ML19030A356

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Submit Monthly Operating Report for the Month of June 1977 for Salem No. 1
ML19030A356
Person / Time
Site: Salem  
Issue date: 07/08/1977
From: Heller H
Public Service Electric & Gas Co
To:
NRC/IE, Office of Nuclear Reactor Regulation
References
Download: ML19030A356 (4)


Text

' _,.

-.J Public Service Electric and Gas Company Salem Nuclear Generating Station P.O. Box #168 Hancocks Bridge, New Jersey 08038

.50--Z 77.,

Director Off ice of U.S. Nuclear Regulatory Washington, D.C.

20555 MONTHLY OPERATING REPORT SALEM GENERATING STATION July 8, 1977 In compliance with Section 6.9, Reporting Requirements for the Salem Technical Specifications, the following Monthly Operating Reports for the month of June, 1977 are being sent to you.

(Original plus 10 copies)

Appendix B -

Average Daily Unit Power Level Appendix C -

Operating Data Report Appendix D - Unit Shutdowns and Power Reductions Additional copies of the Monthly Operating Reports are being sent to:

1.

Mr. James P. O'Reilly Director of US NRC

2.

Office of Inspection and Enforcement Region I 631 Park Avenue King of Prussia, PA 19406 Director, Office of Management Information and Program Control us Nuclear Regulatory Commission (1 COPY)

(_2 COPIES)

Washington, D.C.

20555

!-! ~ kidLJ )01-f Manager -Valero Generating Station Enc.

Pg. 1-4 8-1-7.Rl The Energy People 771*:;15(J::::::;:1 95-2189 (SM) 10-72

MONTH June, 1977 APPENDIX B

  • AVERAGE DAILY UNIT POWER LEVEL OOCKET NO.

50-272 UNIT,

Salem # 1 DATE -----------

COMPLETED BY J.M. Zupko, Jr.

TELEPHONE 309-365-7000 X507 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL 1

2 3

4 5

6 7

8 9

10 11 12 13.

14 15 16.

Pg. 2-4 8.1-7.RI::,

.CMWe-NET) 1,003 1 056 1 076 473 0

0 0

0 0

0 d

0 0

0 0

0 (MWE-NET) 17 0

18 346 19 831 20 947 21 1 016 22 1,057 23 1 043 24 1 040 25 814 26 429 27 0

28 29 575 30 833 31

Pg. :3-4 8-1-7.Rl..

APPBIDIX C OPERATING DATA REFO.

toCKET m. ___

5_0-_2_1_2 ____ _

UNIT Salem #1 DATE July 8, 1977 CCMPLEl'ED BY TELEPHONE*

J.M. Zupko, Jr.

OPERATING S!A'IDS 609-365-7000 X507

l. REPOR!ING PERIOD: June, 1977 GROSS HOURS IN REPORTING PERIOD:

720

2.

CUBREN!LY All'IHORIZED POWER LEVEL (Ml'lt) :333 8MAX.DEPEND.CAPACIT'f(MWe-NEl'): 1090 DESIGN ELECTRICAL RATING(MNe-Net): 1090

3. Pa'lER LEVEL TO WHIClI RF.STRICI'ED (IF ANY) (MWe-Net) : _ _....N_on.._e ____ _
4.

BEA-CONS FOR RESTRICTION (IF mt) :.

S.

NtM3ER OF BJURS REACTOR WAS CRITICAL *

  • THIS MM'H YR TO DATE 393.* 4 3,156.5
6.

REACTOR RESERVE SHIJ'IT.OWN HOURS * * * * * * *

0. 0 o.o
  • 1.

HOURS GENERATOR ON LINE * * * * * * * * *

  • 325.7 2,788.2
8.

UNIT RESERVE SHU'I'001'N HOURS * * * * * * *

  • __

_.o......... o 0.0 CUMULATIVE 3,458.1 o.o 2,828.5 0.0

9.

GROSS TIIERMAL :ENERGY GENERATED {}n'!H) * * *." 9 5 3, 6 4 5 5,631,187 5,679,884 316,470 1,793,610 1,796,840

11. NET ELECTRICAL ENERGY GENERATED (MMi) * * *.2 9 5, 13 9 1,634,483 1,634,483
12.

REACI'OR SERVICE FACTOR * * * * * * * * *

  • 100.0 100.0 100.0 100.0
13.

REACTOR AVAILABILITY FACTOR ***...

14. UNIT SERVI CC F.ACTOR * * * * *
15. UNIT AVAILABILIT'l FACTOR * ****. **.
16. UNIT CAPACITY' FACI'OR(Using MDC)* * * * * * *
77. 0
17. UNIT OOACITf FACl'OR(Using Design MWe) *** __

7

..... 7_..... o

18.

UNIT FORCED OUT.AGE RATE * * * * *, *, *

  • 0
  • O

--..,_,;~

100.0 100.0 100.0 100.0 77.0 77.0 0.0 100.0 100.0 100.0 100.0 77.0 77.0 0.0

19.

SHUTI:XJWNS SCllEDULED OVER Nm 6 MJNI'HS (TYPE,DATE,.~ DURATJ;ON OF EAOl) : 9-17-7 7 Modification of Low Pressure Turbine.

ZO.

IF SHUT OOi'IN AT END OF P-EPOPJ' PERIOD, ESTIMATED DATE OF sr.~:._......:.N~/.;.;A=-----

Zl. UNITS rn ~""!' STATIJS (PRIOR 'IO CDMERCIAL OPERATION) :

FORECAST INITIAL CRITICALIT'f 9-3 0- 7 6 INITIAL ELECTRICITY 11-01-7 6 CCliMERCIAL OPERATION 12-20-76 AC-ilEVED 12-11-76 12-25-76 6-30-77

APPENDIX D DOCKET NO.

50-272 I

~

~

UNIT SHUTDOWNS J\\ND POWER REDUCTIONS UNIT NAME Salem #1 1


," t DATE July 8, 1977


=----'-----

COMPLETED BY J. M. Z upko, Jr.

TELEPHONE 609-365-7000 Ex. 507 REPORT MONTH June, 197 7 METHOD OF CORRECTIVE ACTIONS/COMMENTS~

TYPE OITTAGE SHUTTING DOWN F: FORCED DURATION 1HE REACTOR OR NO.

DATE S: SCHEDULED (HOURS)

REASON REDUCING POWER 77-38 6/4/77 F

328.5 A

3 Failure of a 4kv cable to No. 14 RCP.

77-39 15/23/77 F

0.0 H

4 Clean condensate pump strainers.

77-40 15/24/77 F

0. 0.

H 4

Clean No. 11, 12 Stm. Gen.

Feed Pump Strainers.

77-41 6;26;11 F

9.5 B

3 Startup Test - Generator Trip from 100% Power

  • P

SUMMARY

g.4-4 8.1-7.R 1

  • LOAD REDUCTION.

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