ML18150A224

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Forwards Notice of Violation from Insp Repts 50-280/87-07 & 50-281/87-07 on 870504-08 & as Discussed at 870519 Enforcement Conference.Civil Penalty Will Not Be Proposed Because of Util Prompt & Extensive Corrective Actions
ML18150A224
Person / Time
Site: Surry  
Issue date: 07/15/1987
From: Grace J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To: Stewart W
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
Shared Package
ML18150A226 List:
References
EA-87-078, EA-87-78, NUDOCS 8707220398
Download: ML18150A224 (3)


See also: IR 05000280/1987007

Text

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Docket Nos. 50-280, 50-281

License Nos. DPR-32, DPR-37

EA 87-78

JUL 1 5 1987

Virginia Electric and Power Company

VATTN:

Mr. W. L. Stewart, Vice President,

Nuclear Operations

P. 0. Box 26666

Richmond, VA

23261

Gentlemen:

SUBJECT:

NOTICE OF VIOLATION (NRC INSPECTION REPORT NOS. 50-280/87-07

AND 50-281/87-07)

This refers to the Nuclear Regulatory Commission (NRC) inspection conducted

on May 4 - 8, 1987 at the Surry Nuclear Station.

During this inspection, a

failure to ~amply with NRC regulatory requirements, which was identified by the

licensee, was reviewed.

The report documenting this inspection was sent to you

with a letter dated June 17., 1987.

The NRC concerns relative to this finding

were discussed between Mr. M. Ernst, Deputy Regional Administrator, and other

members of the Region II staff and you and other members of your staff in an

Enforcement Conference held on May 19, 1987.

The report documenting this con-

ference was sent to you by a letter dated June 9, 1987.

The violation described in the enclosed Notice of Violation involved a failure

to meet the requirements of 10 CFR Part 50, Appendix R, with respect to the

independence of cabling associated with alternative safe shutdown equipment.

A

review by your staff revealed that cabling for Diesel Generators numbers 1 and

3, which are required as power sources for the Unit 1 alternative safe shutdown

requirement, were not independent of the specified design basis fire area.

This cabling, as well as cabling for the Unit 2 safe shutdown equipment, was

routed through the Unit 2 Cable Vault and Tunnel which is a design basis fire

area.

A fire in this area could result in the loss of reactor coolant makeup

capability for for both units if offsite.power is not available. This improper

cable routing was the result of an inadequate review for Design Change Package 83-39A.

In accordance with the

11General Statement of Policy and Procedure for NRC

Enforcement Actions,

11 10 CFR Part 2, Appendix C (1987), the violation described

in the enclosed Notice has been classified at a Severity Level III. A civil

penalty is considered for a Severity Level III violation.

However, after

consultation with the Director, Office of Enforcement and the Deputy Executive

Director for Regional Operations, I have decided that a civil penalty will not

be proposed in this case because of your unusually prompt and extensive correc-

tive action to address the problem and prevent recurrence, and your prior good

performance in the area of fire protection, 'and your prompt reporting of the

problem to the NRC.

The good prior performance is illustrated by the category 1

rating in fire protection during the last Systematic Assessment of Licensee Per-

formance which covered the period of March 1, 1985, through August 31, 1986.

8707220398 870715

PDR

ADOCK 05000280

G

PDR

Virginia Electric and Power Company

- 2 -

JUL 1 5 1987

You are required to respond to this letter and should follow the instructions

specified in the enclosed Notice when preparing your response.

In your response

you should document the specific actions taken and any additional actions you

plan to prevent recurrence. It is noted that, in your updated Licensee Event

Report 'No. LER 87-010-01 dated June 11, 1987, you have already addressed some

of these items.

Therefore, in your response you may reference that submittal

where appropriate.

After reviewing your response to this Notice, iricluding your

proposed corrective actions and the results of future inspections, the NRC will

determine whether further NRC enforcement action is necessary to ensure compli-

ance with NRC regulatory requirements.

In accordance with Section 2.790 *of the NRC's "Rule of Practice,

11 Part 2,

Title 10, Code of Federal Regulations, a copy of this letter and its enclosure

will be placed in the NRC Public Document Room.

The responses directed by this letter and its enclosure are not subject to the

clearance procedures of the Office of Management and Budget as required by the

Paperwork Reduction Act of 1980, PL 96-511.

Should you have any questions concerning this letter, please contact us.

Enclosure:

Notice of Violation

cc w/encl:

~- F. Saunders, Station Manager

  • JY.' E. Clark, Manager - Nuclear

Programs and Licensing

Sincerely,

Original signed by

J. Nelson Grace

J. Nelson Grace

Regional Administrator

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