ML18227A396
| ML18227A396 | |
| Person / Time | |
|---|---|
| Site: | Turkey Point |
| Issue date: | 09/09/1975 |
| From: | Schmidt A Florida Power & Light Co |
| To: | Office of Nuclear Reactor Regulation |
| References | |
| Download: ML18227A396 (15) | |
Text
MONT)II.Y REPORTS (FOR GRAY HOOK PREPARATION)
NRC DISTRIBUTION FOR PART 5
.OCKET MATERIAL (TEMPORARY FORM)
CONTROL NO:
6 0 FIjE
~ HolrfIILY REPQRT F,
FROM Flordia Power 8 Light Co.
Miami. Flordia A.
. Schmi t DATE OF DOC DATE R EC'D LTR TWX RPT OTHER CLASS UNCLASS PROPINFO ORIG 1 Si ned INPUT CC OTHER NO CYS REC'D SENT AEC PDR SENT LOCALPDR~~
DOCKST NO:
go-kg DESCRIPTION:
Ltr trans the following:
PLANT NAME: Turkey Point 8 384 ENCLOSURES:
Monthly Report for Au st 1 Plant
& Component Operability & Availabilit This Report to be used in preparing Gray H
by Plans
& Operations.
NEIBER OF COPIES REC'D:
FOR-ACTION/INFO RMATION AB BUTLER (L)
W/'opies CLARK (L)
W/ Copies PARR (L)
W/ Copies KNIEL (L)
. 'W/ Copies SCHWENCER (L)
ZIEMANN(L)
REGAN (E)
W/ Copies W/ Copies W/ Copies STOLZ (L)
DICKER (E)
/LEAR (L) +O NOT ~+<~oyp VASSALLO (L)
KNIGHTON (E)
SPELS W/ Copies W/ Copies W/ Cop,tgsn PURPLE (L)
YOUNGBLOOD (E)~ MIPc/R'~KIIWLED@@@
~ W/ Copies W/ Copies W.4 Copies'NTERNAL DISTRIBUTION F
~ NRC PDR OGC, ROOM P.506A GOSSI CK/STAFF CASE GIAMBUSSO BOYD
'OORE (L)
DEYOUNG (L)
SKOVHOL1 (L')
GOLLER (L) (Ltr)
P. COLLINS
- DENISE, REG OPR FII F A RFGION (2)
~ STEELE TECH REVIEW SCHROEDER MACCARY KNIGHT PAW LIC K I SHAO STELLO HOUSTON NOVAK ROSS IPPOLITO TEDESCO J.
COLLINS LAINAS BENAROYA VOLLMER DENTON LIC ASST G R IMES R. DIGGS (L)
'AMMILL H. GEAR IN (L)
KASTNER E, GOULBOURNE (L)
BALLARD
- p. KREUTZER (E)
SPANG LE R J. LE E (L)
M. RUS:IHV,CCK (L)
E NVIRO
~
S.
R F F D (E)
MULLER M. SERVICE (L)
DICKER S. SHEPPARD (L)
KNIGHTON M. SLATER (E)
YOUNG BLOOD H. SMITH (L)
REGAN S. TEETS (L)
PROJECT LDR G. WILLIAMS(E)
V. WILSON (L)
HAR LESS
~R. INGRAM (L)
)~IDUN AN EXTERNALDISTRIBUTION A/T IND.
BRAITMAN SALTZMAN
- MELTZ, PLANS MCDONALD' CHAPMAN DUDE (Ltr)
E. COUPE PETERSON HARTFIELD (2)
KLECKER EISENHUT WIGGINTON
~1 LOCALPDR ~mj, Flordia
~1 TIC (ADERNATIIY) (1)(2)(10) NATIONALLABS
~1 NSIC (BUCHANAN) 1 W. PFNNINGTON, Rm E-201 GT 1 ASLD 1
CONSULTANTS 1 Newton Anderson
'EWMARK/8LUME/AGBABIAN 1 PD R-SAN/LA/NY 1 BROOKHAVEN NAT LAB 1 G. ULR I KSON, OR N L 1 AGMFD (RUTH GUSSMA Rm B.127 GT 1 J. D, RUNKLES, Rm E-20
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nitat0TJJ P.O. BOX 013100 MIAMI,FLA. 33101 pjle cubi
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LaII gq-!I;1 FLOIIIDA POWEA 5 LIGHT COMPANY September 9,
1975 Office of Management Information, and Program Controls U. S. Nuclear Regulatory Commission Washington, DC 20555 Gentlemen:
Attached are the August, 1975 Operating Status Reports for Turkey Point Units Nos.
3 and 4.
Very truly yours, A.
. Schmidt Vice President Power Resources VTC/dd Attachments cc:
Mr. Norman C. Moseley Jack R.
- Newman, Esquire gdI ~tlat P
ggckel C44 SBBQ V
ENCLOSURE A DOCKET NO.
UNIT NAME TURKEY POINT DATE Se tember 5
1975 Kh%'LETED BY Mar lee Mont orner TELEPHONE NO.
305 245-2910 Ext.
228
'DAILY UNIT P01fER OUTPUT MiVK DAY AVERAGE DAILYMfe-net DAY AVERAGE DAILYMfe-net 2
3 4
7 9
10 13 15 16 18 19
'67 666 660 657 652'49 648 661 668 665 631 461 654 657 657 659 657 657 653 20 21 22 23 24 25 26 27 28 29 30 31 NOTE:
654 664-6 8
383 224'.45
'648
'651 650'aily average power level greater than 666 MWe, due to cooler condenser cool-water.
DOCKET NO.
UiMI'I'Ahfl..
~
DA'IT-'Pi~fPI,E'I'I',D BY TELEPI IPNE 50-250 TURKEY POINT IT No Se temb'er 1
30 245-2910 EXT.
228 REPORT MONTH AUGUST, 1975 OPERATING STATUS 2.
3.
REPORTING PERIOD' 1
75 08 01 THROUGH 2400 75 08 31 GROSS IIOURS IN REPPI<TING PL'RIOD:
744. 0 CURRENTLY AUTHORIZED POWER LEVEL (MWt) 2200 MAX. DEPEND.
CAPACITY (MWo NET) 666 POWER LEVEL'Tp 1CIICH RESTRICTED (IF ANY): (hfffe NET)
NONE REASONS FOR RESTRICTIONS (IF ANY):
5.
MNBER OF HOURS THE REACTOR WAS THIS hfPNIH
'R-Tp-DATE CUiiJLATIVE TO DATE CRITICAL o
~ ~ ~ ~
~ ~
~ ~
~
~
~
~ ~
~
~
~
~
~ ~
~ ~ ~ g, ~ ~ ~I'40. 9 5 577. 4
'9 605.2 6.
REACTOR RESERVE SITDOWN HOURS........ -'0- 7 ~
9.
HOURS GENERATOR OiN LINE...........'....
p UNIT. RESERVE SI UTDOWN HOURS.....;.....
GROSS THERhfAL ENERGY'GBKRATED(MWH)....
733.0 5 476.3 18 894. 6 85 0
10.
GROSS 'LECTRICAL EiiERGY GENEIQTED OM3).........................'.........
490 895 3 665 066 11 092 871 ll; NET ELECTRICAL ENERGY GENERATED (ii1$)..
466 603 3 509 475 10 490 640 12.
REACTOR AVAILABILITYFACTOR Ql 99 6
95.7 81.6 13.
, 14.
15.
UNIT AVAILABILITYFACTOR g2 UNIT CAPACITY FACTOR J3................
UNIT FORCED OUTAGE RATE J4 8
5 94.2
'1.5
- 93. 9 90.4 3.8 78.7
- 67. 0 4.1 16.
17.
SHUTDOWNS SCIIEDULED OVER NEXT 6 MONHIS (TYPE, DATE AND DURATION OF EACH):
Oct.: ?0 - Nov, 30,.1975 - Refueling, Maintenance and 1nspections.
IF SHUTDOWN AT END OF REPORT PERIOD, ESTIhfATED DATE OF STARTUP:
'I Jg REACTOR AVAILABILITY FACTOR '~5 ~&OR WAS CRITI~ X 100 GROSS HOURS IN REPOI<TIN PERIOD HOURS GENEIWfOR ON LINE X 100 J2 UNIT AVAILABILITYFACTOR =
GRpSS HOUI~ IN REppgT PEIupD J3 UNIT CAPACITY FACTPR NEf ELECTRICAI. POWER GENERATED X 100 MAX. Dl;PEiVDABI.E CAPACI'I'Y X GROSS HOURS IN REPOIQ'ERIOD 4
UNIT OUTAGE RA'IT:
FORCED OUTAGE I'IOURS X 140 IIOVIS GL'Nl!RKI'Pl< ON LINE +
FORCI!I) OIJI'AGE IIPVI6
Spg<g<Y:
Unit No.
3 operated at 1004 R.P. for entire month except for'oad reduction
.on august ll, 1975, to repai conden'ser tube leak and reactor.triPs on August 26, 1975.
~
g
~
DOCKET NO.
50-250 UNIT NAME TURKEY POINT UNXT NO ~
3 SEPTEMBER 5, 1975 PREPARED By MARYLEE MONTGOMERY.
TELEPHONE 05 2 5-Ext.
REPORT. MONTH AUGUST, 1975
U N I T S H U T D 0 N N S / R E D U C T I 0 N S NO.'.
DATE I'E F-FORCED
'-SCHEDULED DURATION HOURS)
REASON "'.
METHOD OF SHUTTING DOte GK REACTOR
- 'O&iENTS 25 75-08-,11 N/A'oad on Unxt No.
3 was reduced to repair condenser tube leak (Non-nuclear system) 26 75-08-. 26 27 75-08-26 3.2
.7. 8 A
'3 Reactor was tripped on No.
3C reactor coolant pump breaker open coincident with reactor power greater than 45% R.P.
caused by incipient failure of a, coil in. Unit No.
(Nuclear system)
Reactor was tripped on No.
3C reactor coolant pump breaker open coincident with reactor power greater than 45% R.P.
caused by the failure of a coil in Unit, No.
(Nuclear system)
REASON:
A-EQUIPMENl FAILURE ~EXPLAIN)
B-hfAINT. OR TEST C-REFUELING D REGULATORY RESTRICTION E-OPERATOR TRAINING AM)
LICENSE EXAMINATION F-AMINISTRATIVE G-OPERATIOM' ERROR H-05ER (EPLAQQ l ** h+THOD.
1-~iShiUAL 2-hKVJAL SCRAM
. 3-AUTCiQTIC SCRAhf
ENCLOSURE A DOCKET NO.
50-251 UNIT NAME TURKEY POINT UNIT NO.
4 SEPTEMBER 5, 1975 COMPLETED BY TELEPHONE NO.
MARYLEE MONTGOMERY 305 245-2910
'DAILY 'UNIT POWER OUTPUT AUGUST, 1975 DAY AVERACE DAILYMite-net
.. DAY AVEBA(Z DAILY M<e-net
~
3
~ 622 609 10 20 22 644 647 23.
653 652'47 10 267
" 644 692 642 598 26 27 28 29 30 "643 641 "640 643 638 644 646 649 647 642 NOTE:
~.
Daily average power level greater than 666 MWe, due to cooler condenser cool-water.
64
DOCKET NO. 50-251 UNIT N/WL:.
TURKEY POll UNIT NO.
I[ATE, 'EPTEMBER 5, 1975 (Q4fPI.Q'I'L'D'Y MARYLEE MONTGOMERY TELEPI IONE 305 245-2910 Ext.
228 ORT MONTH AUGUST, 1975 OPERAT I N G STATUS REPORTING PERIOD:
0001 75 08 01 TI.IROUGH 2400 GROSS JIOURS IN REPORTING PEI110D:
2.
CURRENTLY AVEORIZED POWER LEVEL (Mft) 2200 MAX. DEPEND.
CAPACITY (Mfe NET) '66 3.
PPNER LEVEL Tp lNICH RESTRICTED (IF ANY): (Mlle NET) 4.
REASONS FOR RESTRICTIOiNS (IF ANY):
75 08 31 None 5.
NUMBER OF HOURS IHE REACTOR WAS THIS MOTS YR-Tp-DATE CUiV3LATIVE Tp DATE CRITICAL
~ o ~
~
~ ~ ~ '
~ ~
~
~ ~
~ ~
~
~
~
~
~
~ ~
~
~ ~
~
~ ~ ~ ~
0 0 ~
6.
REACTOR RESERVE SHIJI'JNNN HOURS........ 3 663.2 12 997.1 7.
JlPURS GENERATOR ON LINE.. ~... ~........
590 4
3 561.7 12 619. 5 8.'.'NIT RESERVE SFIUTDONN HOURS............ 9.
GROSS TFIERii9Q. ENERGY GENEIQTED{MIQ)....
1 282 ill 7 '550 826 25 903 036 10.
12.
13.
14.
GROSS'LECTRICAL ENERGY GENERATED (MIfFI) ~
~
~
~
~
~
~
~
~
~
~
~
~
~
~ o
~
~
~ ~
~ ~ ~
~
~
~ ~ ~ ~ ~
~
~
~
~
NET ELECTRICAL ENERGY GENERATED (MS)..
REACTOR AVAILABILITYFACTOR Ql UNIT AVAILABILITYFACTOR +2............
I UNIT CAPACITY FACTOR g3,.............;.
- 80. 7
- 79. 3
- 75. 9
- 62. 8
- 61. 1
- 58. 6 396 710 2 403 336 376 310 2 277 006 8 177 597 7 746 062
- 74. 8 72.6 68.2 15.
16.
UNIT FORCED OUTAGE RATE J4 SHIJIDO1'SS SCHEDULED OVER NEXT 6 MpiVHIS (TYPE, DATE AND 0.2 DURATION OF EACII):
4.0 Sept.
13-19, 1975 Scheduled 'Maintenance 17.
IF SFIUTDONN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP:
J$
REACTOR AVAILABILITYIACTpR HOWS ~&OR WAS CRITI~ X 100 GROSS HOURS IN REPOIG'IN PERIOD HOURS GENERATOR ON LINE X 100 2
UNIT AVAI~ILITYFA~R =
GRpSS FIOUI& IN REpplg'I"PEIgpD UNIT CAPACITY FAVOR = NET El'I!CTRICAI'OWER GENERATED X 100 IIAX. DliVL'NDABLECAVACI'IY X GROSS IIOURS IN REPORT PERIOD 4
UNIT OUTAGE RATE = FOR ED OUTAGI! IIOURS X 100 JIOVRS Gl.'.Nf!IKlQR PN I.INL' FORCED OU'I'AGE I IOURS
SQ&f'EY: Unit No..
4 operated at 100%
R.P. except for scheduled maintenance shutdown August 8-9, 1975 and a load reduction on August 12, 1975 DOCKET NO; 50-251
~
PilIT k01E TURKEY POINT UNIT NO.
4 SEPTEIMER 5, 1975 PREPARED BY MARYLEE MONTGOMERY TELEPHONE 30 245-2910 Ext.
8 REPORT M3iVHH AUGUST, 1975 U N I T S H U T D 0 N N S / R E D U C T I 0 N S iXO..
DATE
'I PE F-FORCED
'-SCHEDULED DURATION (HOURS)
REASON "
ME'IHOD OF SHtJITING DOWN
%HE REACIOR **
COUNTS 11 75-08-03 153.7 Unit No.
4 was removed from service. (controlled manual shutdown) to repair No." 4B steam generator tube leak (small leak in one of 3,260 tube).
There were no significant quantities of radio-active material released as a result of this small leak.
(Nuclear system) 12 75-08-12 N/A Load on Unit No.
4 was'utomatically reduced to approximately 70% R.P. by No.
4 reactor protection system caused by loss of power supply to control rod drive mechanism H-4.
(Nuclear system)
REASON i
A"EQJIPMENT FAILURE (EXPLAIN B-MAINT. OR TEST C-REFUELING D-REGULATORY RESTRICTION E-OPERATOR TRAINING AND LICENSE EXAMINATION i
- F"ADMINISTRATIVE G-OPERATION'2 ERROR H-GIBER (EXPLAIN)
! ** MEIHOD:
1-14MAL
~,'-NA'UALSCRAM 3-AUTOMATIC SCRAM
4