ML18106A866

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Forwards SALP Repts 50-272/98-99 & 50-311/98-99 for Salem Units 1 & 2,for Periods 970301-980801.Rept Will Be Discussed at Public Meeting to Be Held at Pse&G Processing Center on 980930
ML18106A866
Person / Time
Site: Salem  PSEG icon.png
Issue date: 09/15/1998
From: Miller H
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To: Keiser H
Public Service Enterprise Group
Shared Package
ML18106A867 List:
References
50-272-98-99, 50-311-98-99, NUDOCS 9809210142
Download: ML18106A866 (4)


See also: IR 05000272/1998099

Text

Mr. Harold W. Keiser

Chief Nuclear Officer & President -

Nuclear Business Unit

Public Service Electric & Gas

Company

Post Office Box 236

Hancocks Bridge, NJ 08038

September 15, 1998

SUBJECT:

SALEM NUCLEAR GENERATING STATION, UNIT NOS. 1 AND 2 -

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE (SALP), REPORT

NOS. 50-272/98-99 AND 50-311 /98-99

Dear Mr. Keiser:

This letter forwards the Salem Nuclear Generating Station, Unit Nos. 1 and 2, SALP report

for the period of March 1, 1997, to August 1, 1998 (Enclosure). The SALP report does

not reflect the period from November 1994 to February 1997, when the U.S. Nuclear

Regulatory Commission (NRC) had suspended the SALP process because of the extended

shutdown of both units. This assessment was conducted using the SALP process that

was implemented by the NRC on July 19, 1993. The SALP process rates licensees in tour

functional areas: Operations, Maintenance, Engineering, and Plant Support. The Plant

Support area includes radiological and effluent controls, chemistry, security, emergency

preparedness, fire protection, and housekeeping.

During the SALP period, the overall performance at the Salem Station improved as

demonstrated by a nearly event free return of both units to operation following the

extended outage. Performance was characterized by strong management oversight by the

new management team assembled since the shutdown, safe and conservative operations

and decisions, good day-to-day engineering support to operations, and sound and effective

programs for independent oversight and self-assessment. The modifications and

maintenance activities performed during the extended shutdown significantly improved the

material condition of the facility. Necessary, significant steps were taken to resolve

operator workarounds stemming from safety related and balance of plant equipment

problems. Although the maintenance and engineering backlogs remain high, the issues

were appropriately prioritized and managed. Some improvement has been noted in the

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work control process. However, while human performance has improved significantly from

/

the period before the extended shutdown due to the extensive training interventions,

personnel errors in the areas of operations and maintenance continue to warrant close

management attention.

  • - Performance in the Operations functional area was rated Category 1 . Performance in

operations improved significantly over the period. A conservative approach was

consistently taken to plant operations. Control room activities were strong as exhibited by

effective command and control, well conducted shift turnovers and special operations

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Mr. H. W. Keiser

2

briefings. Operators performed well during the return of the units to normal operation;

  • restart of the units posed significant challenges owing to the numerous plant configuration

changes and large scope of testing associated with plant modifications made during the

outage. Although human performance has improved, some challenges arose as a result of

occasional lapses in attention to detail and improper equipment status control. Problem

identification and self assessment activities of both the line and oversight organization

were strong. Operator initial and requalification training programs were sound.

Performance in the Maintenance functional area was rated Category 2. The material

condition of the facility dearly improved as demonstrated by good equipment performance

since restart of the units. In general, outage work was properly planned, scheduled, and

implemented. Nonetheless, some problems were noted in transitioning from an outage

environment to an operating environment. Human performance problems involving

equipment verification and adherence to procedures continued to occur. The maintenance

backlog is high, largely due to aggressive discovery efforts during the outage, but site

management has demonstrated an understanding of the indiyidual and cumulative effects

of the backlog and has effectively managed the prioritization of backlogged items. Efforts

have been made to improve the work control process. The use of risk insights and limiting

conditions for operation (LCO) maintenance plans demonstrated a better understanding of

the impact of maintenance on plant safety and reliability. But the backlog reduction has

been impacted by slow progress in implementing the improved work control process.

Performance in the Engineering functional area was rated Category 2. Effective

engineering support also contributed to improved equipment reliability and plant

performance. Good management oversight and involvement were key factors in process

improvements. Activities such as the FSAR Review Project and the Technical

Specifications Surveillance Improvement Project, improved the station's conformance to its

licensing and design bases. With few exceptions, the quality of the design engineering

products was good, including the completion of 10 CFR 50.59 safety evaluations.

Although there was good engineering support to operations, in some noteworthy cases

system performance monitoring was not effective in identifying declining performance

before it impacted plant operations. Progress in this area has been impeded somewhat by

the large engineering backlog, which was also largely due to past performance problems

which were brought to light through aggressive discovery efforts during the outage.

Industry operating experience was effectively used. Licensing submittals were technically

sound; however, the completion of some licensing issues was impacted .by untimely

submission of required supporting information.

Performance in the Plant Support functional area was rated Category 1 . Performance in

radiation protection was excellent as indicated by continued low worker exposures. The

solid radwaste transportation, radioactive effluent, environmental monitoring, and

meteorological monitoring programs were well implemented. Significant improvements

were observed in emergency preparedness and security. While final resolution of electrical

raceway fire barrier systems issues remains to be completed, the fire protection program

was effectively implemented.

...

Mr. H. W. Keiser

3

The schedule for planned NRC inspections of your facility was previously provided with our

May 29, 1998, Plant Performance Review letter.

We have scheduled a management meeting with you to discuss our assessment. The

meeting will be held at 2:00 pm on September 30, 1998, at the PSE&G Processing Center

and will be open to the public. At the meeting, you and your staff should be prepared to

discuss our assessment and any initiatives you have ongoing or plan to take to address the

issues detailed in our evaluation.

We appreciate your cooperation.

Docket Nos. 50-272 and 50-311

Sincerely,

Original Signed By:

Hubert J. Miller

Regional Administrator

Region I

Enclosure: SALP Report Nos. 50-272/98-99

and 50-311 /98-99

cc w/encl:

L. Storz, Senior Vice President - Nuclear Operations

E. Simpson, Senior Vice President - Nuclear Engineering

E. Salowitz, Director - Nuclear Business Support

A. F. Kirby, Ill, External Operations - Nuclear, Delmarva Power & Light Co.

J. A. Isabella, Manager, Joint Generation, Atlantic Electric

C. Bakken, General M*anager - Salem Operations

J. McMahon, Director - QA/Nuclear Training/Emergency Preparedness

D. Powell, Director - Licensing/Regulation & Fuels

R. Kankus, Joint Owner Affairs

A. C. Tapert, Program Administrator

Jeffrey J. Keenan, Esquire

Consumer Advocate, Office of Consumer Advocate

William Conklin, Public Safety Consultant, Lower Alloways Creek Township

State of New Jersey

State of Delaware

Chairman Jackson

Commissioner Diaz

Commissioner McGaffigan.

Institute of Nuclear Power Operations (INPO)

Mr. H. W. Keiser

DISTRIBUTION w/encl:

Region I Docket Room (with concurrences)

Nuclear Safety Information Center (NISC)

NRC Resident Inspector

PUBLIC

H. Miller, RA/W. Axelson, DRA

C. Hehl, DRP Director

J. Linville, DRP

S. Barber, DRP

C. O'Daniell, DRP

J. Wiggins, DRS Director

L. Nicholson, DRS Deputy Director

M. Oprendek, DRP

J. Lanning, DRP

DISTRIBUTION w/encl: (Via e-mail)

J. Callan, EDO

B. McCabe, OEDO

S. Collins, NRR

B. Boger, NRR

J. Zwolinski, NRR

J. Lieberman, OE

R. Capra, NRR/PDl-:2

P. Milano, NRR

R. Correia, NRR

F. Talbot, NRR

DOCDESK

Inspection Program Branch, NRR (IPAS)

DISTRIBUTION via e-mail:

Region I Staff (Refer to SALP Drive)

4

DOCUMENT NAME: G:\\BRANCH3\\2-SAL\\SALP\\SALSALP.98

To receive a copy of this document. Indicate in the box: *c* = Copy without attachment/enclosure "E" = Copy with attachment/enclosure "N" =

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OFFICE

RI/DRS

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