05000281/LER-1980-004-01, /01T:on 800521,during Cold Shutdown,Pressure Transmitter 458 Inoperable Due to Wiring Problem & Isolation Valve for Pressure Transmitter 403 Found Closed,Negating Overpressure Mitigating Sys.Caused by Cable Problem

From kanterella
(Redirected from ML18139A298)
Jump to navigation Jump to search
/01T:on 800521,during Cold Shutdown,Pressure Transmitter 458 Inoperable Due to Wiring Problem & Isolation Valve for Pressure Transmitter 403 Found Closed,Negating Overpressure Mitigating Sys.Caused by Cable Problem
ML18139A298
Person / Time
Site: Surry 
Issue date: 06/04/1980
From: Joshua Wilson
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML18139A297 List:
References
LER-80-004-01T-01, LER-80-4-1T-1, NUDOCS 8006110265
Download: ML18139A298 (2)


LER-1980-004, /01T:on 800521,during Cold Shutdown,Pressure Transmitter 458 Inoperable Due to Wiring Problem & Isolation Valve for Pressure Transmitter 403 Found Closed,Negating Overpressure Mitigating Sys.Caused by Cable Problem
Event date:
Report date:
2811980004R01 - NRC Website

text

'

e NR: rCA1-:1 36~

ri-i7 l U.S. "UC!..E~R REGULATORY C0Ml".-!!S.S10~._

LICENSEE EVENT REPORT EXHIBIT A Cul';TROL SLOCK IQ.

(PLEASE PRINT OR TYPE ALL REQUIRED INFDP.MATIONl [IT] I V ! A!

S! P I S I 2 JG)! 0 ! 0 E

S LICENSEE COO::

14 15 I-I o I ol o I o ! ol-Io I olG)I 4 I 111 111 1101 I IQ LICENSE: NUMBER

.2~

2i, LICC:NSE. TYPE

JO 57 C.:..T 5S cor,,

~

~~~~ W81 o 1 5 1 o Io Io I 21 811 )01 o 1 5 1 2 I 1! 8 I o GI o I 6 10 I 4 I 8 lo 10 c

6",

i~,ccr NUMSER 6S e=

EVENT DATE 1.:

7:,

REPORT OAT~

80 EVErl:T DESCRIPTIOr-.: AND PROBABLE CONSEQUENCES@)

I Buririg cold shutdown, with the RCS in a solid condition.PT 458 was i naperab j e' due to a wiring problem.

Subsequently, the isolation valve for PT 403 was

~

found closed.

This condition negated the Overpressure Mitigating System

~

I by eliminating the two pressure inputs ot the PORV's.

This event is IT))]

contrary to T.S. 3.1.G,.l(b) and reportable Per T.S. 6.6.2.a(2....,__,, ______ ___,

[B2]

  • CITD 7

B 9 SYSTEM CODE I SIR I@

9 10

~

LERIRO CVENT YEAR

'0 ~EPO~T I 8 I O I NUMB_R

2l 22 CAL.:SE

CAUSE

CO::>E SUBCOOE COMPONH/T CODE bLl@ w@, r, N, s, Tl R, u,e 11 12 1:!

SEQUENTIAL REPORT NO Io Io I 4/

16 OCCURRENCE CODE 1.......-1 Io I 11 23 2*

25 2 l 2S 29 COM?.

SUBCOOE LLJ@)

19 REPORT TYPE l1J JO VALVE SUBCODE LU@

20 l=l 31 REVISION NO.

LQJ 80 ACTION FUTURE EFFECT SHUTOOW!',

A ATTACHMENT NPRD-4 T.:.l(EI, ACTION ON PLANT METHOO HOURS b' SUBMITTED FORM ~UE.

PRIME COMP.

SUPPLIER COMPONENT MANUFACTURE.~

LE l@J34 z!@

h5 z!@

lczl J; olo Io I ~J LY I@

~~ I W IF 111 210 I@

CAUSE DESCRIPTION AND CORREC'f!VE ACTIONS @

43 4,,:

47 I The narrow range pressure transmitter had been tagged out, and the tag:. was not cleared prior to putting PT 4G3: in service.

The malfunction of nressure transmitter 458 was due to a cable problem.

At no time during the loss of ITDJ CiTIJ ITEl pressure signals to the PORV's was the Overpressure Mitigating System needed,!

7 B

S FA::ILITY

'Jo' S1 ATVS

'lO. POWEF OTHER STATUS I.::;:/

[QTI lQJ@ IO 10 I OlI~ __

N_A __

a 9

10 12 13 ACTIVITY CO~TENi

?.£LEA.SEO OF r\\ELEASE AMOUf.l OF ACTIVITY @

8IJ ~

@) W@._I _N_A _____

5 9

10 11 80 METHOD OF A

DISCOVERY DISCOVERY DESCRIPTION (5.,

~@... I ___

O-=p'--e_r_a_t_o_r_

1_s_o_b_s_e_r_v_a_t_i_o_n ____ ___..

45 46 BO NA LOCATION OF RELEASE @

45 50 PERSONNEL EXPOSURES Q,,

GE] IO Tosr O 1@1zE1@~D-ES_C_R_IPTI_O_N_~_3_9 _______

N_A _______________________ __.

8 9

11 12 1:?

80 PERSONNEL INJURIES C,\\

NUMBER DESCRIFTIONO

~

JO JOJ Oj@)

7 a

9 11

- 12 _________________________

8

_.o NA LOSS OF OR DAMAGE TO FACILITY 0 TYPE

DESCRIPTION

~

DJi] lzJ@

NA e s

~10:----------------------------------------------80 PUBLICITY

~

~1SSUE!J DESCRIFTION e,,

!::u£J LRJE) _______________

N_A _______

___.j I II I II I II I II I NRC L:SE ONLY 7

s 9

10 58 e;

80 NAr~E OF PREP AR::? __ J~*--=L=-'-. _W"-'-"i""l"'s"'"o~n'----------

PHONE: (804) 357-3184 8006110265

ATTACHMENT, PAGE 1 e

SURRY POWER STATION, UNIT 2 DOCKET NO:

050-0281 REPORT NO:

80-004/0lT-O EVENT DATE:

5-21-80 TITLE OF REPORT:

OVERPRESSURE MITIGATING SYSTEM

1.

DESCRIPTION OF EVENT

With the unit at cold shutdown, solid and pressurized to 230 PSIA, PCV-456 was inoperable due to a wiring problem with the controlling pressure transmitter PT-458.

T.S. 3.l.6.2(a) allows pressurized operation in this mode for up to 7 days.

Subsequently, PT 403 was found isolated from system pressure, which made the Overpressure Mitigation system inoperable.

A second valve line-up was per-formed to correct the discrepancies prior to solid plant operation.

However, this second valve line-up was improperly performed, and did not identify the PT 403 isolation valve out of position. It should be noted that PT 403 did indicate some lower pressure than actual system pressure.
2.

PROBABLE CONSEQUENCES OF EVENT:

The inoperability of the Overpressure Mitigating system had no effect upon the health or safety of the general public because at no time during the loss of pressure signals to the PORV's was the Overpressure Mitigating system needed.

3.

CAUSE OF EVENT

The inoperability of the Overpressure Mitigating system was due to an improper valve line-up.

4.

IMMEDIATE CORRECTIVE ACTION

The innnediate corrective action taken was to open PT 403's isolation valve 2-RC-71.

5.

SCHEDULED CORRECTIVE ACTION:

None

6.

ACTION TAKEN TO PREVENT RECURRENCE:

The importance of proper valve line up was discussed with the operators involved.

In addition, discussions were held with all shift supervisors and asst. shift supervisors relating to the importance of safe and proper plant operation.

A test matrix has been prepared and issued which delineates an integrated thorough system check-out and start-up following the extended outage of Unit #2.

7.

GENERIC IMPLICATIONS:

None