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LER-1979-002, /03L-0 on 790120: During Normal Operation Channel Check Revealed That Pressurizer Pressure Channel I Drifted Above Tech Spec Limit as Compared to Channels II & Iii. Caused by Failure of Channel I Pressure Transmitter |
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| 2811979002R03 - NRC Website |
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LICENSEE EVENT REPORT CONTROL BLOCK:.____,__~_.____,~~'-~' 8 (PLEASE PRINT OR TY.LL REQUIRED INFORMATION) 6
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I V I A I s I p I s I 2 101 0 I O I - I 0 8
9 LICENSEE CODE 14 15 I o I o I o I o I -I ol 0101 41 11 11 11 1101 I 10 LICENSE NUMBER 25 26 LICENSE TYPE 30 57 CAT 58 CON'T
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21 11 sl 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 71 9IG)
BO EVENT DESCRIPTION AND PROBABLE CONSEQUENCES@
j During nomal operation, a channel check revealed that Pressurizer Pres sure Channel.
I drifted above the Technical Specification limit as compared to Channels II and III.f This drift would have resulted 1.n reactor protection--signals from this channel--of 5 psi below setpoints delineated in Tech. Spec. 3*. 7.
This event 1.s reportable per Tech!
[QJ]J Spec. 6.6.2.b.L The*health and safety of the general public were not affected.
8 9 SYSTEM CODE
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8
9 10 Q
LE R/RO CV ENT YEAR
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REPORT 17 I 9 j NUMBER 21 22
CAUSE
CAUSE CODE SU8CODE COMPONENT CODE
~J@ Lu@ I II NI sl Tl RI ul@
11 12 13 18 SEQUENTIAL OCCUR REN CE REPORT NO.
CODE L=.l I 01 Oj 2J J/I g ~
23 24 26 27 28 29 COMP.
SUBCODE LIJ 19 REPORT TYPE
~
30 VALVE SUBCODE w@
20 l=:.I 31
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ATTACHMENT ACTION FUTURE EFFECT SHUTDOWN TAKEN ACTION ON PLANT METHOD HOURS NPRD-4 FORM SUB.
PRIME COMP.
SUPPLIER REVISION NO.
LQJ 32 COMPONENT MANUFACTURER 80
\\..:;I SUBMITTED 1° I L2J@)
40 41
~@LU@ LU@
LU I_O 10 10 33 34 35 36 37
~ ~@) I Fl 11 21 01@
CAUSE DESCRIPTION AND CORRECTIVE ACTIONS @
- 42 43 44 QJI] L]'his event was caused by failure of the Channel I Pressure transmitter.
Channel I [JJJJ !pressurizer Pressure and Channel I Overtemperature Delta T were placed in the trip o:J2J jmode to provide the required degree of redundancy.
The transmitter was replaced, CiJ2) tested, and Channel I was returned to service.
8 9
FACILITY STATUS
% POWER*
OTHER STATUS @
METHOD OF A
47 J
80 [iJ}J ~@
lj 01 Ol@)I.._ __
NA ___
DISCOVERY DISCOVERY DESCRIPTION '2_v
~@... I _O_p=--e_r_a_t_o_r_o_b_s_e_r_v_a_t_1._* o_n __________ __.
8 9
10 12 13
. ACTIVITY CONTENT Q
RELEASED OF RELEASE AMOUNT OF ACTIVITY
~w ~@ ~@1 NA 7
8 9
10 11 45 46 44 80 NA LOCATION OF RELEASE @
44 45 80 PERSONNEL EXPOSURES c;;;,.
NUMBER TYPE DESCRIPTION~
r, [iJ j O I O j oJ@)~@...__N_A _____________________
8 9
11 12 13 80 PERSONNEL INJURIES Q
NUMBER DESCRIPTION~
Gli] j O I O I O l@L ___
N_A __________________ -'---------J 8
9 11 12 80 LOSS OF OR DAMAGE TO FACILITY '43' TYPE
DESCRIPTION
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NA 8
9 10 80 1ssu:isu~;;CRIPTION@
790222C)t>Cf ~
NRC USE ONL y
<D ITI§] ~@...._ __
N_A __________________
II II I I II II II I ~
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10 68 69 80 o, NAME OF PREPARER w. L_._s_t_e_w_a_r_t _______ '-----
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~ (Attachment, page 1~ 1)
Surry Power Station~nit 2 Docket No.:
50-281 Report No.:
79-002/03L-0 Date:
1/20/79 P~essure Indicator (PI-455) Reading hi~h
- 1.
Description of Event
During normal operation, a channel check revealed th~t Pressurizer Pressure Channel I drifted above the Technical Specification limit as compared to Channels II and III.
This drift would have resulted. in reactor protection signals from this channel of 5-psi *below set points delineated in Tech. Spec. 3.7.
This event is reportable per'--Tech. Spec.
6.6.2.b.l.
2, Probable Conseequences:
Immediate corrective action taken was to place the Pressurizer Pressure (Protection) Channel I and the Overtemperature Delta T Channel I in the trip mode.
This provided all affected systems with the required degree of redundancy.
Because the necessary actions were taken to maintain the r.equired instrument operating conditions, the health and safety of the general public were not affected.
- 3.
Cause
The event was caused by failure of the pressure transmitter.
4,
Immediate Corrective Action
Immediate corrective action taken was to place the Pressurizer Pressure (Protection) Channel I and the Overtemperature Delta T Channel I in the trip mode.
- 5.
Subsequent Corrective Action:
The pressure transmitter was replaced, tested and the channels returned to normal mode.
- 6.
Action Taken to Prevent Recurrence:
This failure is considered a random event, therefore no further action will be taken.
- 7.
Generic Implications:
Since this is considered a random failure, ther~ are no generic-~~
implications.
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Caused by Failure of Channel I Pressure Transmitter | /03L-0 on 790120: During Normal Operation Channel Check Revealed That Pressurizer Pressure Channel I Drifted Above Tech Spec Limit as Compared to Channels II & Iii. 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