Similar Documents at Surry |
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LER-1978-034, /03L-0:on 781006,w/unit at Cold Shutdown,Snubbers 2-RH-HSS-20 & 2-WFPD-HSS-9 Inoperable.Caused by Low Fluid Level.Defective Snubbers Dry Because of Leaking Rod Seals & Mechanical Damage to Seals.Snubbers Replaced |
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| 2811978034R03 - NRC Website |
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NRC FORM 36n (7*7J~
u, s. NUCLEAR REGULATORY COMMISSION. --
~ICENSEE EVENT REPORT.
CONTROL BLOCK:!
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(PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 6
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LICENSEE CODE 14 15 LICENSE NUMBER 25 26 LICENSE TYPE
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- 1 s 10 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES (10) j With unit 2 t cold shutdown, snubbers Y-RH-HSS-20 and 2-WFPD-HSS-9 were found inoperable!
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I on the end-of-interval inspection.
The units were inoperable because of low fluid *
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'I:-.:..s conditio:i is contrary to T.S. 3.20.A and is reportable in accordance with T.S. 6.6.:.~.(2).
~22 health and safety of the public were not affected.
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CAUSE
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SUBCODE
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@ RL::~~~ ci~,,~-~~~r SEQUENTIAL REPORT NO.
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- -3 24 26 COMPONENT CODE 1u I p 10 IR IT 1@
18 OCCURRENCE CODE I/I Io 13 r 27 28 29 COMP.
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19 REPORT TYPE
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30 VALVE SUBCODE
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20 REVISION NO.
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31 32 PRIME C,OMP.
TAKEN ACTIO.'.
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SUPPLIER COMPONENT MANUFACTURER ACTION FUTUR::
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42 43 44 47 CAUSE DESCRI;:--=:::-...:.'\\;:::;: ::;-;:;::;=:CT/VE ACTIONS@
I The defec--'*- 0 s------~.:o.~s were dry because of leaking rod sea1s. The seals were EP materi-1 Lili] I al and had '=>:::*.-=-d C""' to mechanical damage to the seal~_ The* inoperable snubbers CIII] I were replaced wic:2 snop spares.
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80 FACILITY STATUS
% ?OW::R OTHER STATUS DISCOVERY DISCOVERY DESCRIPTION 32
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RELEASED OF RE LEAS::
AMOUNT OF ACTIVITY GE ~@ ~§I NA 1
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10 11 45 46 80 NA
_LOCATION OF RELEASE @
44 45 80 PERSONNEL EXPOSURES NUMBER r:::;,,. TYPE DESCRIPTION@
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NUMBER DESCRIPTION6 [D.TI I 01 01 0 I@
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LOSS OF OR DAMAGE TO FACILITY '4:0 TYPE
DESCRIPTION
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(Attachment,*Page 1 ~l)
Surry Power Station, Unit 2 Docket No: 050-0281 Report No: 78-034/03L-0 Event Date:
10-6-78 Snubber Inspection Results
- 1.
Description of Event
~ith the unit at cold shutdown, snubbers 2-RH-HSS-20 and 2-WFPD-HSS-9 were ietermined to be inoperable by the end-of-interval inspection.
The s~ub~2rs had no detectable fluid level.
This condition is contrary to Te~tc_i=al Speci=ication 3.20.A and is reportable in accordance with Technical S?eci=i~ation 5.6.~.b.(2).
~-=-
-,--c.::.cc----:_--=----=-s of an inoperable snubber is an increase in the probability o:;: 0::-----,--:::"'.-==-=::,:.::.
-':J piping as a result of seismic or other event initiating dyn;::-- - - -:=-=:o.
.::-----j.=.~ protection is required only during a low probability of eve::::~, ::::2::--2:=':.-::-2~ =~-:e total loss of suppressor fluid from 2-RH-HSS-20 and 2-HF~=-=.3:::-; ~:: :-_,:: effect upon the health and safety of the general public.
- 3.
Cause --.::.-.-==.:::
_ -=-
.::c::-*.:::.:,
the low fluid level was leaking rod seals on both snubbers.
The s"'--=-=--=- -,,e:::-'= :i:::::?.:.aterial and had suffered mechanical damage, rather than aging -2.:'=2*::::5 :='::-o::i radiation or heat.
- 4.
Immedia::e C8::-r2~tive Action:
7:i:::e failed snubbers were replaced with shop spares.
- 5.
Scheduled Corrective Action:
1-io further corrective actions are scheduled at this time.
- 6.
Action Taken to Prevent Recurrence:
Present intentions are to replace the "as found" inoperable snubbers with Q.C. accepted operable snubbers.
- 7.
Generic Implications:
Leaking of snubber fluid is a problem, inherent to hydraulic systems, maintained within safe bounds by periodic inspection and routine maintenance.
The loss of reservoir fluid, as in the case of hydraulic snubbers 2-RH-HSS-20 and 2-HFPD-HSS-9, is not considered a.generic problem because of the infrequency of such occurrence,at these snubber locations.
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| 05000280/LER-1978-001, Submit Licensee Event Report No. LER-78-001/03L-0 Re Hydraulic Shock Suppressor Found Inverted with Empty Reservoir | Submit Licensee Event Report No. LER-78-001/03L-0 Re Hydraulic Shock Suppressor Found Inverted with Empty Reservoir | | | 05000280/LER-1978-002, Submit Licensee Event Report No. LER-78-002/01T-0 Re Additional Radial Peaking Factor Surveillance | Submit Licensee Event Report No. LER-78-002/01T-0 Re Additional Radial Peaking Factor Surveillance | | | 05000280/LER-1978-003, Submit Licensee Event Report No. LER-78-003/03L-0 Re Failed Heat Tracing, Panel 8 Circuit 24 | Submit Licensee Event Report No. LER-78-003/03L-0 Re Failed Heat Tracing, Panel 8 Circuit 24 | | | 05000280/LER-1978-004-03, /03X-1 on 780305:loss of Svc Water Flow Through Charging Pump Intermediate Seal Cooler Was Caused by Corrosion of Stem of Discharge Gate Valve;Corrosion Was Galvanic(Brass Touching Bronze);Problem Will Be Studied | /03X-1 on 780305:loss of Svc Water Flow Through Charging Pump Intermediate Seal Cooler Was Caused by Corrosion of Stem of Discharge Gate Valve;Corrosion Was Galvanic(Brass Touching Bronze);Problem Will Be Studied | | | 05000280/LER-1978-004, Submit Licensee Event Report No. LER-78-004/03L-0 Re Loss of Service Water Flow Through Charging Pump Intermediate Seal Cooler | Submit Licensee Event Report No. LER-78-004/03L-0 Re Loss of Service Water Flow Through Charging Pump Intermediate Seal Cooler | | | 05000280/LER-1978-005, Forwarding Licensee Event Report No. LER-78-005/01T-0 Re Westinghouses Error in LOCA-ECCS Evaluation Model, Which Will Result in Higher Calculated Peak Clad Temperature | Forwarding Licensee Event Report No. LER-78-005/01T-0 Re Westinghouses Error in LOCA-ECCS Evaluation Model, Which Will Result in Higher Calculated Peak Clad Temperature | | | 05000280/LER-1978-006, Submit Licensee Event Report No. LER-78-006/01T-0 Re Seismically Disqualified Two Pipe Extensions on Fire Protection Yard Piping | Submit Licensee Event Report No. LER-78-006/01T-0 Re Seismically Disqualified Two Pipe Extensions on Fire Protection Yard Piping | | | 05000280/LER-1978-007, Submit Licensee Event Report No. LER-78-007/03L-0 Re Leak on Body to Bonnet Joint Diaphragm Valve 1-CH-98 | Submit Licensee Event Report No. LER-78-007/03L-0 Re Leak on Body to Bonnet Joint Diaphragm Valve 1-CH-98 | | | 05000280/LER-1978-008, Submit Licensee Event Report Nos. LER-78-008/03L-0, LER-78-009/03L-0, LER-78-010/03L-0, LER-78-011/03L-0 for Surry Unit No. 1 | Submit Licensee Event Report Nos. LER-78-008/03L-0, LER-78-009/03L-0, LER-78-010/03L-0, LER-78-011/03L-0 for Surry Unit No. 1 | | | 05000281/LER-1978-011-03, /03X-1 on 780305:During Normal Full Pwr Oper,There Was No Svc Water Flow Thru Charging Pump Intermediate Seal Cooler 2-SW-E-1B,due to Failure of the Coolers Discharge Gate Valve | /03X-1 on 780305:During Normal Full Pwr Oper,There Was No Svc Water Flow Thru Charging Pump Intermediate Seal Cooler 2-SW-E-1B,due to Failure of the Coolers Discharge Gate Valve | | | 05000281/LER-1978-011, Forwards LER 78-011/03X-1 | Forwards LER 78-011/03X-1 | | | 05000280/LER-1978-012, Submit Licensee Event Report No. LER-78-012/03L-0 Re Inside Recirculation Spray Pump 1-RS-P-1A, Failure to Rotate by Hand | Submit Licensee Event Report No. LER-78-012/03L-0 Re Inside Recirculation Spray Pump 1-RS-P-1A, Failure to Rotate by Hand | | | 05000280/LER-1978-013, Submit Licensee Event Report Nos. LER 78-013/03L-0 Re Six Snubbers Not Meeting Test Criteria, & 78-014/03L-0 Re Mount Plate Was Warped, & 3 of 8 Bolts Were Insufficiently Embedded | Submit Licensee Event Report Nos. LER 78-013/03L-0 Re Six Snubbers Not Meeting Test Criteria, & 78-014/03L-0 Re Mount Plate Was Warped, & 3 of 8 Bolts Were Insufficiently Embedded | | | 05000280/LER-1978-015, Submit Licensee Event Report No. LER-78-015/03L-0 Re Valve Cleanliness Inspection Found Foreign Material on Valve Seating Surfaces | Submit Licensee Event Report No. LER-78-015/03L-0 Re Valve Cleanliness Inspection Found Foreign Material on Valve Seating Surfaces | | | 05000280/LER-1978-016, Submit Licensee Event Report No. LER 78-016/03L-0 Re Valve MOV-RH-100 Was Not Opening | Submit Licensee Event Report No. LER 78-016/03L-0 Re Valve MOV-RH-100 Was Not Opening | | | 05000280/LER-1978-017, Submit Licensee Event Report Nos. LER 78-017/03L-0 Re Not Documenting Four Electric Maintenance Procedures & Two Periodic Tests, & 78-020/03L-0 Re Suspended Air Bubbles in Reservoir Fluid | Submit Licensee Event Report Nos. LER 78-017/03L-0 Re Not Documenting Four Electric Maintenance Procedures & Two Periodic Tests, & 78-020/03L-0 Re Suspended Air Bubbles in Reservoir Fluid | | | 05000280/LER-1978-018, Sutmit Licensee Event Report No. LER 78-018/03L-0 Re Two Main Steam Safety Valves Were Not within Plus or Minus 3% of Setpoint as Required | Sutmit Licensee Event Report No. LER 78-018/03L-0 Re Two Main Steam Safety Valves Were Not within Plus or Minus 3% of Setpoint as Required | | | 05000280/LER-1978-022-03, /03X-1 on 780726:Hydro Test Pump Failed to Build Up Pressure During Attempt to Fill Safety Injection Accumulators Due to Lifting of Its Relief Valve.Valve Replaced & Checked.Accumulator Refilled | /03X-1 on 780726:Hydro Test Pump Failed to Build Up Pressure During Attempt to Fill Safety Injection Accumulators Due to Lifting of Its Relief Valve.Valve Replaced & Checked.Accumulator Refilled | | | 05000280/LER-1978-022, Forwards LER 78-022/03X-1 | Forwards LER 78-022/03X-1 | | | 05000280/LER-1978-024, Submit Licensee Event Report No. LER 78-024/03L-0 Re No Alarm During a Planned Release of Liquid Radioactive Waste | Submit Licensee Event Report No. LER 78-024/03L-0 Re No Alarm During a Planned Release of Liquid Radioactive Waste | | | 05000280/LER-1978-027, Submit LER 78-027/03L-0 Re Seven Snubbers Not Meeting Inspection Criteria | Submit LER 78-027/03L-0 Re Seven Snubbers Not Meeting Inspection Criteria | | | 05000280/LER-1978-028-03, /03L-0 on 780916:snubber Not Meeting Inspec Criteria Caused by Low Oil Level Due to Leakage at Mating Surface Between Body & End Plate.Holding Bolts Were Tightened & Snubber Was Refilled | /03L-0 on 780916:snubber Not Meeting Inspec Criteria Caused by Low Oil Level Due to Leakage at Mating Surface Between Body & End Plate.Holding Bolts Were Tightened & Snubber Was Refilled | | | 05000280/LER-1978-028, Forwards LER 78-028/03L-0 | Forwards LER 78-028/03L-0 | | | 05000280/LER-1978-029-03, X-1, LER 78-029-03L-0, & LER 78-031-03L-0 for Surry 2 Re Critical Below Minimum Insertion Limit on D Control Bank | X-1, LER 78-029-03L-0, & LER 78-031-03L-0 for Surry 2 Re Critical Below Minimum Insertion Limit on D Control Bank | | | 05000280/LER-1978-029, Forwards LER 78-029/03L-0 | Forwards LER 78-029/03L-0 | | | 05000280/LER-1978-030, Forwards LER 78-030/03L-0, 78-031/03L-0, 78-032/03L-0, 78-033/03L-0 | Forwards LER 78-030/03L-0, 78-031/03L-0, 78-032/03L-0, 78-033/03L-0 | | | 05000280/LER-1978-030-03, /03L-0 on 781009:w/unit at Rated Pwr,Charging Pump Component Cooling Water Pump Btripped.Pump Tripped on Overcurrent.Caused by Corrosion Damage to Motor Bearings. Pump & Motor Rebuilt & Reinstalled | /03L-0 on 781009:w/unit at Rated Pwr,Charging Pump Component Cooling Water Pump Btripped.Pump Tripped on Overcurrent.Caused by Corrosion Damage to Motor Bearings. Pump & Motor Rebuilt & Reinstalled | | | 05000280/LER-1978-031-03, /03X-1 on 781001:during Normal Operation,Channel I Pressurizer Level (Protection) L-I-459 Drifted High.Caused by Drift of Electronic Zero Adjustment,In Conjunction W/ Leakage Thru Transmitter Bypass/Equalizing Valve | /03X-1 on 781001:during Normal Operation,Channel I Pressurizer Level (Protection) L-I-459 Drifted High.Caused by Drift of Electronic Zero Adjustment,In Conjunction W/ Leakage Thru Transmitter Bypass/Equalizing Valve | | | 05000280/LER-1978-031, Forwards LER 78-031/03X-1 & 78-038/03X-1 | Forwards LER 78-031/03X-1 & 78-038/03X-1 | | | 05000281/LER-1978-032, Forwards LER 78-032/03L-0 | Forwards LER 78-032/03L-0 | | | 05000280/LER-1978-032-03, /03L-0 on 781011:heat Tracing Circuit Faults Had Occurred as a Result of Boric Acid Incursion.Faults Repaired & Circuit Current Verified | /03L-0 on 781011:heat Tracing Circuit Faults Had Occurred as a Result of Boric Acid Incursion.Faults Repaired & Circuit Current Verified | | | 05000281/LER-1978-032-03, /03L-0:on 780921,heat Tracing Circuit Manual Boration/Boric acid-to-blender Failed.Caused by Boric Acid Penetration of Heat Tracing Tape Circuits.Heat Tracing Tape Replaced | /03L-0:on 780921,heat Tracing Circuit Manual Boration/Boric acid-to-blender Failed.Caused by Boric Acid Penetration of Heat Tracing Tape Circuits.Heat Tracing Tape Replaced | | | 05000281/LER-1978-033, Forwards LER 78-033/03L-0 | Forwards LER 78-033/03L-0 | | | 05000281/LER-1978-033-03, /03X-1 on 780926:circulating Water Outlet Valve MOV-CW-200D Failed to Close When Operated Electrically. Caused When Actuator Cam for Shut Torque Switch Became Wedged Against Torque Switch Hold Down Screw | /03X-1 on 780926:circulating Water Outlet Valve MOV-CW-200D Failed to Close When Operated Electrically. Caused When Actuator Cam for Shut Torque Switch Became Wedged Against Torque Switch Hold Down Screw | | | 05000280/LER-1978-033-03, /03L-0 on 781015:heat Tracing Circuit Failed. Caused by Old Boric Acid Buildup & Penetration of Heat Leakage | /03L-0 on 781015:heat Tracing Circuit Failed. Caused by Old Boric Acid Buildup & Penetration of Heat Leakage | | | 05000281/LER-1978-034-03, /03L-0:on 781006,w/unit at Cold Shutdown,Snubbers 2-RH-HSS-20 & 2-WFPD-HSS-9 Inoperable.Caused by Low Fluid Level.Defective Snubbers Dry Because of Leaking Rod Seals & Mechanical Damage to Seals.Snubbers Replaced | /03L-0:on 781006,w/unit at Cold Shutdown,Snubbers 2-RH-HSS-20 & 2-WFPD-HSS-9 Inoperable.Caused by Low Fluid Level.Defective Snubbers Dry Because of Leaking Rod Seals & Mechanical Damage to Seals.Snubbers Replaced | | | 05000280/LER-1978-034-01, /01X-1 on 781101:noted That 17 Spare Process Piping Penetrations on Unit 1 & 23 on Unit 2 Were Not Capped in Auxiliary Bldg.Caused by Failure to Properly Complete Capping at End of Constr | /01X-1 on 781101:noted That 17 Spare Process Piping Penetrations on Unit 1 & 23 on Unit 2 Were Not Capped in Auxiliary Bldg.Caused by Failure to Properly Complete Capping at End of Constr | | | 05000280/LER-1978-034, Update to LER 78-034/01X-2 on 781101:17 Spare Process Piping Containment Penetrations Were Not Capped.Condition Has Been Overlooked Since Const.Design Change Approved to Weld Caps on Open Ends | Update to LER 78-034/01X-2 on 781101:17 Spare Process Piping Containment Penetrations Were Not Capped.Condition Has Been Overlooked Since Const.Design Change Approved to Weld Caps on Open Ends | | | 05000280/LER-1978-035, Forwards LER 78-035/01T-0 | Forwards LER 78-035/01T-0 | | | 05000281/LER-1978-035-03, /03L-0:on 781007,during Cold Shutdown,Valve Pit Flooded While Draining Circulating Water Box D.Caused by Damage of Valve from Flooding | /03L-0:on 781007,during Cold Shutdown,Valve Pit Flooded While Draining Circulating Water Box D.Caused by Damage of Valve from Flooding | | | 05000280/LER-1978-035-01, /01T-0 on 781109:study of Calibr Techniques Showed That SI Accumulators Indicated Level Would Be Lower than Actual Level.Discovered After Rigorous Review of Factors Affecting Instru | /01T-0 on 781109:study of Calibr Techniques Showed That SI Accumulators Indicated Level Would Be Lower than Actual Level.Discovered After Rigorous Review of Factors Affecting Instru | | | 05000280/LER-1978-036, Forwards LER 78-036/03L-0, 70-037/03L-0 & 78-038/03L-0 | Forwards LER 78-036/03L-0, 70-037/03L-0 & 78-038/03L-0 | | | 05000280/LER-1978-036-03, /03L-0 on 781107:failure of Heat Tracing Circuit 24D,Unit 1,due to Boric Acid Damage.Heat Tracing Tape Replaced | /03L-0 on 781107:failure of Heat Tracing Circuit 24D,Unit 1,due to Boric Acid Damage.Heat Tracing Tape Replaced | | | 05000281/LER-1978-036-03, /03L-0 on 781015:compensatory Surveillance on RCP Cstator & Hearing Temp Had Not Been Performed.Caused by Failure of Operating Personnel to Restore Process Computer Trend Block Following Computer Reinitialization | /03L-0 on 781015:compensatory Surveillance on RCP Cstator & Hearing Temp Had Not Been Performed.Caused by Failure of Operating Personnel to Restore Process Computer Trend Block Following Computer Reinitialization | | | 05000281/LER-1978-036, Forwards LER 78-036/03L-0 | Forwards LER 78-036/03L-0 | | | 05000281/LER-1978-037, Forwards LER 78-037/03L-0 | Forwards LER 78-037/03L-0 | | | 05000280/LER-1978-037-03, /03L-0 on 781107:procedure Deviation Found Re Filling & Venting Reactor Coolant Sys on 770105.Procedure Deviation Was Misrouted to Records Vault W/O Review by Snsoc.Deviation Has Now Been Submitted to Snsoc for Review | /03L-0 on 781107:procedure Deviation Found Re Filling & Venting Reactor Coolant Sys on 770105.Procedure Deviation Was Misrouted to Records Vault W/O Review by Snsoc.Deviation Has Now Been Submitted to Snsoc for Review | | | 05000281/LER-1978-037-03, /03L-0 on 781022:with Unit at Rated Pwr,Panel Indicator for Radiat Monitor RM-213 Monitoring a Steam Generator Blowdown Read 0.Caused by Loose Connector Joining Detector Cable to Electronic Chassis | /03L-0 on 781022:with Unit at Rated Pwr,Panel Indicator for Radiat Monitor RM-213 Monitoring a Steam Generator Blowdown Read 0.Caused by Loose Connector Joining Detector Cable to Electronic Chassis | | | 05000281/LER-1978-038-03, /03X-1 on 781030:boric Acid Flow from Boric Acid Tank to Blender Was Interrupted.Caused by Blockage of Crystallized Boron at Elbow in Line 1-CH-356-152 | /03X-1 on 781030:boric Acid Flow from Boric Acid Tank to Blender Was Interrupted.Caused by Blockage of Crystallized Boron at Elbow in Line 1-CH-356-152 | | | 05000280/LER-1978-038-03, /03X-1 on 781108:review of Operational Data Showed That Quarterly Calibr of Nuclear Power Range Instrumentation Had Not Been Performed Per Schedule,Due to Scheduling Error | /03X-1 on 781108:review of Operational Data Showed That Quarterly Calibr of Nuclear Power Range Instrumentation Had Not Been Performed Per Schedule,Due to Scheduling Error | |
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