ML19030A356

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Submit Monthly Operating Report for the Month of June 1977 for Salem No. 1
ML19030A356
Person / Time
Site: Salem  PSEG icon.png
Issue date: 07/08/1977
From: Heller H
Public Service Electric & Gas Co
To:
NRC/IE, Office of Nuclear Reactor Regulation
References
Download: ML19030A356 (4)


Text

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Public Service Electric and Gas Company Salem Nuclear Generating Station P.O. Box #168 Hancocks Bridge, New Jersey 08038 July 8, 1977

.50--Z 77.,

Director Off ice of U.S. Nuclear Regulatory Washington, D.C. 20555 MONTHLY OPERATING REPORT SALEM GENERATING STATION In compliance with Section 6.9, Reporting Requirements for the Salem Technical Specifications, the following Monthly Operating Reports for the month of June, 1977 are being sent to you.

(Original plus 10 copies)

Appendix B - Average Daily Unit Power Level Appendix C - Operating Data Report Appendix D - Unit Shutdowns and Power Reductions Additional copies of the Monthly Operating Reports are being sent to:

1. Mr. James P. O'Reilly (1 COPY)

Director of US NRC Office of Inspection and Enforcement Region I 631 Park Avenue King of Prussia, PA 19406

2. Director, Office of Management Information (_2 COPIES) and Program Control us Nuclear Regulatory Commission Washington, D.C. 20555

!-! ~ kidLJ )01-f Manager -Valero Generating Station Enc.

Pg. 1-4 8-1-7.Rl 771*:;15(J::::::;:1 The Energy People 95-2189 (SM) 10-72

APPENDIX B AVERAGE DAILY UNIT POWER LEVEL OOCKET NO. 50-272

"' UNIT , Salem # 1 DATE -----------

COMPLETED BY J.M. Zupko, Jr.

TELEPHONE 309-365-7000 X507 MONTH June, 1977 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL

.CMWe-NET) (MWE-NET) 1 1,003 17 0 2 1 056 18 346 3 1 076 19 831 4 473 20 947 5 0 21 1 016 6 0 22 1,057 7 0 23 1 043 8 0 24 1 040 9 0 25 814 10 0 26 429 11 d 27 0 12 0 28 13 . 0 29 575 14 0 30 833 15 0 31 16 . 0 Pg. 2-4 8.1-7 .RI::,

APPBIDIX C OPERATING DATA REFO.

toCKET m. ___5_0-_2_1_2_ _ _ __

UNIT Salem #1 DATE July 8, 1977 CCMPLEl'ED BY J.M. Zupko, Jr.

OPERATING S!A'IDS TELEPHONE* 609-365-7000 X507

l. REPOR!ING PERIOD: June, 1977 GROSS HOURS IN REPORTING PERIOD: 720
2. CUBREN!LY All'IHORIZED POWER LEVEL (Ml'lt) :333 8MAX.DEPEND.CAPACIT'f(MWe-NEl'): 1090 DESIGN ELECTRICAL RATING(MNe-Net): 1090
3. Pa'lER LEVEL TO WHIClI RF.STRICI'ED (IF ANY) (MWe-Net) :_ _....N_on.._e_ _ _ __
4. BEA-CONS FOR RESTRICTION (IF mt) : .

THIS MM'H YR TO DATE CUMULATIVE S. NtM3ER OF BJURS REACTOR WAS CRITICAL *

  • 393 .* 4 3,156.5 3,458.1 o.o o.o
6. REACTOR RESERVE SHIJ'IT.OWN HOURS * * * * * * *

0. 0

  • 1. HOURS GENERATOR ON LINE * * * * * * * * *
  • 325.7 2,788.2 2,828.5
8. UNIT RESERVE SHU'I'001'N HOURS * * * * * * *
  • _ __.o......... o 0.0 0.0
9. GROSS TIIERMAL :ENERGY GENERATED {}n'!H) * * * ." 9 5 3 , 6 4 5 5,631,187 5,679,884

. .316,470 1,793,610 1,796,840

11. NET ELECTRICAL ENERGY GENERATED (MMi) * * * .2 9 5 , 13 9 1,634,483 1,634,483
12. REACI'OR SERVICE FACTOR * * * * * * * * *
  • 100.0 100.0 100.0
13. REACTOR AVAILABILITY FACTOR *** ... 100.0 100.0 100.0
14. UNIT SERVI CC F.ACTOR * * * * * ..... 100.0 100.0 100.0 15.

16.

UNIT AVAILABILIT'l FACTOR * * * *

  • UNIT CAPACITY' FACI'OR(Using MDC)* * * * * *
  • __ 100.0

........,....0 77.

100.0 77.0 100.0 77.0

17. UNIT OOACITf FACl'OR(Using Design MWe) * *
  • _ _7.....7_..... o 77.0 77.0
18. UNIT FORCED OUT.AGE RATE * * * * * , * , * * --..,_,;~ 0*O 0.0 0.0
19. SHUTI:XJWNS SCllEDULED OVER Nm 6 MJNI'HS (TYPE ,DATE,.~ DURATJ;ON OF EAOl) : 9-17-7 7 Modification of Low Pressure Turbine.

ZO. IF SHUT OOi'IN AT END OF P-EPOPJ' PERIOD, ESTIMATED DATE OF sr.~:._......:.N~/.;.;A=-----

Zl. UNITS rn ~""!' STATIJS (PRIOR 'IO CDMERCIAL OPERATION) : FORECAST AC-ilEVED INITIAL CRITICALIT'f 9- 3 0- 7 6 12-11-76 INITIAL ELECTRICITY 11-01-7 6 12-25-76 Pg. :3-4 CCliMERCIAL OPERATION 12-20-76 6-30-77 8-1-7 .Rl..

APPENDIX D DOCKET NO. 50-272 I ~


'- ~

UNIT SHUTDOWNS J\ND POWER REDUCTIONS UNIT NAME Salem #1 - 1


," t DATE July 8, 1977


=----'-----

COMPLETED BY J . M. Zupko , Jr.

TELEPHONE 609-365-7000 Ex. 507 REPORT MONTH June , 197 7 ----------

ACTIONS/COMMENTS~

METHOD OF TYPE OITTAGE SHUTTING DOWN F: FORCED DURATION 1HE REACTOR OR NO. DATE S: SCHEDULED (HOURS) REASON REDUCING POWER CORRECTIVE 77-38 6/4/77 F 328.5 A 3 Failure of a 4kv cable to No. 14 RCP.

77-39 15/23/77 F 0.0 H 4 Clean condensate pump strainers.

77-40 15/24/77 F 0. 0 . H 4 Clean No. 11, 12 Stm. Gen.

Feed Pump Strainers.

77-41 6;26;11 -

F 9.5 B 3 Startup Test - Generator Trip from 100% Power *

SUMMARY

*LOAD REDUCTION.

Pg.4-4 8.1-7.R 1 __J