ML18152A449

From kanterella
Jump to navigation Jump to search
Insp Repts 50-280/93-12 & 50-281/93-12 on 930503-07. Violations Noted.Major Areas Inspected:Design Changes & Mods & Engineering Support Activities
ML18152A449
Person / Time
Site: Surry  Dominion icon.png
Issue date: 06/04/1993
From: Branch M, Matt Thomas
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A450 List:
References
50-280-93-12, 50-281-93-12, NUDOCS 9306160176
Download: ML18152A449 (14)


See also: IR 05000280/1993012

Text

Report Nos.:

Licensee:

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

50-280/93-12 and 50-281/93-12

Virginia Electric And Power Company

Glen Allen, VA 23060

Docket Nos.:

50-280 and 50-281

Facility Name:

Surry 1 and 2

Inspection Conducted:

May 3-7, 1993

License Nos.: DPR-32 and DRP-37

Inspector: mt~ ~

M. Thomas

Accompanying Inspectors: H. Whitener

M. Miller

Approved by:

C -~~J~,,.

k_

M.Bran~ ~

Test Programs Section

Engineering Branch

Division of Reactor Safety

SUMMARY

Scope:

,-~-7~

Date Signed

c/lf/93

Date Signed

This routine, announced inspection was conducted in the areas of design

changes and modifications and engineering support activities.

Results:

In the areas inspected one violation and one inspectorfollowup item {IFI)

were identified.

Violation 50-280,281/93-12-0l, for failure to follow procedures in

updating design drawings within the required time period following

the implementation of two design change packages {DCP) {paragraph

3).

IFI 50-280,281/93-12-02, Labeling of test valves installed in the

emergency diesel generator air start system {paragraph 2.b.) *

9306160176 6gggg~80

~DR

ADOCK

PDR

2

The various engineering groups worked well together to resolve

complex problems that could potentially affect plant operations.

Timely and effective engineering support was provided to resolve

the pressurizer safety relief valve issue.

Engineering has provided timely support in resolving deviation*

reports (DRs) and requests for engineering assistance (REA).

A weakness was noted in the documentation of the 10 CFR 50.59

safety evaluation for DCP 92-49 (paragraph 2.b.).

The licensee's program for reducing the DCP and engineering work

request (EWR) modification backlog provided adequate justification

for cancelling the DCPs reviewed.

The licensee's self assessment efforts continue to demonstrate the

licensee's commitment to improving the quality and effectiveness

of engineering support provided to the plant .

..

1.

Persons Contacted

Licensee Employees

REPORT DETAILS

  • W. Benthall, Manager, Nuclear Licensing
  • R. Bilyeu, Licensing Engineer

D. Blake, Design Engineer, Station Engineering

  • R. Blount, Superintendent, Station Engineering
  • A. Fletcher, Assistant Superintendent, Station Engineering
  • B. Foster, Mechanical Engineering Supervisor, Station Engineering

R. Green, Systems Engineering Supervisor, Station Engineering

  • D. Hart, Supervisor, Quality Assurance
  • M. Kansler, Station Manager
  • R. MacManus, Systems Engineering Supervisor, Station Engineering
  • J. Price, Assistant Station Manager, Nuclear Safety and Licensing
  • R. Saunders, Assistant Vice President Nuclear Operations
  • J. Swientoniewski, Supervisor, Station Nuclear Safety

E. Watts, Electrical Engineering Supervisor, Station Engineering

Other licensee employees contacted during this inspection included

engineers, operators, craftsmen, and administrative personnel.

NRC Resident Inspectors

J. York, Senior Resident Inspector

  • S. Tingen, Resident Inspector
  • Attended exit meeting

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

2.

Design Changes and Plant Modifications (37700)

a.

Plant Modifications to Improve Reactor Safety

The inspectors reviewed the initiatives taken by the licensee to

identify and implement plant modifications to improve reactor

safety. This included reviewing the licensee's efforts to reduce

the backlog of DCPs and EWRs.

The licensee implemented a Level I Project Modification Package

Backlog Reduction program designed to reduce the EWRs and DCPs

from 333 in August 1992 to 150 by June 1993.

The inspectors

reviewed trend reports and monthly status reports and determined

that the EWR/DCP reduction was on schedule as of April 1993 with

172 packages remaining in the backlog population.

The packages in

the backlog population were in various stages of completion.

In

some cases the engineering design work, modification

implementation, and technical review were complete and final

closeout awaited only sign off of the documentation.

At the other

..

2

extreme, some DCP numbers were assigned, but were not funded and

no engineering work had been performed.

Closeout methods varied

from closure with the completion of documentation, closure with

partial implementation, closure with no implementation, closure by

cancellation, and closure of assigned numbers which were not

approved for funding.

This process was consistent with the VEPCO

General Nuclear Standard (STD-GN-0001, Revision 10) which provided

interim instructions for changes in the design control process.

Subsequent to September 16, 1991, all plant modifications (major

and minor) are to be performed using the DCP process and EWRs are

to be used for engineering technical evaluations.

DCPs and EWRs

initiated prior to this date may be completed in the old format,

canceled, or converted to the new DCP format as appropriate.

STD-

GN-0001, Revision 11 and VPAP 0301, Revision 1, Design Change

Process, specify that cancellation of EWRs/DCPs will be

accomplished through a field change (FC) which identifies the

reason for cancellation and if there was any 'impact on systems or

projects resulting from not implementing the design change.

A sample of FCs for canceled EWRs/DCPs was reviewed to evaluate

any impact on system reliability and safe operation of the plant.

FCs reviewed and evaluated included the following:

DCP 90-013-1, Revision 8 - 2/20/92

This was a corporate issued DCP specifying replacement of

the motor operators for six valves.

Replacement was

completed for two valves, two valves did not require

replacement, and two valves required maintenance.

Subsequent to the operational readiness review, the DCP was

canceled for the four valves not requiring operator

replacement.

While cancellation was justified, the FC was weak in that

the reason for not replacing the operators on four of the

six valves had to be determined from other sources.

EWR 89-467, Revision A - 9/25/92

This EWR was an evaluation to perform a commercial grade

dedication for replacement relief valves in the component

cooling water system in order to upgrade the valves to

safety related status. Based on the current design change

standards, EWRs are not the proper vehicle for performing

commercial grade dedication of equipment.

The EWR was

canceled and the new valves will be procured and qualified

under the Virginia Power Safety Related Dedication

Procedures and Standards program.

The FC provided adequate justification for the cancellation .

3

EWR 88-012, Revision J - 9/11/92

This EWR provided instructions for replacing existing

auxiliary feedwater system check valves. According to a

systems engineering evaluation, replacement was not

necessary.

The existing valves were performing

satisfactorily.

Due to valve performance, cancellation was considered

justified. Should valve replacement be necessary in the

future, it would be addressed under the current design

change standard with a DCP.

EWR 89-730, Revision B - 8/31/92

This EWR was issued for engineering authorization to replace

a leaking one inch Pacific gate valve (no longer available}

with a one inch Velan gate valve. Discussions with System

Engineering indicated that in a recent leak rate test the

Pacific valve was not leaking.

The licensee concluded that

it was not necessary to replace the Pacific valve.

Cancellation of this EWR was considered justified based on

valve performance .

DCP 92-48-1

Engineering reviewed a request for engineering assistance

(REA} to develop a DCP to install new ventilation flow

elements. Although the new elements were slightly different

from the original elements, the differences were minor and

considered within the scope of the Item Equivalency Program.

Procurement Engineering performed an evaluation to address

the differences.

The new elements are to be installed by

work orders 123458 and 123459.

Design Engineering will

assist by providing a package of electrical wiring diagrams,

equipment support drawings, and the general installation

sequence identifying special implementation requirements.

Cancellation of the DCP was considered justified in that the

flow elements will be installed under an approved, standing

program.

DCP 90-16-1, Revision 6 - 11/19/92

This DCP was issued to modify the reactor cavity seal.

Prior to performing this modification a walkdown revealed

dimensional discrepancies between the actual cavity seal

area and the new seal design. Therefore, the DCP was not

implemented.

Instead, the original method of cavity seal

was accomplished via EWR 90-328. This method is performing

~*

4

satisfactorily. Consequently, DCP 90-16-1, which would

require major redesign, will not be implemented.

In that the current cavity seal method is performing

satisfactorily, cancellation of the redesigned seal is

considered justified.

EWR 90-158, Revision A - 10/20/92

This EWR was issued to relocate an electrical receptacle

located near a battery in the emergency service water pump

house to reduce an explosion hazard.

An engineering

walkdown prior to implementation found that the receptacle

had been removed, the wires taped and the opening capped.

In that there were sufficient receptacles in the pump house,

this specific receptacle was eliminated rather that

relocated. Cancellation of the EWR was considered

justified.

EWR 90-237, Revision A - 9/4/92

This EWR was issued in response to valve thermal

binding/bonnet pressurization problems identified in INPO

Significant Operating Experience Report 84-07.

Engineering

reviewed all air operated {AOV) and motor operated {MOV)

safety related gate valves for Surry Units 1 and 2 and

issued a Type 1 Report on the investigattve methods and

findings.

The review consisted of an initial screening to

identify the AOVs and MOVs susceptible to the thermal

binding/bonnet pressurization phenomena.

A detailed

analysis was performed on valves identified by the screening

process.

The licensee concluded that none of the valves

have a significant possibility of experiencing thermal

binding/bonnet pressurization leaking.

In response to the Operating Experience Review Group

concerns, engineering developed calculations showing that,

for the MOVs of concern, the motor operators have the

capacity to open the valves against the binding forces.

Based on the valve operation histories, the analysis of

operating conditions, and force calculations, cancellation

of this DCP was considered justified.

Review of the above sample of FCs issued to cancel EWRs/DCPs

indicated that safe operation of the plant or reliability of

systems has not been compromised.

Based on discussions with

licensee engineering personnel, and review of the above

documentation, the inspectors concluded that the licensee has a

..

b.

5

satisfactory process for identifying and implementing plant design

changes to improve reactor safety and to reduce the EWR/DCP

backlog.

Planning, Development and Implementation of Plant Modifications

The inspectors reviewed the DCPs listed below to: (1) determin~

the adequacy of the 10 CFR 50.59 safety evaluations performed; (2)

verify that the DCPs were reviewed and approved in accordance with

TS and applicable administrative controls; (3) verify the subject

modifications were installed (for those that could be physically

inspected) in accordance with the DCP package; (4) verify that

applicable plant operating and design documents (drawings, plant

procedures, FSAR, TS, etc.) were revised to reflect the subject

modifications; (5) verify that the modifications were reviewed and

incorporated into the operations training program as applicable;

and (6) verify that post modification test requirements were

specified and that adequate testing was performed.

The following

DCPs were reviewed:

DCP 88-32, Addition of Diesel Generator Sequencing, Unit 2

This modification was initially dated December 11, 1988, to

add an emergency diesel generator (EDG) load sequencing

scheme that would be initiated by a loss of offsite power

(LOOP).

The purpose of this scheme was to ensure that the

maximum EDG load capabilities would not be exceeded under

the worst case load applications, and therefore resolve NRC

concerns described in IE Information Notice 85-91.

The

second part of this DCP was dated February 26, 1991, to

modify the control circuits for the auxiliary feedwater

pumps.

The control circuits were modified by eliminating

the latching relays and replacing them with auxiliary type

relays. Four auxiliary relays were added to control

circuits.

This DCP included both the engineering design change

packages and the installation work plans.

The inspectors

conducted a detailed walkdown inspection to verify that

components were installed and the drawings reflected the as-

built plant condition.

The inspectors determined that this

modification was implemented in a satisfactory manner.

DCP 91-12, RSHX Service Water Flow Element Modifications,

Units 1 and 2

This DCP was implemented to replace existing pitot venturi

flow elements (l-SW-FE-105A and -105B, 2-SW-FE-205A and

-205B) that monitor SW flow in the supply headers to the

RSHXs; and venturi flow elements (l-SW-FE-106A,B,C,D, 2-SW-

FE-206A,B,C,D) that monitor SW outlet flow from each of the

6

RSHXs, with V-Cone flo~ elements.

The V-Cone flow element

provided stable and accurate flow indication during the RSHX

flow test that was performed on April 6, 1991.

The inspectors reviewed the DCP in accordance with the

criteria specified above and performed a field inspection to

verify that the components were installed and the applicable

drawings reflected the as-built plant configuration. The

inspectors determined that this DCP was satisfactorily

implemented.

DCP 92-49, Removal of Motor Operators From Ol/02-RH-MOV-

100/200

This modification required the removal of motor operators

from the RHR containment isolation valves 01-RH-MOV-100 and

02-RH-MOV-200.

In the DCP's "Statement of the Problem", the

reasons for the removal of these valves' motor operators

were the initial installation had an improper design, there

were significant difficulties with proper operation, and the

valves repeatedly failed the "Type C" leak testing. These

problems were caused by the design configuration originated

for the initial installation of the motor operators by DCP 74-001 performed in 1975.

The previous manual valves had

motor operators remotely installed above them using a long

drive shaft. Since this arrangement was not effective the

motors were later disconnected and the valves were manually

operated.

The purpose of DCP 74-001 was to install an overflow line

from the RWST to the safeguards valve pit to prevent the

uncontrolled release of radioactive water.

The basis for

this modification was that pumps were installed in the pit

to pump the water to the liquid waste system.

The motor

operators were installed on the valves to automatically

close upon a high level alarm on the RWST to prevent over

filling.

(The valves are in the lines feeding the RWST and

are only used during refueling.)

In 1984 another modification was performed in this area.

EWR 84-089 was initiated to prevent the release of

unmonitored gaseous effluents from the RWST.

This

modification required the capping of the vent on top of the

RWST and extended .the overflow line down further in the

valve pit.

EWR 84-089 discussed the basis of DCP 74-001

where the manual valves had motor operators installed to

provide the automatic shutoff to prevent RWST overfill.

During the review of this modification the inspectors

determine that the licensee's basis for removing the motor

operators was acceptable: However, several concerns were

identified during the review of the safety evaluation for

..

7

the removal of the motor operators which indicated an

inattention to details. The licensee's safety evaluation

form required a response and an explanation for each

question.

The explanation provided as justification for

several of the questions was that the RWST overflow

occurrence had been previously analyzed in DCP 74-001 and

EWR 84-089.

The inspectors determined that DCP 74-001 and

EWR 84-089 analyses clearly stated that the valves had motor

operators added to provide automatic shutoff to prevent the

RWST from being overfilled. Therefore, using the analyses

from DCP 74-001 and EWR 84~089 for removing the motor

operators was inappropriate.

In the "Programs Review

Checklist

II the question for ALARA, asks if the work in the

DCP affects systems, facilities, and/or equipment which

process or contain radioactive materials, fluids or gases?

The answer checked was no.

The purpose of the earlier

modifications, DCP 74-001 and EWR 84-089, was to control the

release of radioactive effluents. The inspectors identified

these responses in the safety evaluation as concerns that

appeared to be due to inattention to details.

The inspectors concluded that the licensee's basis for

removing the motor operators was justified and there was no

safety concern.

However, the responses to several of.the

questions indicated an inattention to detail .

DCP 92-72, EG Check Valve Testing Modification, Units I

and 2

This DCP was implemented to install a test valve in each EDG

air start system between the compressor and the safety-

related air receiver check valve, in order to test for back

leakage by the check valve.

Leak testing of the check valve

is performed to meet an ASME Section XI Inservice Testing

commitment.

The inspectors reviewed this DCP to the criteria specified

above and performed a field inspection to verify proper

installation. During the field inspection, the inspectors

noted that the drawings had been updated to reflect the

modification, but only one of the six test valves installed

by this DCP was labeled. The inspectors discussed this

discrepancy with licensee personnel who indicated that the

valves were being labeled as part of the licensee's upgraded

labeling program, which was still ongoing.

The licensee

further indicated, and the inspectors verified, that the

valves were only for test purposes and performed no safety

function.

The inspectors will verify labeling of the test

valves during a future inspection. This item will be

identified as IFI 50-280, 281/93-12-02, Labeling of test

valves in emergency diesel generator air start system .

C

3.

8

The inspectors noted that, except for the discrepancies discussed

above, the DCPs were satisfactorily implemented.

None of the

discrepancies noted had a safety impact. Violations or deviations

were not identified in the areas inspected.

Drawing Control

The inspectors reviewed the licensee's program and procedures that were

developed and implemented to maintain configuration control of the

applicable drawings after DCP implementation.

The program was examined

to ensure that design control was maintained and that the drawings

affected by DCPs were updated in a timely manner to reflect the as-built

plant. The procedures reviewed for the configuration drawing control

program included the following documents:

VPAP-0301, Virginia Power Administrative Procedure, Design Change

Process

SUADM-ADM-11, Surry Power Station Administrative Procedure,

Station Drawing Revision and Distribution

VPAP-0301 was the detailed procedure that established the process for

managing the preparation and implementation of design changes.

It also

established interfaces among the various organizations and defined the

controls necessary to assure safe implementation of station design

changes.

In addition, the VPAP discusses the requirements for updating

the design drawings in accordance with SUADM-ADM-11.

The purpose of

SUADM-ADM-11 was to prescribe the method for revision of controlled

drawings, for annotation of drawings to reflect design changes in

progress, and to provide guidelines for proper distribution and

maintenance of station controlled drawings.

The inspectors selected

drawings from completed DCPs to determine if the drawings were updated

in a timely manner as required by the licensee's procedures.

In

addition, the drawings in the Control Room were examined to ensure that

they were also updated.

The drawings for the following DCPs were

examined:

DCP 93-20, EPH 34.5 KV BUS NO. 5

DCP 92-64, CHARGING PUMP LOGIC

DCP 89-09, POWER SUPPLY-ATWS MIGITATION SYSTEM

DCP 87-26, ATWS MITIGATION SYSTEM

DCP 88-32, ADDITION OF DIESEL GENERATOR SEQUENCING

DCP 92-63, LP HEATER DRAIN PUMP RECIRCULATION LINE

DCP 91-12, RSHX SERVICE WATER FLOW ELEMENT MODIFICATIONS

DCP 92-72, EG CHECK VALVE TESTING MODIFICATIONS

..

9

During the drawing review, the inspectors identified on May 6, 1993,

that the priority drawings for DCP 93-20 and DCP 92-64, which required

revision within 15 days of the operational readiness review (ORR)

completion date, were not completed.

The ORR completion date for DCP

93-20 was April 8, 1993, and the drawing not updated was 11448-FE-lA.

The ORR completion date for DCP 92-64 was April 9, 1993 and the drawings

not updated were 11548-ESK-SP, -SQ, -SR, and -5S.

The licensee's

failure to update these 15-day priority drawings as required by SUADM-

ADM-11 is identified as Violation 50-280, 281/93-12-01, Priority

Drawings Not Updated.

The licensee took immediate corrective action by

issuing deviation reports for DCP 92-64 and DCP 93-20, identifying the

discrepancies and requiring that the drawings be updated.

Both DRs were

dated May 6, 1993.

The inspectors verified that the licensee updated

the overdue drawings on May 6, 1993.

One violation was identified in the areas inspected.

4.

Engineering and Technical Support Activities

The inspectors reviewed activities performed by Station Engineering in

an effort to assess the effectiveness of the support being provided to

the plant operations and maintenance staffs for day-to-day activities.

These activities included responding to DRs, REAs, Systems Engineering

activities, and self assessments .

The inspectors concluded that the various engineering groups worked well

together to resolve complex problems and, in general, provided timely

and effective engineering support to the plant.

a.

Deviation Reports and REAs

The inspectors reviewed Engineering's involvement in resolving

DRs, which included reviewing DR trend reports over the last year.

The inspectors noted that from January 1992 to May 1993, a total

of 654 DRs were assigned to Station Engineering (458 DRs for 1992

and 196 DRs for 1993).

Engineering was only overdue in responding

to 16 of the DRs (exceeding 30 days) in 1992.

There have been no

late DR responses for 1993. There were 13 DRs currently open for

1993 and there were no open 1992 DRs.

The inspectors also reviewed Engineering's involvement in

resolving REAs.

Since June 1992, 390 REAs were received by

Engineering.

A total of 338 REAs have been closed by Engineering,

11 REAs have been reviewed by Engineering and were awaiting review

by the MMRT, and 41 REAs were under review by Engineering.*

The inspectors concluded that Station Engineering provided timely

responses for assigned DRs and REAs .

b.

10

Systems Engineering

The licensee's engineering organization is diversified in

specialty areas including corporate, maintenance, design, system,

material, modification implementation, and testing. The

inspectors reviewed engineering activities to ascertain

involvement in plant operations and maintenance.

The Surry Station Engineering Services (SSES) 3.01, Revision 2,

Controlling Procedure for System Engineering, identifies

Maintenance Engineering (ME) as the component engineering experts

and describes the System Engineer (SE) as the system expert

responsible for system management and oversight. Duties included

ensuring system performance per design basis; maintaining

cognizance of system conditions; coordinating diverse group

efforts to resolve problems; and serving as the expert for system

design, regulatory, testing and operational questions.

In this

regard the SE writes and reviews procedures, performs system

tests, reviews test results and trends system performance.

Additionally, the SE reviews all work orders on assigned systems

prior to work.

When multiple work orders are involved the SE

generates a post maintenance testing (PMT) package which details

the sequence of testing, a flow chart, procedures, and procedure

changes to accomplish a meaningful PMT.

This package is

distributed to operations, management, maintenance and engineering

for review and comment.

The inspectors reviewed DRs and REAs and determined that

engineering's response in support of plant operations and

maintenance was adequate and prompt.

The inspectors also reviewed

portions of the Station Engineering Weekly Events Reports for

February 1993 - May 1993 and the System Engineering Quarterly

Report for the fourth quarter of 1992.

These reports present the

historical problems of the system, the problems experienced during

the report quarter, actions taken to resolve problems and

recommendations to upgrade and enhance system reliability. The

quarterly report also trends system parameters.

The. inspectors

reviewed portions of these reports for the EDG and instrument air

systems and concluded that engineering was responsive in

identifying and resolving problems.

The inspectors also followed a real time event which occurred

during this inspection. During startup, the pressurizer code

safety valves were simmering.

The licensee obtained a waiver of

compliance to permit gagging the relief valves and performing the

system hydrostatic test. Subsequently, system pressure was

reduced to about 1900 psig to allow the code valves to seat and

stabilize. System pressure was then brought up to 2135 psig,

where the plant will be operated. This is 100 ps~ below normal

operating pressure and required NRC approval and an emergency TS

change.

.

' .

c.

11

Engineering was active in obtaining approval for operation at

reduced pressure. Corporate engineering performed calculations to

show adequate departure from nucleate boiling safety margin,

design engineering walked down the system and developed alternate

plans of action in case leakage did not stop at reduced pressure,

System Engineering was involved in obtaining the waiver of

compliance for the hydrostatic test and Maintenance Engineering

was involved in details of gagging the valves and communicating

with the vendor, and a management oversight committee followed the

events closely. The inspectors considered this a good example of

engineering groups working together to support the plant.

Based on review of records and observations of the licensee's

response to the above event the inspectors concluded that

engineering activity supports plant operations and maintenance.

Self Assessment

The inspectors reviewed certain aspects of the licensee's self

assessment program.

One assessment reviewed was the appraisal of

the engineering programs.

The licensee developed a rating system

and performed a survey of 24 engineering programs to evaluate the

programs' effectiveness. A score of 5 indicates average program

effectiveness.

The survey results showed that four of the

programs (Appendix R, Setpoint Coordination, TS Compliance

Coordination, and Computer Software Control) were rated as average

to less than average. Corrective action plans were developed and

entered in the licensee's commitment tracking system to enhance

and improve the programs.

The inspectors reviewed the action

plans for three of the programs.

The inspectors also reviewed selected QA audits of engineering

activities. Audits reviewed included activities such as the

vendor information program, drawing update, and configuration

control.

The audits were detailed and identified areas of

weakness and strength.

The inspectors determined that the licensee's self assessment

efforts continue to demonstrate the licensee's commitment to

improving the quality and effectiveness of engineering support

provided to the plant.

Violations or deviations were not identified in the areas inspected .

-

.

'

5.

12

Exit Interview

The inspection scope and results were summarized on May 7, 1993, with

those persons indicated in paragraph 1.

The inspectors described the

areas inspected and discussed in detail the inspection results listed

below.

Proprietary information is not contained in this report.

Dissenting comments were not received from the licensee.

The following

findings were discussed:

Violation 50-280, 281/93-12-01, Failure to follow procedures in

updating design drawings within the required time period.

(paragraph 3)

IFI 50-280, 281/93-12-02, Labeling of test valves installed in the

emergency diesel generator air start system. (paragraph 2.b.)

6.

Acronyms and Initialisms

ALARA

ADV

ASME

ATWS

DCP

DR

EOG

EWR

FC

FSAR

IFI

INPO

kV

LOOP

LP

MDV

NRC

ORR

psi

psig

QA

REA

RH

RHR

RSHX

RWST

SW

TS

As Low As Reasonably Achievable

Air Operated Valve

American Society of Mechanical Engineers

Anticipated Transient Without Scram

Design Change Package

Deficiency Report

Emergency Diesel Generator

Engineering Work Request

Field Change

Final Safety Analysis Report

Inspector Followup Item

Institute of Nuclear Power Operations

Kilovolts

Loss Of Offsite Power

Low Pressure

Motor Operated Valve

Nuclear Regulatory Commission

Operational Readiness Review

Pounds Per Square Inch

Pounds Per Square Inch Gauge

Quality Assurance

Request for Engineering Assistance

Residual Heat

Residual Heat Removal System

Recirculation Spray Heat Exchanger

Refueling Water Storage Tank

Service Water

Technical Specification