/03L-0 on 781015:compensatory Surveillance on RCP Cstator & Hearing Temp Had Not Been Performed.Caused by Failure of Operating Personnel to Restore Process Computer Trend Block Following Computer Reinitialization| ML18113A609 |
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| Site: |
Surry  |
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| Issue date: |
11/03/1978 |
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| From: |
Baucom T VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.) |
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| To: |
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| Shared Package |
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| ML18113A608 |
List: |
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| References |
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| LER-78-036-03L, LER-78-36-3L, NUDOCS 7811090240 |
| Download: ML18113A609 (2) |
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Similar Documents at Surry |
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LER-1978-036, /03L-0 on 781015:compensatory Surveillance on RCP Cstator & Hearing Temp Had Not Been Performed.Caused by Failure of Operating Personnel to Restore Process Computer Trend Block Following Computer Reinitialization |
| Event date: |
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| Report date: |
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| 2811978036R03 - NRC Website |
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text
NRG.FORM 36-6 (7-77) e U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT CONTROL BLOCK: ~' -....__~ _
_.______,_ _ _.__.....,I G) 1 6
(PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)
~
I v 1 A I s I P I s I 2 101 o lo I - I o I o I o 1 o I o I - I o I o 101 4 11 11 11 11 101 I I G) 7 8
9 LICENSEE CODE 14 15 LICENSE NUMBER
- - 25 26 LICENSE TYPE 30 57 CAT 58 CON'T [iliJ 7
8
- ~~~~~ L!J© I O I 5 I O I O I O I 2 I 8 I 1 101 11
- 0 I 1 I s 1 7 j 8 jG) j l I 11 0 I 3 I 7 I s 10 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES@
I With the unit in normal operation at rated power, it was determined that compensa-I tory surveillance on RCP "C" stator and bearing temperatures had not been performed CUTI.
[Q]3J I as require~.
This is contrary to T.S. 3.21.A and is reportable per T.S. 6.6.2.b(3).
~
I The health and safety of the public were not affected.
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7 8 9 lIITl 7
8 SYSTEM CODE I Al Bl@
9 10
~
LER/RO CV ENT YEAR
\\!..!.,/ REPORT 17 j 8 I NUMBER
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CAUSE
CAUSE COMP.
CODE SUBCODE COMPONENT CODE SUBCODE U@ ~@
11 N I s I T I R I u I@ l!J@
11 12 13 18 19 SEQUENTIAL OCCUR REN CE REPORT VALVE SUBCODE
~@
20 REPORT NO.
CODE TYPE I O I 3 I 6 f I.,I I O I 3 I L:'.J l=::l 23 24 26 27 28 29 30 31 ACTION FUTURE' TAKEN ACTION CN ?LAN, METHOD HOURS
. SUBMITTED FORM :;UB, SU?PLIER REVISION NO.
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32 COMPONENT MANUFACTURER 80 E:=FECT SHUTDOWN
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ATTACHMENT NPRD-4 PRIME COMP.
l!!J@~@ ~@ L:J I O I O I O I I ~@ ~@) ~@
33 34 36 3 7 40 41 42 43 IF 10 is-11 I CAUSE DESCRIPT!CN AND CCRR!::CTlVE ACTIONS w',
44 47
!This occurre~ce was brought about'-=-by the failure of operating personnel to restore ITTIJ I the process coquter trend block following a computer reinitialization., Upon the r:IIIJ I discovery 0£ the 1.2.a.vailability of surveillance data, the computer trend block was reinitiated.
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9 FACILITY STATUS
% POl'IE'R METHOD OF A
80 OTHER STATUS NA ITfil W@ 11 Io Io l@I 7
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___.44 DISCOVERY DISCOVERY DESCRIPTION
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REL~SED OF RZLEASE AMOUNT OF ACTIVITY [iliJ L:J @) ~@I NA 7
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10 11 PERSONNEL EXPOSURES i
NUMBER
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_LOCATION ~F RELEASE @
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DESCRIPTION6 NA
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DESCRIPTION
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~~1 4' on/".'""\\ LI BO ISSUEDr,,-;;*/ESCRIPTION~
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"Attachment (page 1 of 1)~
Surry Power Station, Unit 2 Docket No: 50-281 Report No: 78-036/0JL-0 Event Date: 10-15-78 Missed Surveillance -
RCP 'C' Fire Protection
1. Description of Event
With unit in normal operation at rated power, it was determined that compensatory surveillance on RCP "C" stator and bearing temperatures had not been performed hourly as required, from 1650 on 10-15-78 to 0138 on 10-16-78.
This surveillance was required because the fire protection heat detector system on RCP "C" was not operable.
The event constitutes a condition contrary to Technical Specification 3.21.A and is reportable in accordance with Technical Specification 6.6.2.b(3).
- 2. Probable Consequences/Status of Redundant Systems:
Although the hourly surveillance was missed, the unit process computer would have flagged high stator or bearing temperature through its alarm programs.
Therefore, the health and safety of the public were not affected.
- 3.
Cause
This occurrence was brought about by the failure of operating personnel to restore the process-computer trend block which provides the surveillance data following a computer reinitialization.
- 4.
Immediate Corrective Action
Upon. the discovery of the unavailability of surveillance data, the computer tre:ld block was reinitiated.
Subsequently,_ the RCP "C" fire prevention *system detector was repaired.
- 5.
Scheduled Corrective Action:
Tne -prcblem was corrected innnediately and no further action is deemed necessa...ry.
k*
- . 6. *Action Taken to Prevent Recurrence:
Operators were instructed on 10-17-78 to monitor once per hour::the temperature of the systems affected by the RCP."C" fire protection sensor failure.
- 7.
Generic Implications:
There are no generic implications associated with this event.
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