unit 1 No. 11 and No. 12 Boric Acid Storage Tanks Inoperable ML19031B1801977-01-19019 January 1977 LER 1976-028-42 for Salem, Unit 1 Radioactive Spill and Unauthorized Release ML19031B0681977-01-14014 January 1977 LER 1976-026-01 for Salem, Unit 1, Boron Injection Tank Inoperable ML19031A7621977-01-14014 January 1977 LER 1976-020-01 for Salem, Unit 1 High Reactor Coolant System Chlorides ML19031B1811977-01-14014 January 1977 LER 1976-025-01 for Salem Unit 1 Reduction of Shutdown Margin During Special Test Exceptions ML19031A9191977-01-0404 January 1977 LER 1976-024-01 for Salem, Unit 1, Failure of Radiation Monitoring System Channel Rlla, Containment/Plant Vent Air Particulate Monitor ML19031A5471977-01-0404 January 1977 LER 1976-017-01 for Salem, Unit 1 Inoperable Personnel Air Lock - Elevation 100' ML19031A9201977-01-0303 January 1977 LER 1976-016-01 for Salem Unit 1 Improper Use of Test Leads ML19031A9181976-01-0707 January 1976 LER 1976-021-01 for Salem, Unit 1, Boron Injection Tank Inoperable 2023-08-03
[Table view] |
Text
I I
i
\
Frederick W. Schneider Public Service Electric and Gas Company 80 Park Place Newark. f\l.J. 07101
- 201/622-7000 Vice Pres,der.t Production January 14, 1977 Mr. James P. O'Reilly Director of USNRC Off ice of Inspections and Enforcements Region I 631 Park Avenue King of Pruss~a, Pennsylvania
Dear Mr. O'Reilly:
LICENSE NO. DPR-70 DOCKET NO. 50-272 REPORTABLE OCCURRENCE 76-20/3L Pursuant to the requirements of Salem Generating Station Unit
Sincerely yours, CC: Director, Office of Inspection and Enforcement (40 copies)
Director, Office of Management Information and Program Control
( 3 copies)
Report Number:
Report Date:
Occurrence Date:
Facility:
.-_ 76-9-'3L 1/3/77 12/7/76 Salem Generating Station Public *service Electric & Gas Company Hancock's Bridge, New Jersey 08038*
IDENTIFICATION OF OCCURRENCE:
High .Reactor Coolant System Chlorides CONDITIONS PRIOR TO OCCURRENCE:
Operational Mode 3 P~ant Pressure 2235 psig Plant Temperature 540°F DESCRIPTION OF OCCURRENCE:
On 12/7/76 at 1630 hours0.0189 days <br />0.453 hours <br />0.0027 weeks <br />6.20215e-4 months <br />, the Performance Department informed the Shift
- Supervisor that the results of the Reactor Coolant System Chloride Analysis was 0.17 ppm. Being above the allowable Technical Specification Steady Si;".ate limit of 0.15 ppm Cl-, the Shift Supervisor implemented Technical Specification Action Statement 3.4.7 (a). The Performance Department continued to take chloride samples. No. 12 Mixed Bed Demineralizer was placed in service, No. 11 Mixed Bed Demineralizer was removed from service. On 12/8/76 (1600-2400 shift), the Reactor Coolant System chloride samples were within the Technical Specification limit. The Technical Specification Action Statement was cancelled.
DESIGNATION OF APPARENT CAUSE OF' OCCURRENCE:
The Boric Acid Storage Tank, which_had a chloride concentration near the upper limit (limit 0.15 ppm Cl),. was used to refill the Boron Inj ectin:n. Tar..k. The Boron Injection Tank was injected into the Reactor
- Coolant System four . (4) times due to inadvertent safety injection actuation which would have increased the chloride concentration but this determination is inconclusive due to the difficulty in achieving accurate chloride analysis in a boric acid solution. When 20,000 ppm boric acid solut".i.on is diluted to 5,0QO ppm boric acid, the dilut;!;on factor of 4 must be applied to the Cl endpoint. ~ny error in Cl titration endpoint is amplified by the application of the dilution factor~
ANALYSIS OF OCCURRENCE:
An Engineering,evaluation was performed by Westinghouse to determine the effects of the out of specification chloride condition in regard to the structural integrity of the Reactor Coolant System. The evaluation concluded that a chloride concentration of 0.3 ppm for a period of 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> would not cause any adverse effect to the Reactor Coolant System. Based on the RCS chloride concentration which was 0.17 ppm in regard to the Engineering evaluation performed assuming 0.3 ppm Cl- for a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> period, no corrective action is proposed for the Reactor Coolant System. At no time was there any danger to the health and safety of the public or site personnel.
LER 76-20/3L CORRECTIVE ACTION:
No. ll Mixed Bed was removed from service to determine whether or*not
. chlorides were being leached off the bed into the reactor coolant*. Both Mixed Beds were found to be performing satisfactorily. *The chemistry procedure for chloride determination by titration will be reviewed and revised as necessary to improve the "endpoint" determination.. Laboratory personnel will be reinstructed on the methods and techniques described in the procedure to visually determine the titration "endpoint". The Public Service Energy Laboratory will attempt.to develop a better pro-cedure for chloride analysis. The Westinghouse analysis of the problem determined there were no detrimental effects to the structural integrity ot the reactor coolant system. Follow up analyses indicate chlorides in the reactor coolant system to be well within specifications.
FAILURE DATA:
This is the first occurrence of this type. Equipment identification not
I Prepared by B. Canfield
, lr0 ~;1 * /
Manager - plem Generating Station
.SORC Meeting 3-77
LICENSEE EVENT REPORT.
CONTROl. !!LOC)( I 6
1..ICi:'.NS:EE \.ICENSlt !VENT NAME: 1..ICENSE NUMSER T.Vs>E TY~
@E]INIJ-!S!G!S!lf 9 . 14 j50!0l-IOIOIOI 010*1-101 qJ k41 ll ll ll l~ 1?1\~
~E:PO!=tT REPORT CATEGQRV TV"E SOURCE OQC~ET NUM6EA EVENT CATE REPORT OAT~
ram coN-rtS7P 1o1SB j-'"i l1J Sil
~
50 1015101-101217121 s1 e.a 1112101717161 69 74 10111013!7t7J 75 EVENT OESCRIPTION
@liI I During Mode 3 operation, the Performance Department 1.
1
@))I 89 (Chemistry) informed the Shift Supervisor that the results ro J
1 8 9
@El I of the reactor co.olant system sample anavlsis was 0 .17 ppm.
7 8 9 J
' @:fill Being above the allowable Technical Specification limit of I 1 a9 ao
~I 0.15 ppm,- the Shift Supervisor implemented (see attached) I" 7 a 9 . . PRIME ao SVSTEM c..=.use: COMPONENT COMPONENT
. COCE cooe: COMPONENT cooe SUF'Pl..IER MANUPACTUR!::R . VIOl.ATlON
@TI] t Cl BI L!J IZ I Z I Z I Z I ~ LE.J I ZI 9 I 9 I 9 I lliJ 1 s 9 10 11 12 17 43 44 47 48 CAUSE OESCl'llPTION
~I The Boric Acid Storage Tank chloride reading was near the I
@mi9 limit which was used to fill the Boron Injection Tank. The j 1 ag ea
[!]£JI Boron Injection Tank was injected into tha (see attached) I 7 a 9 ea FACll..ITV ME:TMOO OF
. STATUS ... POWER OTHER !.TAn.JS OISCOVS:RV osscove:Rv oe:sci:11PT10N
[El l.£j. 10 I O! 01 l~~~N~/~A,__~__.I @J I Chemistry Analysis 1 a 9 IQ 12 l:l 44 45 so FORM OF ACTIVITV CONTENT REl..EASEO OF i'IEl..EASE AMOUNT OF ""CTIVITV 1.oc:;i.TtON OF R£1...EASE
[!TI) ~ lbJ 11 N/A I '~---~___,,____N~/~A-.-~~-.--.-~_.,!I 1* a 9 10 11 44 45* so PERSONNEL EX?OSURES r.T.;'J NUMSER TVPE 0SC.RIPT10N
~[010101 1 a9
~I~~~*~N-/A---~~~~~~~~~~~~~~~~---:dl t:l so PERSONNEi. INJURIES NUM8£R C£SCRIPTION (IE}1010101 1 a9 11 NA
'="12;----------'---------------------------,,-,!eo OFFSITc CONSEQUENCES
- µE!l~9 ~~~~~~~~~*~N~/~A-=.,.-~~~~~~--~~~~--.,.~~~~~---...1J "LOSS OR OAMAGc TO FACILIT"I' TV!>!; C£~C.RtPTION (ili]1z1 I N/A j 1 a'T'""' ~10..-----------.._------------------------"r:l~
?t.181..ICITY
[!I?]
7 8~9------------.u+...<;>..----------------------- . . . . ----'
AOOITIONAI. FACTORS QE 1 a~3-~-----------------------------------------'ao
[lli]
1 a~~:------------------------------------------=' 90 NAMS: _ _ _ _ _ _ _B_.--E_.__ c_a_n_.f_i_e_l_d____ PHONe: ( 6 09) 3 65-7 0 00 Ext. Salem-5 2
Reportable Occurrence 76-20/3L Licensee Event Report Page (2)
EVENT DESCRIPTION (Continued)
Technical Specification Action Statement 3.4.7 (a). The Performance Department continued to t&ke additional samples. No. 11 Mixed Bed Demineraliz~r was taken out of service and No. 12 Mixed Bed Demineral-izer was placed in service. On 12/8/76 (4 PM ~ 12 PM shift), sample results were in specification. Technical Specification Action State-rnent was cancelled. Redundant system availability is not applicable for this occurrence. This is the first occurrence of this type (76-20/3L).
CAUSE DESCRIPTION (Continued)
Reactor Coolant System four times due to.inadvertent safety injection actuation which could have resulted in the increased chloride concert-tration, but this cannot be conclusive due to the ,difficulty to achieve accurate chloride sample analysis in a boric acid solution by the method of mercuric titration. When a 20,000 ppm boric acid sample is diluted to 5,000 ppm to titrate for chlorides, any error i!f determining this epdpoint is multiplied by the original dilution ratio (4 to 1). Also, consistent results are difficult to achieve when the.boron concentration changes. Hydrazine and ammonia analyses were performed on No. 11 Mixed Bed Demineralizer which verified no inter-reaction occurred to produce chlorides.
Manufacturers nameplate data not applicable for this occurrence.