Similar Documents at Salem |
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Category:MONTHLY OPERATING ANALYSIS REPORT
MONTHYEARML18107A5571999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With 991014 Ltr ML18107A5581999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With 991014 Ltr ML18107A5301999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 990913 Ltr ML18107A5311999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 ML18107A4811999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With 990813 Ltr ML18107A4821999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With 990813 Ltr ML18107A4341999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With 990713 Ltr ML18107A4351999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With 990713 Ltr ML18107A3681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With 990611 Ltr ML18107A3721999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With 990611 Ltr ML18107A2991999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With 990514 Ltr ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 ML18107A2971999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With 990514 Ltr ML18107A1831999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 990414 Ltr ML18107A1821999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With 990414 Ltr ML18106B1021999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With 990315 Ltr ML18106B1011999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With 990315 Ltr ML18106B0571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With 990212 Ltr ML18106B0561999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With 990212 Ltr ML18106B0261998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 1.With 990115 Ltr ML18106B0251998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With 990115 Ltr ML18106A9831998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Salem,Unit 2.With 981214 Ltr ML18106A9801998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Salem,Unit 1.With 981214 Ltr ML18106A9641998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Salem,Unit 2. with 981112 Ltr ML18106A9631998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Salem,Unit 1. with 981112 Ltr ML18106A9151998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Salem,Unit 2.With 981012 Ltr ML18106A9131998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Salem,Unit 1.With 981012 Ltr ML18106A8751998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Salem Generating Station,Unit 2.With 980915 Ltr ML18106A8741998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Salem Unit 1.With 980915 Ltr ML18106A8161998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Salem,Unit 1. W/980817 Ltr ML18106A8151998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Salem,Unit 2. W/980817 Ltr ML18106A7151998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Salem,Unit 2. W/980715 Ltr ML18106A7141998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Salem,Unit 1. W/980715 Ltr ML18106A6541998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Salem Unit 1. W/980615 Ltr ML18106A6531998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Salem Unit 2. W/980615 Ltr ML18106A6121998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Salem Generating Station,Unit 1.W/980515 Ltr ML18106A6111998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Salem Unit 2. W/980515 Ltr ML18106A5561998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Salem,Unit 1. W/980415 Ltr ML18106A4591998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Salem Unit 2. W/980415 Ltr ML18106A3771998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Salem Generating Station,Unit 1.W/980316 Ltr ML18106A3761998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Salem Generating Station,Unit 2.W/980316 Ltr ML18106A3281998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Salem,Unit 2. W/980217 Ltr ML18106A3271998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Salem,Unit 1. W/980217 Ltr ML18106A2721997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Salem,Unit 2. W/980115 Ltr ML18106A2711997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Salem Generating Station,Unit 1.W/980115 Ltr ML18106A2081997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Salem,Unit 1. W/971212 Ltr ML18106A2071997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Salem,Unit 2. W/971212 Ltr ML18102B6811997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Salem,Unit 2.W/ 971117 Ltr ML18102B6801997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Salem,Unit 1.W/ 971117 Ltr ML18102B6271997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Salem,Unit 2. W/971015 Ltr 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML18107A5581999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With 991014 Ltr ML18107A5571999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With 991014 Ltr ML18107A5301999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 990913 Ltr ML18107A5311999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 ML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A5201999-08-12012 August 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#9) Second Interval,Second Period, First Outage (96RF). ML18107A4811999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With 990813 Ltr ML18107A4821999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With 990813 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A5211999-07-0101 July 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#10) Second Interval,Second Period,Second Outage (99RF). ML18107A4351999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With 990713 Ltr ML18107A4341999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With 990713 Ltr ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A3681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With 990611 Ltr ML18107A3721999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With 990611 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 ML18107A3151999-04-30030 April 1999 Submittal-Only Screening Review of Salem Generating Station Individual Plant Exam for External Events (Seismic Portion), Rev 1 ML18107A2991999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With 990514 Ltr ML18107A2971999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With 990514 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18107A2881999-04-0707 April 1999 Rev 0 to NFS-0174, COLR for Salem Unit 2 Cycle 11. ML18107A1821999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With 990414 Ltr ML18107A1831999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 990414 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B1021999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With 990315 Ltr ML18106B1011999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With 990315 Ltr ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0561999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With 990212 Ltr ML18106B0571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With 990212 Ltr ML20205P1671999-01-31031 January 1999 a POST-PLUME Phase, Federal Participation Exercise ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0251998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With 990115 Ltr 1999-09-30
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Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038 Salem Generating Station November 14, 1994 U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Attn.: Document Control Desk MONTHLY OPERATING REPORT SALEMNO. 2 DOCKETN0.:50-311 In compliance with Section 6.9.1.6, Reporting Requirements for the Salem Technical Specifications, the original copy of the monthly operating reports for the month of October 1994 are being sent to you.
Average Daily Unit Power Level Operating Data Report Unit Shutdowns and Power Reductions 10CFR50.59 Evaluations Operating Summary Refueling Information Sincerely yours, ager-Salem Operations RH:vls Enclosures C Mr. Thomas T. Martin Regional Administrator USNRC, Region I 631 Park Avenue
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The power ism .G!.i.~ p: 9411230308 941031 PDR ADDCK 05000311 R PDR 95-2189 REV 7-92
AVERAGE DAILY UNIT POWER LEVEL Docket No.: 50-311 Unit Name: Salem #2 Date: 11-10-94 Completed by: Mike Morroni Telephone: 339-5142 Month October 1994 Day Average Daily Power Level Day Average Daily Power Level (MWe-NET) (MWe-NET) 1 164 17 0 2 420 18 0 3 990 19 0 4 968 20 0 5 1035 21 0 6 1033 22 0 7 1037 23 0 8 1050 24 0 9 1021 25 0 10 1056 26 0 11 1040 27 0 12 1037 28 0 13 606 29 0 14 0 30 0 15 0 31 0 16 0 P. 8.1-7 Rl
.. OPERATING DATA REPORT ~
Docket No: 50-311 Date: 11/10/94 Completed by: Mike Morroni Telephone: 339-5142 Operating Status
- 1. Unit Name Salem No. 2 Notes
- 2. Reporting Period October 1994
- 3. Licensed Thermal Power (MWt) 3411
- 4. Nameplate Rating {Gross MWe) 1170
- 5. Design Electrical Rating (Net MWe) 1115
- 6. Maximum Dependable Capacity(Gross MWe) 1149
- 7. Maximum Dependable Capacity (Net MWe) 1106
- 8. If Changes Occur in Capacity Ratings (items 3 through 7) since Last Report, Give Reason None.
- 9. Power Level to Which Restricted, if any (Net MWe) N/A
- 10. Reasons for Restrictions, if any N/A This Month Year to Date cumulative
- 11. Hours in Reporting Period 745 7296 114409
- 12. No. of Hrs. Rx. was Critical 310.7 6335.7 75615.2
- 13. Reactor Reserve Shutdown Hrs. 0 0 0
- 14. Hours Generator On-Line 303.6 6078.4 72967.9
- 15. Unit Reserve Shutdown Hours 0 0 0
- 16. Gross Thermal Energy Generated (MWH) *941985.6 18510844.8 180973784.2 Gross Elec. Energy Generated (MWH) 288670 5903490 76450008
- 18. Net Elec. Energy Gen. (MWH) 271853 5606784 72734061
- 19. Unit Service Factor 40.8 83.3 63.8
- 20. Unit Availability Factor 40.8 83.3 63.8
- 21. Unit Capacity Factor (using MDC Net) 33.0 69.5 57.5
- 22. Unit Capacity Factor (using DER Net) 32.7 68.9 57.0
- 23. Unit Forced outage Rate 2.1* 10.1 21.8
- 24. Shutdowns scheduled over next 6 months (type, date and duration of each)
We are presently in a maintenance and refueling outage scheduled to last 77 days.
- 25. If shutdown at end of Report Period, Estimated Date of startup:
December 29 1994.
- Monthly number has been adjusted to reflect a revision of Augusts monthly number and an adjustment due to feed flow nozzle inaccuracies.
8-1-7.R2
UNIT SHUTDOWN AND POWER REDUCTIONS REPORT MONTH OCTOBER 1994 DOCKET NO. 50-311 ~*
UNIT NAME Salem*#2 DATE 11-10-94 COMPLETED BY M;ke Morron; TELEPHONE: -'3=3...,9_.-5._.1-..4.._2_ __
METHOD OF SHUTTING LICENSE DURATION DOWN EVENT SYSTEM COMPONENT CAUSE AND CORRECTIVE ACTION NO. DATE TYPE 1 (HOURS) REASON 2 REACTOR REPORT # COOE 4 COOE 5 TO PREVENT RECURRENCE 1785 10/01/94 F 6.6 G 4 ---------- CD zzzzzzzzzz INADVERTANT VALVE CLOSURE 1788 10/01/94 F 23.3 A 5 ---------- CH INSTRU STEAM GEN. FEED PUMP CONTROLS 1861 10/04/94 F .8 A 5 ---------* HC PUMPXX # 24 VACUUM PUMP 1862 10/04/94 F 7.6 A 5 ----------- CH VAL VEX # 23 CN27 VALVE 1881 10/13/94 s 434.8 c 1 ----------- RC FUELXX NORMAL REFUELING 1 2 3 4 5 F: Forced Reason Method: Exhibit G - Instructions Exhibit 1 - Same S: Scheduled A-Equ;pment Fa;lure (expla;n) 1-Manual for Preparation of Data Source B-Ma;ntenance or Test 2-Manual Scram Entry Sheets for Licensee C-Refuel;ng 3-Automatic Scram Event Report CLER) File D-Requlatory Restr;ct;on 4-Continuation of (NUREG-0161)
E-Operator Tra;n;ng & L;cense Exam;nation Previous Outage F-Administrative 5-Load Reduction G-Operational Error (Explain) 9-0ther H-Other (Explain)
, 10CFR50.59 EVALUATIONS DOCKET NO: 50-311 MONTH: OCTOBER 1994 UNIT NAME: SALEM2 DATE: 11/10/94 COMPLETED BY: R. HELLER TELEPHONE: 609-339-5162 1
The following items were evaluated in accordance with the provisions of the Code of Federal Regulations 10CFR50.59. The Station Operations Review Committee has reviewed and concurs with these evaluations.
- 1. Design Change Packages (DCP) 2EE-0053, Pkgs 1-4 Service Water System Check Valve Replacements - The proposed modification entails the replacement of check valves 21SW53, 22SW77, 21SW51, 2lSW79, 22SW5, 22SW51, 22SW79, 24SW5, 22SW53 and 22SW77. The existing check valves are carbon steel rubber lined Mission Duo Check Valves, which have a history of erosion/
corrosion problems due to the rubber lining becoming separated from the valve body, allowing the valve to leak by. The replacement valves are C&S Valve Co. Dual Plate, hard seat, 6% Molybdenum stainless steel valves which have excellent corrosion/erosion resistance. In addition, the valve closure spring configuration has been redesigned to alleviate valve plate chattering due to turbulence. There is no reduction in the margin of safety as defined in the basis for any Technical Specification. (SORC 94-077) 2EE-0060, Pkg. 1 Feedwater System, Section 1 Boundary Change - Change the Section I Code boundary of the feedwater system from the BF3 Valves to the BF19 valves. This will bring the boundary in line with Section 1, Figure PG-58.3.1 "Code Jurisdictional limits for Piping Drum type Boilers", and the PSE&G commitment to the State ofNew Jersey. This change affects the non-safety related portion of the Feedwater System. It changes the boundary of the Section 1, boiler external pipe jurisdiction. It makes no other changes. There is no reduction in the margin of safety as defined in the basis for any Technical Specification.
(SORC 94-077
IOCFR50.59 EVALUATIONS DOCKET NO: 50-311 MONTH: OCTOBER 1994 UNIT NAME: SALEM 2 DATE: 11/10/94 COMPLETED BY: R. HELLER TELEPHONE: 609-339-5162 2EC-3319, Pkg. 1 Feedwater Flow Nozzle Replacement - The scope of this DCP is for the replacement of the existing feed water flow metering nozzles to improve accuracies of flow measurement and control. The new installation will utilize flanges to provide for convenient access to flow nozzles for periodic inspections. In addition, new Chordal Type Leading Edge Ultrasonic Meters will be installed upstream of the replaced flow meters to provide divers flow measurement for information purposes. There is a reactor trip system signal associated with Steam/feedwater flow Mismatch and Low Steam Generator Water Level. The feedwater flow control circuitry associated with the replacement of the flow metering nozzles is not affected by the nozzle replacement. The reactor trip setpoints were not altered by this change. There is no reduction in the margin of safety as defined in the basis for any Technical Specification.
(SORC 94-078) 2EC-3269, Pkg. 1 Auxiliary Building Ventilation System Enhancements - Rev.
1 - This DCP provides design enhancements which will increase ABV system performance and reliability and reduce auxiliary building pressure problems. The enhancements simplify the way the system operates, which will facilitate balancing and also reduce maintenance requirements. This revision to the package incorporates pressure instrumentation and partial balancing. There is no reduction in the margin of safety as defined in the basis for any Technical Specification. (SORC 94-080) 2EC-3228, Pkg. 2 Waste Gas Analyzer Panel Replacement - This package installs one new gas analyzer panel, 110-2, on elevation 122' of the Unit 2 Auxiliary Building. The panel consists of two (2) hydrogen analyzers, one (1) recorder, sample selection sequencing logic, alarm unit, flow instrumentation,
... ' 10CFR50.59 EVALUATIONS DOCKET NO: 50-311 MONTH: OCTOBER 1994 UNIT NAME: SALEM 2 DATE: 11/10/94 COMPLETED BY: R. HELLER TELEPHONE: 609-339-5162 sample pumps, tubing and valving. One set of 02 and H 2 analyzers in the panel will continuously monitor the in-service waste gas decay tank (WGDT). The second set of analyzers will normally monitor the cover gasses in sequential manner. Under administrative control, the sequential monitoring is also capable of including the in-service WGDT for both Units and the tank cover gasses from Unit 1. The proposed change does not reduce the margin of safety as defined as defined in the basis of the Technical Specifications. The proposed changes will not increase the risk of explosivity and do not have effect on monitoring of gaseous efiluents. Since no system having a safety function i_s affected by the modification, the margin of safety is not reduced. (SORC 94-080) 2EE-0065, Pkg. 1 22SJ145 Replacement - Valve 22SJ145 will be replaced with an equivalent valve. there is no anticipated impact from this change. The valve serves as a test connection for the Safety Injection hot leg to the RCS and is adjacent to valve 22SJ40, which is the containment isolation boundary valve. The margin of safety of the service water system is defined, in part, by the requirements set forth by ASME I design code. The design requirements for the proposed modification have been satisfied. The function of the 22SJ145 globe valve/safety injection system has not changed. The margin of safety as defined by Technical Specifications is therefore, unaffected.* (SORC 94-081) 2EE-0063, Pkg. 1 No. 26 Service Water Pump Discharge Check Valve 26SW2 Replacement - The proposed modification entails the replacement of No. 26 Service Water Pump discharge check valve 26SW2. The existing check valve is a C&S
- Valve Co. Dual Plate, soft seat, aluminum bronze valve, which had a history of erosion problems due to the soft seat becoming separated from the valve body and allowing the valve to leak by. The replacement valve is C&S Valve Co.
... ...11., y 10CFR50.59 EVALUATIONS DOCKET NO: 50-311 MONTH: OCTOBER 1994 UNIT NAME: SALEM 2 DATE: 11/10/94 COMPLETED BY: R. HELLER TELEPHONE: 609-339-5162 (Cont'd)
Dual Plate, hard seat, 6% Molybdenum Stainless Steel valve, which has excellent erosion/corrosion characteristics.
The seat material for the new valve is the same as the valve body and should exhibit the same excellent erosion/
corrosion characteristics. The replacement valve is dimensionally the same, no modifications to the piping system are required. There is no reduction in the margin of safety as defined in the basis for any Technical Specification.
(SORC 94-080)
~ ( ' i.:.
SALEM GENERATING STATION MONTHLY OPERATING
SUMMARY
- UNIT 2 OCTOBER 1994 SALEM UNIT NO. 2 The Unit began the period ma power escalat10n fotiowing a manual trip on September 29, 1994. On October 4, 1994, power was briefly reduced to 87% due to problems with #24 Vacuum Pump. The Unit was returned to 100% power, and continued to operate at full power until October 13, 1994, when a 5% per hour power reduction was commenced to take the Unit off line for the 2R8 refueling outage. The Unit remained shutdown throughout the rest of the period while outage activities continued.
... .i.-. , )*
REFUELING INFORMATION DOCKET NO: 50-311 MONTH: OCTOBER 1994 UNIT NAME: SALEM2 DATE: 11/10/94 CO:MJ>LETED BY: R. HELLER TELEPHONE: 609-339-5162 MONTH: OCTOBER 1994
- 1. Refueling information ha~ changed from last month: YES____A_NO _ _
- 2. Scheduled date for next refueling: October 14. 1994
- 3. Scheduled date for restart following refueling: December 29. 1994
- 4. a. Will Technical Specification changes or other license amendments be required?
YES NO NOT DETERMINED TO DATE __A_
- b. Has the reload fuel design been reviewed by the Station Operating Review Committee?
YES NO ____A_
Ifno, when is it scheduled? November
- 5. Scheduled date(s) for submitting proposed licensing action: ---~N/A._ _ __
- 6. Important licensing considerations associated with refueling:
- 7. Number ofFuel Assemblies:
- a. Incore 0
- b. In Spent Fuel Storage 749
- 8. Present licensed spent fuel storage capacity: _1170_ _
Future spent fuel storage capacity: 1170
- 9. Date oflast refueling that can be discharged to the spent fuel pool assuming the present licensed capacity: March 2003 8-1-7.R4