ML18227B096
| ML18227B096 | |
| Person / Time | |
|---|---|
| Site: | Turkey Point |
| Issue date: | 09/09/1975 |
| From: | Schmidt A Florida Power & Light Co |
| To: | Office of Nuclear Reactor Regulation |
| References | |
| Download: ML18227B096 (14) | |
Text
MONTllLY ~EPORTS (FOR GRAY BOOK PREPARA7>
9)
NRC TRIBUTIQN FOR PART 50 DOCKE MATERIAL (TEMPORARY FORM)
CONTROL NO:
6 O
FII E
~ MONTllLY REPORT FI FROM Flordia Power
&, Light Co.
Miami. Flordia A.. Schmi t DATE OF DOC DATE REC'D LTR TWX RPT OTHER TO:
ORIG NRC 1 Si ned CC OTHER SENT AEC PDR SENT LOCAL PDR CLASS UNCLASS PROP INFO INPUT NO CYS REC'D DOCKET NO:
5-21 DESCR IPTION:
Ltr trans the following:
PLANT NAME:
Turkey Point g 3'NCLOSURES:
Monthly Report for Au st 1 Plant
& Component Operability & Availabilit This Report to be used in preparing Gray Bo by Plans
& Operations.
NUIIBER OF COPIES REC'D:
FOR ACTION/INFORMATION AB BUTLER (L)
W/'opies CLARK (L)
W/ Copies PARR (L)
W/ Copies KNIEL (L)
W/ Copies FI R
R OGC, ROOM P-506A.
GOSSI CK/STAF F CASE GIAMBUSSO BOYD MOORE (L)
DEYOUNG (L)
SKQVHQLT (L)
GQLLER (L) (Ltr)
P. COLLINS DENISE REG OPR FII F It( REGION (2)
STEELE SCHWENCER (L)
ZIEMANN(L)
W/ Copies W/ Copies STOLZ (L),
DICKER (E)
W/ Copies W/ Copies VASSAL LO (L)
KNIGHTON (E)
W/ Copies W/ Copies PURPLE (L)
YOUNGBLOOD
~ W/ Copies W/ Copies INTERNALDISTR DENTON GRIMES GAMMILL KASTNER BALLARD SPANGLER TECH REVIEW SCHROEDER MACCARY KNIGHT PAWLICKI SHAO STE LLO HOUSTON NOVAK ROSS IPPOLITO TEDESCO J
COLL?NS LAI NAS BEMAROYA VOLLMER ENVIRQ MULLER DICK F R KNIGHTON YOUNG B LOQD BEGAN PROJECT LDR HAR LESS M DUN EXTERNALDISTRIBUTION REGAN (E)
W/ Copies gLEAR (L(
A(CKNOWLED SPELS W/ Copies (El~ MIPc/PE DO NOT P@MO+@
W.4 Copies IBUTION LIC ASST A/T IND.
R. DIGGS (L) 'RAITMAN H. GEAR IN (L)
SALTZMAN E. GOULBOURNE (L)
IVIELTZ P. KREUTZER (E)
J. LEE (L)
M. RUSliBRCCK (L)
~ MCDONALD S. REED (EI
. ~CHAPMAN M SERVICE (L)
DUDE (Ltr)
S. SHEPPARD (L)
E. COUPE M. SLATER (E)
PETERSON H. SMITH (L)
HARTFIELD (2)
S. TEETS (L)
KLECKER G. WILLIAMS(E)
EISENHUT V. WI LSON (L)
WIGGINTON
~R. INGRAM (L)
AN
~l LOCALPDR M~K, Flordia
~1 TIC (ABERNATHY)
(1)(2)(10) NATIONALLABS
~1 NSIC (BUCHANAN) 1 W. PENNINGTON, Rm E-201 GT 1 ASLB 1
CONSULTANTS 1 Newton Anderson NEWMAR K/BLUME/AGBAB I AN 1 PD R-SAN/LA/NY 1 BROOKHAVEN NAT LAB 1 G. ULRIKSON, ORNL 1 AGMED (RUTH GUSSMAN Rm B-127 GT 1 J. D. RUNKLES, Rm E-201
IteguletotiI I) o~
e.~,;%Imp SEt'221975 ~
6 KS.
II1CI- -oVIIpT C$4SIIouoIpiI
,IIt1SiiItpmy I'>II Scsllss a
gSeje', 4d P.O. BOX 013100 MIAMI,FLA. 33101 FLORIDA POWER & LIGHT COMPANY September 9, l975 Office of Management Information and Program Controls U. S. Nuclear Regulatory Commission Washington, DC 20555 Gentlemen:
Attached are the August, l975 Operating Status Reports for Turkey Point Units Nos.
3 and 4.
Very truly yours, Vice President Power Resources VTC/dd Attachments D~/Q D0CKBSg
.AIIIIQ 2
SE 1,
i197So 5
Ihoil Soctioq Ducat Cbh, e
cc:
Mr. Norman C. Moseley Jack R.
- Newman, Esquire SBBQ HELPING BUILD FLORIDA
ENCLOSURE A DOCKET NO.
UNIT NAME TURKEY POINT NI DATE Se tember 5
1975 COMPLETED BY Mar lee Mont orner TELEPHONE NO.
305 245-2910 Ext.
228 "DAILY 'UNIT'PONER OUTPUT M3iVIH DAY AVERAGE DAILYWe-net DAY AVERAGE DAILY M<e-net 3
4 9
10 12 13 16 17 19
67 666 660 657 652'49 648 661 668 665 631 461 654 6 57.
657 659 657 657 653 20 21 22 23.
24 25 26 27 20 29 30 31 NOTE:
654 6
4 6
8 383
- '224" 6,45
'" 648
' '651"
<65pa Daily average power level greater than 666 MWe, due to cooler condenser cool-water.
DOCKET NO."50-250 UiiIIT NNIE'>>
TURKEY POINT IT No 3
k REPORT MONTH AUGUST, 1975 DATE Se tember 5
19 CPi%'I.EIED BY TELEPIIONE '0 245-2910 EXT.
228 OPERATING STATUS 1.
REPORTING PERIOD:
01 75 08 Ol THROUGH 2400 75 08 31 GROSS HOURS IN REPOI<'I'ING PERIOD:
744.0 2.
3.
CURRENTLY AUTHORIZED PP1KR LEVEL (Mft) 2200 Mi1X. DEPEND.'APACITY (MWe NET) 666 POWER LEVEL TO lRICH RESTRICTED (IF.ANY): (M~'e NET):
NONE 4.
REASOiNS FOR RESTRICTIONS (IF ANY):
S.
NUiiBER OF HOURS THE REACTOR WAS I
CRITICAL
~
~
~
~
~
~
~
~
~
~
~
~
~ ~
~
~
~
~
~
~ t'
~ ~
~
~ ~
~
6.
REACTOR RESERVE SHUTDOWN HOURS........
7.40.9 5 577.4 'IBIS MONTH
'R-Tp-DATE CUMULATIVE TO DATE 19 605.2 * ~
=
~
7.
HOURS GENERATOR ON LINE...............
733.0 5 476.3 18 894.6 8.'~
UNIT. RESERVE SHUTDOWN HOURS.....:.....
9.
'GROSS THECAL ENERGY GENERATED(MR).... "85 0
10.
GROSS ELECTRICAL EiiERGY GENERATED (MR).........................;........
490 895
- 3. 665 066 ll; NET ELECTRICAL ENERGY GENERATED (MR)..
466 603 3 509 475 12.
REACTOR AVAILABILITYFACTOR +1.........
- 99. 6
- 95. 7 11 092 871 10 490 640 81.6 13.
14.
1S.
UNIT AVAILABILITYFACTOR J2',...........
UNIT CAPACITY FACTOR J3................
UNIT FORCED OUTAGE RATE J4 8
5 94.2 i1.5 93.9 90.4 3.8 78.7
- 67. 0 4.1 16.
17.
SHUTD01%S SCI.IEDULED OVER NEXT 6 MONTHS (TYPE, DATE AND DURATION OF EACH):
Oct,. ?0 - Nov,, 30, 1975 - Refueling, Maintenance and Inspections.
IF SHUTDOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP:
Jl REACTOR AVAILABILITY FACTOR 'OWS ~&OR WAS GRITI~ X 100 GROSS HOURS IN REPORTIN PERIOD J2 UNIT AVAILABILITYFACTOR Hp~ GENEIRTOR ON LINE X 100 GROSS HOURS IN REPORT PERIOD
~Ii 3 4 UNIT CAPACITY FJ CTPR NET ELECTRICAL POWER GENERATED X 100 MAX. DEPENDABLE CAPACITY X GROSS HOURS IN REPORT PERIOD 4
UNIT OUTAGE RATE = FORCED OUTAGE HOURS X MO HOURS GENEIKNR PN LINE +
FORCED OUTAGE HOURS
/
0 S
SR&MY:
Unit No.
3 operated at. 100
.R.P..for entire month except for. load reduction, on august ll, 1975, to repai condenser tube leak and reactor.trips on August -26,
. 1975.
DOCKET NO.
50 250 ggIT NAME
" TURKEY POXNT'UNIT NO.
3 DATE SEPTEMBER 5 g 1 9 75 PREPARED BY MARYLEE MONTGOMERY.
TELEPHONE 05 245-1 Ext.
REPORT hoiVTH AUGUST, 1975 U N I T S H U T D 0 N N S / R E D U C T I 0 N S T PE F-FORCED S-SCHEDULED DURATIOiV (HOURS)
REASON *
~
MEIHOD OF SHUTTING DONii1
'IHE REACTOR COi%KKS 25 75-08-3.1 F N/A'oad on Unit No.
3 was reduced to repair condenser tube leak (Non-nuclear system) 26
~ 27 75-'08-. 26 75-08-26 3.2
.7. 8 A,
~
3 3
Reactor was tripped on No.
3C reactor coolant pump breaker open coincident with reactor power greater than 45% R.P.
caused by incipient failure of a. coil in. Unit No.
(Nuclear system)
Reactor was tripped on No.
3C reactor coolant pump breaker open coincident with reactor power greater than 45% R.P.
caused by the failure of a coil in Unit No.
(Nuclear system)
REASOiV:
A-E(PIPi~KÃZ FAILURE ~LAIhO B-hS.INT.
OR TEST C-REFUEI.ING D-REGULATORY RESTRICTION E-OPERATOR TRAINING AND LICENSE EXAMINATIOiV F-AIMINISTRATIVE G-OPERATIONAL ERROR H-OTHER (EXPLAIN)
.! ** hK1HOD:
l-h MAL 2-h94WAL SCRAM 3 AUTOMATIC SCRAM
~
k\\
~ I
(
II 0
I l f
~ h
ENCLOSURE A DOCKET NO.
50-251 UNIT NAME TURKEY POINT UNIT NO.
4 SEPTEMBER 5, 1975 COMPLETED BY TELEPHONE NO.
MARYLEE MONTGOMERY 305 245-2910 DAILY UNIT'OWER OUTPUT AUGUST, 1975 AVERAGE DAILYN'fe-net
.. DAY AVERA(Z DAILYMite-net
~ 622 609 10 267 644 692 642 598 20 21 22 23 24 25 26 27 28 29 30 31 644 647 651 653 652 647 645
'" 643 641
=640 64-3 638 644
'46 649 647 642 NOTE:
Daily average power level greater than 666 MWe, due to cooler condenser cool-water.
64
1 DOCKET NO. 50-251 UjiIIf N~IE.
TURKEY'OI UNXT NO.
4, DATE SEPTEMBER 5
1975 COMPLE'fED BY MARYLEE MONTGOMERY TELEPIIOiNE 30 245-2910 Ext.
228 ORT MONTH AUGUST, 1975 OPERATING STATUS
\\
1.
REPORTING, PERIOD:
0001 75 08 01 TFIROUGH 2400 75 08 31 GROSS FIOURS IN REPORTING PERIOD:
4 2.
CURRENTLY AIJIHORIZED POWER LEVEL (Mft)
MAX. DEPEND.
CAPACITY (bNe NET) 2200 666 3.
POWER LEVEL TO NILICH RESTRICTED (IF ANY):
(MI<e.NET)
None 4.
REASONS FOR RESTRICTIONS (IF ANY):
THIS MOVIN YR-TO-DATE CUMLATIVE
'IQ DATE 5.
NUMBER OF HOURS THE REACTOR WAS CRITICAL
~
~
~
~
~
~
~ ~
~
~
~
~
~
~
~
~
~
~
~
~ ~
~ y 600 ~ 1 6.
REACTOR RESERVE SHUTDOWN HOURS......,, 3 663.2 12 997.1 7.
HOURS GENERATOR ON LINE...............
8.'.'NIT RESERVE SHUTDOWN HOURS......;....
590.4 3 561.7 12 619. 5 9.
GROSS THEMEENERGY GENERATED(Mt%)....
1 282 ill 7 '550 826 25 903 036 10.
GROSS ELECTRICAL ENERGY GENERATED 8)
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~ ~
~
~
~
~
(Ml 396 710 11.
NET ELECTRICAL ENERGY GENERATED (Mt%)..
376 310 12.
REACTOR AVAILABILITYFACTOR +1........,
- 80. 7 2 403 336 2 277 006
- 62. 8 l
v 8 177 597 7 746 062 74.8 13.
UNIT AVAILABILITYFACTOR J2'............
14.
UNIT CAPACITY FACIQR J3.........,.....;.
15.
UNIT FORCED OUTAGE RATE J4
- 79. 3 75.9 61. 1
- 58. 6 0.2 72.6 68.2
-4;;0 16, SHUTDOINS SCHEDULED OVER NEXT 6 MONTHS (TYPE, DATE AND DURATION OF EACH):
Sept.
13-19, 1975 Scheduled
'Maintenance 17.
IF SHUTD01% AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP:
J$
REACTOR AVAILABILITY FACTOR 'O~
EAGTOR 10 S CRITI~ X 100 GROSS HOURS IN REPOR'I'IN PERIOD T AVAILABILITY FACIQR kIO~ GE&MTOR ON LINE X 100 GROSS HOURS IN REPORT 'PERIOD 3
UNIT CAPACITY FACTOR NET ELECTRICAL POWER GENERATED X 100 MAX. DEPENDABLE CAPACITY X GROSS HOURS IN REPORT PERIOD IT OUTAGE RATE FORCED OUTAGE HOURS X 100 FIOUIG GEJKIKIQR ON LINE +
FORCED OUTAGE HOURS
~
e' h
1I 4
4 (J
I* l
SUMMARY
- Unit No..
4 operated at 100%
R.P. except for scheduled maintenance shutdown August 8-9, 1975 and a load reduction on August 12, 1975 DOCKET NO.
50 251
,UNIT NAt5.
.."'URKEY POINT UNLT NO.
4 DATE SEPTEMBER 5, 1975 PREPARED BY MARYLEE MONTGOMERY TELEPHONE 30
- 245-2910 Ext.
228 REPORT MOVHH AUGUST, '975 U N I T S H U T D 0 N N S / R E D U C T I 0 N S
'1 PE F-FORCED
'-SCHEDULED DURATION (HOURS)
REASOiN
- METHOD OF SHUTTING ROUN
'IHE REACTOR *"
'OilENTS 11 75-08-03'53.7
~ B Unit No.
4 was removed from service. (controlled manual shutdown) to repair No.
4B steam generator tube leak (small leak in one of 3,260 tube).
There were no significant quantities of radio-active material released as a result of this small leak.
(Nuclear system) 12 75-08-12 N/A Load on Unit No.
4 was'utomatically reduced to approximately 70% R.P.
by No.
4 reactor protection system caused by loss of power supply to control rod drive mechanism H-4.
(Nuclear system)
REASON e
A-EQUIPiiT FAILURE (EPLAIg I
B-MAINT. OR TEST C-REFUELING D-REGULATORY RESTRICTION E-OPERATOR TRAINING AND LICENSE EXAMINATION F-ADMINISTRATIVE G-OPERATIOi%G ERROR H-OIHER (EXPLAIN METHOD:
1-MANUAL 2-MANUAL SCRAM 3-AUTO~iTIC SCRAM
~
I