ML18347A836

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Monthly Operating Data for June 1975
ML18347A836
Person / Time
Site: Palisades Entergy icon.png
Issue date: 07/02/1975
From: Meincke J
Consumers Power Co
To:
Office of Nuclear Reactor Regulation
References
Download: ML18347A836 (4)


Text

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  • i:Lcu ,.7 consumers Power company Palisades Nuclear Plant: Route 2, Box 154, Covert, Michigan 49043 July 2, 1975

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U. So Nuclear Regulatory Commission Mail and Records Section Washington, D. C., 20555 Re: License Reports DPR-20 Docket No.: 50-255 Gentlemen:

Enclosed is a copy of the monthly operating data for the Palisades Nuclear Plant for the month of June, 1975*

Sincerely, James A. Meineke General Engineer JAM: DB cc: J.G.Keppler, NRG R.L.Haueter R.B.Sewell 7J 17'i

.-* *--~

APPENDIX C DOCKET NO. -~5_0-_2~5~5__

UNIT __P_a_l_i_s_a_d_e_s_

DATE July -2, 1975 COMPLETED BY J .A.Meineke AVERAGE DAILY UNIT POWER LEVEL MONTH June 121'.2 AVERAGE DAILY POWER LEVEL A VERA GE DAILY POWER LEVEL DAY (MWc-net) DAY (MWe-net) 1 505 17*. 495 2 504 18 482 I"

3 506 19' 488 4 494 20 408 5 427 21 0 6 504 22

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  • .  ;.-:.h 7 507 23 0 B 503 24 . 0 9 504 25 0

. 10 5.DO 26 o*

11 428 27. 6 12 505 28 0 13 211 29 0 14 208 30 1"5 505 31 16 '204 DAILY UNIT POWER LEVEL FORM INSTRUCTIONS On this form, list the average daily unit power level in t-.*1\Ve-net for each day in the reporting month.

Compute to the nearest whole megawatt.

These figures will be used to plot a graph for each reporting month. Note that by usi*ng maximum dependable capacity for the net electrical rating of the unit, there may be occasions when the daily

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  • averJge power level exceeds the 100% line (or the restricted power level* line). In such cases, the

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  • Q*:**. *: averJge daily unit power output sheet should be footnoted to explain the ap.parentanomaly.

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0 APPENDIX E

.o DOCKETNO. --"-50_-_25~5_ _ __

UNlT SHUTDOWNS UNIT NAME Palisades

  • DATE July 2, 1975 COMPLETED BY J .A.Meineke REPORT MONTH _ _;.J;..;;u=n=e....::1=9'"""7""5_ _

TYPE METHOD OF F-FORCED DURATION $HUTTING DOWN NO. DATE S-SCHEDULED (HOURS) REASON (1) THE REACTOR (2) CORRECTIVE ACTIONS/COMMENTS 3 750620 F. 227.3 A l Shutdown to Repair CRDM Seal Leak 4 750630 F 7.9 R 2 Feedwater Pump trip

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(1) REASON (2) METHOD A--EQUIPMENT FAILURE* (EXPLAIN) I-MANUAL B- MAINT. OR TEST 2-MANUAL C--REFUELING SCRAM D-REGULATORY RESTRICTION 3-A UTOMA TIC*

E-OPERATOR TRAINING AND SCRAM LICENSE EXAMINATION

- . F-ADMINISTRATIVE G-OPERATIONAL ERROR.

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(EXPLAIN)

H-OTHER (EXPLAIN) l

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SUMMARY

IJ:he unit operated at 80% power until June. 20t~ when a:leaking Control_ Rod seal caused the unit to shut down. The unit was put on-line June 30th af'ter repairs, taken off when a feedwater pump tripped, and again put on-line andhold~ng at 25%.

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    • e APPENDIX D*

UNIT _ _P_a_l_i_s_a_d_e_s__

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DATE July 2 J.;975

  • 616-764-8913 .

' COMPLETED BY _ _J_._A_._M_e_in_c_k_e_

' ' DOCKET N0. _ _5_0_-_2'--55'-----

OPERATING STATt;S

1. REPORTING PERIOD: _ _ _7_5_0_6_0_l_ _ _ _ _ _ _ _ THROUGH _ _ _7'-5_0_6-'3_0_ _~----

HOURS IN REPORTl:-:G PERIOD: _ _ _ _7'-2_0_---,--------------------..,--,---

2. CURRENTLY ACTHORIZED POWER LEVEL ('.\1Wth). 2200 MAX. DEPENDABLE CAPACITY (l\!We-NET) 6R4
3. LOWEST POWER LEVEL TO WlllCI! SPECIFICALLY RESTRICTED (IF ANY) (MWe-NET): _ _ _6_3~0______
4. REASONS FOR RESTRICTION (IF AN,Y): Power .restricted to 2100 Mvrt due to reduced*

Pr:ilnary Coolant Flow as a result of Steam Generator Tube plugging.

THIS CUMULATIVE REPORTING PERIOD YR TO DATE TO DATE S. HOURS REACTOR WAS CRITICAL. . . . . . . . * . . . . 492.7 1,976.5 12,213.4

6. REACTOR RES!ORYE SHUTDOWN HOURS ......* /" 0 0 0
7. HOURS GENERA TOR ON LINE. *. . . . . . . . . . . * .
  • 485.5 1,887.3 11, 208. 4
8. UNJT RESERVE SHUTDOWN HOURS . *.. ~ . . . . . .
  • 0 0 0
9. GROSS THERC\IAL ENERGY GENERATED(MWHJ . . . . . * . . . . . . . * . * . . . * . 873,360 3,175,872 17,289,432
10. GROSS ELECi:RICAL ENERGY GENERA TED ('.\!Wll) . . . . . . . . . . . . . . . . * . . . . 257,000 952,840 5,457,090 c;**,*Q.'. 11. NET ELECTRICAL ENERGY GENERATED

(!\!Will ...................*..*.*.... 881,977 5 ,135 ,682 68.4~ 39.9%.

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l :!. REACTOR AVAILABILITY fACTOR (!) . . . . . . . . . "45.5%

13. UNIT AVAILABILITY FACTOR (2) . . . * * . * * . * . . 61.4' 0 ' 43*.4~ _ _,;.;36_._6%;
14. l 1NIT C-AP.*\CITY FACTOR (3) ............*.. 48.4% 29.7°/o 28.J%
15. UNIT FORCED OllTAGE RATE (4) . . . * . . . . . * . . 32.6% _26.6% 60.8%
16. SllVTDOWNS SCHEDULED TO BEGIN IN. NEXT 6 MONTHS (STATE TYPE, DATE, A ND DURATION OF EACH):

Steam Generator inspect1:si~l1~~st, 8 weeks_ . . *

17. IF SHt:T DOWN AT END OF. REPORT PERIOD, ESTIMATED DATE Of S T A R T U P : - - - - - - - - - - - -
18. UNITS IN TEST STATUS (PRIOR TO COM:.IERCIAL OPERATION) REPORT THE FOLLOWING:

DATE LAST DA TE FORECAST ACHIEVED INITIAL CRITICALITY INITIAL ELECrRICAL POWER GENERATION * .

COMMERCIAL OPERATION HOURS RF.ACTOR WAS CRITICAL (1) R,EAC'TOR A \'AILABILITY FACTOR x 100 HOURS IN REPORTING PERIOD

_H_O_U_R_S__G_l_:N_'E_*R_A_T_O_R_O_N_L_IN._'E_ _ X I OO t:NIT A\' AlLABILITY FACTOR HOURS IN REPORTING PERIOD NET ELF.CTR IC' AL POWFR GE!'IERATED MAX. DEl'ENDABLI-: CAPACITY (l\!Wc-NET) X HOURS IN REPORTING l'EIUOD FORCED OUTAGE HOURS.

- - - - - - - - - - - - x 100 HOURS GENERATOR ON LINE+ FORCED OUTAGE HOURS 1.16-D-J