ML18100A730

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Forwards Insp Repts 50-272/93-82 & 50-311/93-82 on 930816-0903 & Notices of Violation & Deviation
ML18100A730
Person / Time
Site: Salem  
Issue date: 11/30/1993
From: Hodges M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To: Miltenberger S
Public Service Enterprise Group
Shared Package
ML18100A731 List:
References
NUDOCS 9312070042
Download: ML18100A730 (3)


See also: IR 05000272/1993082

Text

Docket Nos. 50-272

50-311

Mr. Steven E. Miltenberger

NOV 3 0 1993

Vice President and Chief Nuclear Officer

Public Service Electric and Gas Company

P. 0. Box 236

Hancocks Bridge, New Jersey 08038

Dear Mr. Miltenberger:

SUBJECT:

NOTICE OF VIOLATION

NRC COMBINED INSPECTION REPORT NOS. 50-272/93-82; 50-311/93-82

This refers to the announced electrical distribution system functional inspection (EDSFI:{

conducted by Mr. Leonard Cheung of this office from August 16 to September 3, 1993. The

inspection included a review of activities authorized for Salem Units 1 and 2. At the

conclusion of the inspection, the findings were discussed with those members of your staff

identified in the enclosed report. Additionally, the status of the inspection findings was

discussed with Messrs. M. Burnstein and B. Thomas of your staff during subsequent

telephone conversations on September 29, 1993, and October 27, 1993.

This inspection was directed toward areas important to public health and safety. The purpose

of this inspection was to determine whether the electrical distribution system as designed,

installed, and configured at Salem Units 1 and 2 is capable of performing its intended safety

functions. In addition, this inspection also included a review of your self-assessment of the

electrical distribution system and a review of the August 19, 1993, event involving a battery

cell voltage dropping below the technical specification limit.

The team determined that your self-assessment was adequate, although some weaknesses

were identified as discussed in the attached inspection report. In addition, based on the

team's independent review of selected electrical and mechanical design areas, and

. maintenance and test areas, we determined that, in general, your electrical distribution

system is capable of performing its intended function.

Based upon the results of this inspection, one of your activities appeared to be in violation of

NRC requirements, as indicated in the Notice of Violation enclosed as Appendix A. This

violation involved failure to follow station procedures as a result of your staff's action in

response to the August 19, 1993, event. In addition, two of your activities appeared to

deviate from the Salem updated final safety analysis report, as indicated in the Notice of

Deviation enclosed as Appendix B. One of these deviations pertains to emergency diesel

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NOV 3 0 1993

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generator (EDG) equipment protection against a tornado-generated missile. This deviation

applies to Salem Unit 2 only. The other deviation, which relates to EDG fuel supplies, was

originally identified by your self- assessment EDSFI team. Corrective actions for this issue

were not implemented because your staff took credit for the nonsafety-related fuel oil storage

tank. You are required to respond to the Notice of Violation and the Notice of Deviation.

In preparing your response, you* should follow the instructions provided in Appendices A

and B.

In addition, 13 unresolved items and two observations were identified as listed in the

Executive Summary of the inspection report. *We request that you provide to us, in writing,

within 60 days of receipt of this letter, a schedule for the resolution of the 13 unresolved

items.

In accordance with 10 CFR 2. 790 of the NRC's "Rules of Practice," a copy of this letter and

its enclosure will be placed in the NRC Public Document Room.

The responses directed by this letter and the enclosed Notice are not subject to the clearance

procedures of the Office of Management and Budget as required by the Paperwork Reduction

Act of 1980, Pub. L.96-511.

Your cooperation with us in this matter is appreciated.

Sincerely,

~t::ef:.t:

Division of Reactor Safety

Enclosures:

1. Notice of Violation

2. Notice of Deviation

3. 50-272/93-82; 50-311193-82

Public Service Electric

and Gas Company

cc w/encls:

NOV 3 0 1993

3

J. J. Hagan, Vice President, Nuclear Operations

C. Schaefer, External Operations - Nuclear, Delmarva Power & Light Co.

C. Vondra, General Manager - Salem Operations

R. Hovey, General Manager - Hope Creek Operations

F. Thomson, Manager, Licensirig and Regulation

R. Swanson, General Manager - QA and Nuclear Safety Review.

J. Robb, Director, Joint Owner Affairs

A. Tapert, Program Administrator

R. Fryling, Jr., Esquire*

M. Wetterhahn, Esquire

P. J. Curham, Manager, Joint Generation Department,

Atlantic Electric Company

Consumer Advocate, Office of Consumer Advocate

William Conklin, Public Safety Consultant, Lower Alloways Creek Township

K. Abraham, PAO (2)

Public Document Room (PDR)

Local Public Document Room (LPDR)

Nuclear Safety Information Center (NSIC)

NRC Resident Inspector

State of New Jersey

bee w/encls:

Region I Docket Room (with concurrences)

H. Leung, Electrical Engineer, AECL, Canada

M. Schlyamberg, Mechanical Engineer

D. Vito (RI-93-A-0177)

bee w/encls: (Via E-Mail)

J. Stone, NRR

S. Dembek, NRR

V. McCree, OEDO

M. Boyle, Acting PDI-2, NRR

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