Similar Documents at Salem |
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Category:OPERATING LICENSES-APPLIATION TO AMEND-RENEW EXISTING
MONTHYEARML18107A4991999-08-25025 August 1999 Application for Amends to Licenses DPR-70 & DPR-75,proposing to Authorize Licensee to Perform Single Cell Charging of Connected Cells in Operable Class 1E Batteries ML18107A5141999-08-25025 August 1999 Suppl to 971114 Application for Amends to Licenses DPR-70 & DPR-75,deleting Footnotes Added as one-time Changes & Proposing Change Identified Subsequent to 971114 Submittal That Corrects Error Issued in Amend 69 for Unit 2 ML18107A4631999-07-29029 July 1999 Application for Amends to Licenses DPR-70 & DPR-75,replacing Surveillance 4.6.1.1a with Appropriate NUREG-1431 Requirements ML18107A4581999-07-23023 July 1999 Application for Amends to Licenses DPR-70 & DPR-75 to Change TS Surveillance Requirement 4.8.1.1.2 D 7 by Removing Restriction to Perform Test Every 18 Months During Shutdown ML18107A4221999-07-0202 July 1999 Application for Amends to Licenses DPR-70 & DPR-75 to Relocate TS 3/4.3.4 Lco,Surveillance Requirements & Bases from TS to Ufsar,Iaw GL 95-10 ML18107A3771999-06-10010 June 1999 Application for Amends to Licenses DPR-70 & DPR-75,modifying TS 3/4.6.1, Containment Integrity, by Clarifying When Verification of Primary Containment Integrity May Be Performed by Administrative Means ML18107A3571999-06-0404 June 1999 Application for Amends to Licenses DPR-70,DPR-75 & NPF-57 Re Transfer of PSEG Ownership Interests & Licensed Operating Authorities to New,Affiliated Nuclear Generating Company, PSEG Nuclear Llc.Proprietary Encls Withheld ML18107A2081999-04-14014 April 1999 Application for Amends to Licenses DPR-70 & DPR-75,revising TS 3/4.9.12, Fhvas, to Ensure Consistency Between TS Requirements for Fhavs & Sys Design Basis,Per NUREG-1431. Page 4 of 4 in Attachment 2 of Incoming Submittal Omitted ML18106B1571999-03-31031 March 1999 Suppl to 990115 Application for Amend to License DPR-70, Allowing Plant Operation to Continue to Thirteenth Refueling Outage (1R13),currently Scheduled to Begin on 990918 ML18106B0621999-02-0808 February 1999 Application for Amends to Licenses DPR-70 & DPR-75, Respectively.Proposed Amend Modifies ECCS Subsystems Surveillance Requirement 4.5.3.2.b by Adding Option of Providing Necessary Isolation Function When Testing ML18106B0501999-02-0202 February 1999 Application for Amends to Licenses DPR-70 & DPR-75,revising Max Permissible Enrichment of Stored New Fuel Described in TS Section 5.6.1.1.Rept Entitled, Criticality Analysis of Salem Units 1 & 2 Fresh Fuel Racks, Encl ML18106B0221999-01-15015 January 1999 Application for Amend to License DPR-70,proposing one-time Changes to Certain Unit 1 TS Surveillance Requirements for Fuel Cycle 13,currently Scheduled to Begin on 990918 ML18106A9161998-10-12012 October 1998 Application for Amend to License DPR-75,requesting one-time Changes to Certain Unit 2 TS SR for Fuel Cycle 10.Basis for Requested Changes,Analysis Supporting No Significant Hazards Determination & Marked Up TS Pages,Encl ML18106A8921998-09-29029 September 1998 Application for Amends to Licenses DPR-72 & DPR-75,modifying TS 3/4.9.4 to Permit Use of Equivalent Methods to Obtain Containment Closure During Refueling Operations for Containment Equipment Hatch ML18106A8761998-09-17017 September 1998 Application for Amends to Licenses DPR-70 & DPR-75,modifying TSs 3/4.8.2.2,3/4.8.2.4 & 3/4.8.2.6 to Address Movement of Irradiated Fuel & Deleting LCO Re Requirement to Establish Containment Integrity ML18106A8351998-08-12012 August 1998 Application for Amends to Licenses DPR-70 & DPR-75,modifying TS for Containment Air Locks for Salem Units 1 & 2 ML18106A7911998-07-30030 July 1998 Application for Amends to Licenses DPR-70 & DPR-75,revising Acceptance Criteria for CR Emergency Air Conditioning Sys from Maintaining CR at 1/8-inch Positive Pressure W/Respect to Adjacent Areas to Following Phrase ML18106A4271998-03-26026 March 1998 Application for Amend to License DPR-70,changing Applicability Statement from Mode 3 to Modes 1 & 2 ML18106A4221998-03-26026 March 1998 Application for Amends to Licenses DPR-70 & DPR-75, Respectively,Incorporating Note at Bottom of Salem Unit 2 T3/4.8.2 Into Salem 1 TS & Adding Asterisks to Word Inverters. ML18106A2521998-01-0808 January 1998 Supplemental Application for Amends to Licenses DPR-70 & DPR-75,respectively Adding Asterisk to Word Operable in LCO & Associated Note at Bottom of Page ML18106A2111997-12-15015 December 1997 Application for Amends to Licenses DPR-70 & DPR-75,revising TS to Adopt Option B of 10CFR50,App J,For Type B & C Testing & Modifying Existing TS Wording for Previous Adoption of Option B on Type a Testing ML18106A1941997-12-11011 December 1997 Application for Amend to License DPR-70,requesting one-time Exemption to Allow Containment Purging in Modes 3 & 4 ML18102B6771997-11-14014 November 1997 Application for Amends to Licenses DPR-70 & DPR-75,providing TS Surveillance Requirements to Codify Existing Procedural Commitments for SW Accumulator Vessels ML18102B6731997-11-14014 November 1997 Application for Amends to Licenses DPR-70 & DPR-75, Correcting Editorial & Administrative Errors in Ts,Which Existed Since Initial Issuance ML18102B6611997-11-0404 November 1997 Application for Amends to Licenses DPR-70 & DPR-75,revising TS 3/4.8.1 Re EDG & Deleting SR 4.8.1.1.2.d.1,calling for Diesels to Be Subjected to Insp Based on Vendor Recommendations ML18102B6571997-11-0404 November 1997 Application for Amends to Licenses DPR-70 & DPR-75,revising Surveillance Requirement 4.6.2.1.b to Verify That on Recirculation Flow,Containment Spray Pumps Develop Differential Pressure of Greater than or Equal to 204 Psid ML18102B6371997-10-29029 October 1997 Application for Amend to License DPR-75,revising TS 3/4.4.6, Steam Generators, Making One Time Change to Unit 2 SG Insp Schedule to Require Next Insp within 24 Months of Mode 2 for Unit 2 Fuel Cycle 10 ML18102B6411997-10-29029 October 1997 Application for Amends to Licenses DPR-70 & DPR-75,revising SR 4.8.1.1.2.d.2 Proposed in Util 960925 Submittal Re EDG Testing ML18102B6471997-10-24024 October 1997 Application for Amends to Licenses DPR-70 & DPR-75,modifying TS 3/4.7.7, Auxiliary Building Exhaust Air Filtration Sys & Bases ML18102B6441997-10-24024 October 1997 Application for Amends to Licenses DPR-70 & DPR-75,revising Containment Hydrogen Analyzer SRs of TS 4.6.4.1 ML18102B6291997-10-21021 October 1997 Application for Amends to Licenses DPR-70 & DPR-75,extending Applicability of Power Range Neutron Flux TS Trip to Require Operability & Surveillance Testing in Mode 3,when Reactor Trip Sys Breakers in Closed Position ML18102B6181997-10-14014 October 1997 Application for Amend to License DPR-70,modifying Pressure Isolation Valve Lco,Lco Action Statement,Surveillance Requirement & Table 4.4-4 to Be Consistent W/Salem Unit 2 ML18102B6061997-10-0606 October 1997 Application for Amend to License DPR-70,changing TS for LCOs 3.1.3.1, Movable Control Assemblies & 3.1.3.2.1, Position Indication Sys. ML18102B5551997-08-27027 August 1997 Application for Amends to Licenses DPR-70 & DPR-75,providing Revised TS Bases Pages for TS 3.7.3, CCW Sys, to State That CCW Pumps Required to Be Operable to Meet LCO ML18102B5281997-08-19019 August 1997 Application for Amend to License DPR-75,providing Addl Operational Flexibility to Allow Orderly Resumption of Startup & Preclude Unwarranted Power Transients at Plant Unit 2 ML18102B5321997-08-18018 August 1997 Application for Amend to License DPR-75,incorporating Plant Computer (P-250) Into TS Bases for Movable Control Assemblies ML18102B4871997-08-0101 August 1997 Application for Amends to Licenses DPR-70 & DPR-75,rewording TS Section 4.2.1 to State That Util Will Adhere to Section 7 Incidental Take Statement Approved by Natl Marine Fisheries Svc ML18102B3041997-05-14014 May 1997 Application for Amends to Licenses DPR-70 & DPR-75,revising SR 4.7.6.1.d.1 to Indicate That Specified Acceptable Filter Dp Is to Be Measured Across Filter Housing & to Reflecting Filter Dp Acceptance Value of Greater than 2.70 Wg ML18102B2611997-05-0101 May 1997 Suppl Info to Util 970211 Application for Amends to Licenses DPR-70 & DPR-75,revising TS for Chilled Water Sys - Auxiliary Bldg Subsystem.Ref to Radiation Monitoring Signal Removed from Bases Section ML18102B2581997-05-0101 May 1997 Application for Amend to License DPR-75,revising TS Section 3/4.7.7 to Reflect Extended Allowed Outage Times & Creating New TS Section 3/4.7.11 to Address Importance of Switchgear & Penetration Area Ventilation Sys ML18102B0071997-04-30030 April 1997 Application for Amends to Licenses DPR-40,DPR-56,DPR-70 & DPR-75,requesting Consent of NRC for Indirect Transfer of Control of Interest in Plants That Will Occur Under Proposed Merger ML18102B2511997-04-28028 April 1997 Submits Suppl to 970131 & 0314 Applications for Amends to Licenses DPR-70 & DPR-75,revising TS on Pressurizer Power Operated Relief Valves.Suppl Issued to State That Conclusion of NSHC Remains Valid ML18102B0221997-04-25025 April 1997 Application for Amends to Licenses DPR-70 & DPR-75, Eliminating Flow Path from RHR Sys to RCS Hot Legs as Specified in LCO 3.5.2.c.2 ML18102A9791997-04-11011 April 1997 Application for Amends to Licenses DPR-70 & DPR-75, Increasing Cw Flow to 2550 Gpm for 31 Day Surveillance Fans Started & Operated in Low Speed ML18102A8951997-03-0404 March 1997 Application for Amends to Licenses DPR-70 & DPR-75,modifying ECCS Surveillance Test Acceptance Criteria for Centrifugal Charging & SI Pumps ML18102A8491997-02-11011 February 1997 Application for Amends to Licenses DPR-70 & DPR-75, Requesting Addition of New TS 3/4.7.10, Chilled Water Sys ML18102A8361997-01-31031 January 1997 Application for Amends to Licenses DPR-70 & DPR-75,revising TS 3/4.4.3 to Ensure That Automatic Capability of Power Operated Relief Valve to Relieve Pressure Is Maintained When Valves Are Isolated by Closure of Block Valves ML18102A8021997-01-31031 January 1997 Application for Amends to Licenses DPR-70 & DPR-75, Requesting Rev to TS Re Containment Systems Air Temp to Ensure Representative Average Air Temp Is Measured ML18102A7861997-01-23023 January 1997 Application for Amend to License DPR-75,revising TS Bases 3/4.3.3.1 Re Radiation Monitoring Instrumentation Channel 2R41 ML18102A7361997-01-0707 January 1997 Application for Amends to Licenses DPR-70 & DPR-75,revising Eighteen Month Surveillance Performed to Measure RCS Total Flow Rate to Account for Necessary Plant Conditions for Performing Test in Mode 1 & Current Extended Plant Outages 1999-08-25
[Table view] Category:TEXT-LICENSE APPLICATIONS & PERMITS
MONTHYEARML18107A4991999-08-25025 August 1999 Application for Amends to Licenses DPR-70 & DPR-75,proposing to Authorize Licensee to Perform Single Cell Charging of Connected Cells in Operable Class 1E Batteries ML18107A5141999-08-25025 August 1999 Suppl to 971114 Application for Amends to Licenses DPR-70 & DPR-75,deleting Footnotes Added as one-time Changes & Proposing Change Identified Subsequent to 971114 Submittal That Corrects Error Issued in Amend 69 for Unit 2 ML18107A4631999-07-29029 July 1999 Application for Amends to Licenses DPR-70 & DPR-75,replacing Surveillance 4.6.1.1a with Appropriate NUREG-1431 Requirements ML18107A4581999-07-23023 July 1999 Application for Amends to Licenses DPR-70 & DPR-75 to Change TS Surveillance Requirement 4.8.1.1.2 D 7 by Removing Restriction to Perform Test Every 18 Months During Shutdown ML18107A4221999-07-0202 July 1999 Application for Amends to Licenses DPR-70 & DPR-75 to Relocate TS 3/4.3.4 Lco,Surveillance Requirements & Bases from TS to Ufsar,Iaw GL 95-10 ML18107A3771999-06-10010 June 1999 Application for Amends to Licenses DPR-70 & DPR-75,modifying TS 3/4.6.1, Containment Integrity, by Clarifying When Verification of Primary Containment Integrity May Be Performed by Administrative Means ML18107A3571999-06-0404 June 1999 Application for Amends to Licenses DPR-70,DPR-75 & NPF-57 Re Transfer of PSEG Ownership Interests & Licensed Operating Authorities to New,Affiliated Nuclear Generating Company, PSEG Nuclear Llc.Proprietary Encls Withheld ML18107A2081999-04-14014 April 1999 Application for Amends to Licenses DPR-70 & DPR-75,revising TS 3/4.9.12, Fhvas, to Ensure Consistency Between TS Requirements for Fhavs & Sys Design Basis,Per NUREG-1431. Page 4 of 4 in Attachment 2 of Incoming Submittal Omitted ML18106B1571999-03-31031 March 1999 Suppl to 990115 Application for Amend to License DPR-70, Allowing Plant Operation to Continue to Thirteenth Refueling Outage (1R13),currently Scheduled to Begin on 990918 ML18106B0621999-02-0808 February 1999 Application for Amends to Licenses DPR-70 & DPR-75, Respectively.Proposed Amend Modifies ECCS Subsystems Surveillance Requirement 4.5.3.2.b by Adding Option of Providing Necessary Isolation Function When Testing ML18106B0501999-02-0202 February 1999 Application for Amends to Licenses DPR-70 & DPR-75,revising Max Permissible Enrichment of Stored New Fuel Described in TS Section 5.6.1.1.Rept Entitled, Criticality Analysis of Salem Units 1 & 2 Fresh Fuel Racks, Encl ML18106B0221999-01-15015 January 1999 Application for Amend to License DPR-70,proposing one-time Changes to Certain Unit 1 TS Surveillance Requirements for Fuel Cycle 13,currently Scheduled to Begin on 990918 ML18106A9161998-10-12012 October 1998 Application for Amend to License DPR-75,requesting one-time Changes to Certain Unit 2 TS SR for Fuel Cycle 10.Basis for Requested Changes,Analysis Supporting No Significant Hazards Determination & Marked Up TS Pages,Encl ML18106A8921998-09-29029 September 1998 Application for Amends to Licenses DPR-72 & DPR-75,modifying TS 3/4.9.4 to Permit Use of Equivalent Methods to Obtain Containment Closure During Refueling Operations for Containment Equipment Hatch ML18106A8761998-09-17017 September 1998 Application for Amends to Licenses DPR-70 & DPR-75,modifying TSs 3/4.8.2.2,3/4.8.2.4 & 3/4.8.2.6 to Address Movement of Irradiated Fuel & Deleting LCO Re Requirement to Establish Containment Integrity ML18106A8351998-08-12012 August 1998 Application for Amends to Licenses DPR-70 & DPR-75,modifying TS for Containment Air Locks for Salem Units 1 & 2 ML18106A7911998-07-30030 July 1998 Application for Amends to Licenses DPR-70 & DPR-75,revising Acceptance Criteria for CR Emergency Air Conditioning Sys from Maintaining CR at 1/8-inch Positive Pressure W/Respect to Adjacent Areas to Following Phrase ML18106A4271998-03-26026 March 1998 Application for Amend to License DPR-70,changing Applicability Statement from Mode 3 to Modes 1 & 2 ML18106A4221998-03-26026 March 1998 Application for Amends to Licenses DPR-70 & DPR-75, Respectively,Incorporating Note at Bottom of Salem Unit 2 T3/4.8.2 Into Salem 1 TS & Adding Asterisks to Word Inverters. ML18106A2521998-01-0808 January 1998 Supplemental Application for Amends to Licenses DPR-70 & DPR-75,respectively Adding Asterisk to Word Operable in LCO & Associated Note at Bottom of Page ML18106A2111997-12-15015 December 1997 Application for Amends to Licenses DPR-70 & DPR-75,revising TS to Adopt Option B of 10CFR50,App J,For Type B & C Testing & Modifying Existing TS Wording for Previous Adoption of Option B on Type a Testing ML18106A1941997-12-11011 December 1997 Application for Amend to License DPR-70,requesting one-time Exemption to Allow Containment Purging in Modes 3 & 4 ML18102B6771997-11-14014 November 1997 Application for Amends to Licenses DPR-70 & DPR-75,providing TS Surveillance Requirements to Codify Existing Procedural Commitments for SW Accumulator Vessels ML18102B6731997-11-14014 November 1997 Application for Amends to Licenses DPR-70 & DPR-75, Correcting Editorial & Administrative Errors in Ts,Which Existed Since Initial Issuance ML18102B6611997-11-0404 November 1997 Application for Amends to Licenses DPR-70 & DPR-75,revising TS 3/4.8.1 Re EDG & Deleting SR 4.8.1.1.2.d.1,calling for Diesels to Be Subjected to Insp Based on Vendor Recommendations ML18102B6571997-11-0404 November 1997 Application for Amends to Licenses DPR-70 & DPR-75,revising Surveillance Requirement 4.6.2.1.b to Verify That on Recirculation Flow,Containment Spray Pumps Develop Differential Pressure of Greater than or Equal to 204 Psid ML18102B6371997-10-29029 October 1997 Application for Amend to License DPR-75,revising TS 3/4.4.6, Steam Generators, Making One Time Change to Unit 2 SG Insp Schedule to Require Next Insp within 24 Months of Mode 2 for Unit 2 Fuel Cycle 10 ML18102B6411997-10-29029 October 1997 Application for Amends to Licenses DPR-70 & DPR-75,revising SR 4.8.1.1.2.d.2 Proposed in Util 960925 Submittal Re EDG Testing ML18102B6471997-10-24024 October 1997 Application for Amends to Licenses DPR-70 & DPR-75,modifying TS 3/4.7.7, Auxiliary Building Exhaust Air Filtration Sys & Bases ML18102B6441997-10-24024 October 1997 Application for Amends to Licenses DPR-70 & DPR-75,revising Containment Hydrogen Analyzer SRs of TS 4.6.4.1 ML18102B6291997-10-21021 October 1997 Application for Amends to Licenses DPR-70 & DPR-75,extending Applicability of Power Range Neutron Flux TS Trip to Require Operability & Surveillance Testing in Mode 3,when Reactor Trip Sys Breakers in Closed Position ML18102B6181997-10-14014 October 1997 Application for Amend to License DPR-70,modifying Pressure Isolation Valve Lco,Lco Action Statement,Surveillance Requirement & Table 4.4-4 to Be Consistent W/Salem Unit 2 ML18102B6061997-10-0606 October 1997 Application for Amend to License DPR-70,changing TS for LCOs 3.1.3.1, Movable Control Assemblies & 3.1.3.2.1, Position Indication Sys. ML18102B5551997-08-27027 August 1997 Application for Amends to Licenses DPR-70 & DPR-75,providing Revised TS Bases Pages for TS 3.7.3, CCW Sys, to State That CCW Pumps Required to Be Operable to Meet LCO ML18102B5281997-08-19019 August 1997 Application for Amend to License DPR-75,providing Addl Operational Flexibility to Allow Orderly Resumption of Startup & Preclude Unwarranted Power Transients at Plant Unit 2 ML18102B5321997-08-18018 August 1997 Application for Amend to License DPR-75,incorporating Plant Computer (P-250) Into TS Bases for Movable Control Assemblies ML18102B4871997-08-0101 August 1997 Application for Amends to Licenses DPR-70 & DPR-75,rewording TS Section 4.2.1 to State That Util Will Adhere to Section 7 Incidental Take Statement Approved by Natl Marine Fisheries Svc ML20148K0841997-06-0404 June 1997 Amends 194 & 177 to Licenses DPR-70 & DPR-75,respectively, Changing TSs 3.4.3 & 3.4.5, Relief Valves, to Ensure That Automatic Capability of PORVs to Relieve Pressure Is Maintained When Valves Are Isolated ML18102B3041997-05-14014 May 1997 Application for Amends to Licenses DPR-70 & DPR-75,revising SR 4.7.6.1.d.1 to Indicate That Specified Acceptable Filter Dp Is to Be Measured Across Filter Housing & to Reflecting Filter Dp Acceptance Value of Greater than 2.70 Wg ML18102B2611997-05-0101 May 1997 Suppl Info to Util 970211 Application for Amends to Licenses DPR-70 & DPR-75,revising TS for Chilled Water Sys - Auxiliary Bldg Subsystem.Ref to Radiation Monitoring Signal Removed from Bases Section ML18102B2581997-05-0101 May 1997 Application for Amend to License DPR-75,revising TS Section 3/4.7.7 to Reflect Extended Allowed Outage Times & Creating New TS Section 3/4.7.11 to Address Importance of Switchgear & Penetration Area Ventilation Sys ML18102B0071997-04-30030 April 1997 Application for Amends to Licenses DPR-40,DPR-56,DPR-70 & DPR-75,requesting Consent of NRC for Indirect Transfer of Control of Interest in Plants That Will Occur Under Proposed Merger ML18102B2511997-04-28028 April 1997 Submits Suppl to 970131 & 0314 Applications for Amends to Licenses DPR-70 & DPR-75,revising TS on Pressurizer Power Operated Relief Valves.Suppl Issued to State That Conclusion of NSHC Remains Valid ML18102B0221997-04-25025 April 1997 Application for Amends to Licenses DPR-70 & DPR-75, Eliminating Flow Path from RHR Sys to RCS Hot Legs as Specified in LCO 3.5.2.c.2 ML18102A9791997-04-11011 April 1997 Application for Amends to Licenses DPR-70 & DPR-75, Increasing Cw Flow to 2550 Gpm for 31 Day Surveillance Fans Started & Operated in Low Speed ML18102A8951997-03-0404 March 1997 Application for Amends to Licenses DPR-70 & DPR-75,modifying ECCS Surveillance Test Acceptance Criteria for Centrifugal Charging & SI Pumps ML18102A8491997-02-11011 February 1997 Application for Amends to Licenses DPR-70 & DPR-75, Requesting Addition of New TS 3/4.7.10, Chilled Water Sys ML18102A8361997-01-31031 January 1997 Application for Amends to Licenses DPR-70 & DPR-75,revising TS 3/4.4.3 to Ensure That Automatic Capability of Power Operated Relief Valve to Relieve Pressure Is Maintained When Valves Are Isolated by Closure of Block Valves ML18102A8021997-01-31031 January 1997 Application for Amends to Licenses DPR-70 & DPR-75, Requesting Rev to TS Re Containment Systems Air Temp to Ensure Representative Average Air Temp Is Measured ML18102A7861997-01-23023 January 1997 Application for Amend to License DPR-75,revising TS Bases 3/4.3.3.1 Re Radiation Monitoring Instrumentation Channel 2R41 1999-08-25
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Public Service Electric and Gas Company Joseph J. Hagan Public Service Electric and Gas Company P.O. Box 236, Hancocks Bridge, NJ 08038 609-339-1200 Vice President - Nuclear Operations JUN 111993 NLR-N93077 LCR 93-17 United States Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Gentlemen:
REQUEST FOR AMENDMENT BORON CONCENTRATION REDUCTION SALEM GENERATING STATION I UNIT NOS. 1 AND 2 I~
FACILITY OPERATING LICENSES NOS. DPR-70 AND DPR-75 !
DOCKET NOS. 50-272 AND 50-311 In accordance with the requirements of 10CFR50.90, Public Service Electric and Gas Company (PSE&G) hereby transmits a request for amendment of Facility Operating Licenses DPR-70 and DPR-75 for Salem Generating Station, Units Nos., 1 and 2, respectively. In accordance with 10CFR50.91 (b) (1) requirements, a copy of this request for amendment has been sent to the State of New Jersey.
The proposed amendment reduces the boron concentration in the boric acid tank from 12 percent by weight to between 3.75 and 4.0 percent by weight. The reduced boron concentration results in eliminating the need for heat tracing. With the lower temperature and lower boron concentration, reliability and availability of -
the boric acid system will be significantly improved.
A description of the requested amendment, supporting information and analyses for the change, and the basis for a no significant hazards consideration determination are provided in Attachment 1.
The Technical Specification pages affected by the proposed change are marked-up in Attachment 2. A detail technical bases and operational analysis CEN-606 is in Attachment 3.
l?OCGG
Document Control Desk JUN 11 1993 NLR-N93077 Upon NRC approval of this proposed change, PSE&G requests that the amendment.be made effective on the date of issuance, but implemented prior to mode 4 following the eleventh refueling outage for Unit 1, and following the eighth refueling cycle for Unit 2. Please note that the proposed TS change is similar to that approved for Turkey Point Nuclear Plant on July 16, 1991 and posted for Sequoyah Nuclear Plant on May 12, 1993.
Should you have any questions regarding this request, we will be pleased to* discuss them with you.
Sincerely, Attachments (3) c Mr. T. T. Martin, Administrator - Region I
- u. s. Nuclear Regulatory Commission 475 Allendale Road King of Prussia, PA 19406 Mr. J. C. Stone, Licensing Project Manager
- u. s. Nuclear Regulatory Commission One White Flint North 11555 Rockville Pike Rockville, MD 20852 Mr. T. P. Johnson (S09)
USNRC Senior Resident Inspector Mr. K. Tosch, Manager, IV NJ Dept. of Environmental Protection Division of Environmental Quality Bureau of Nuclear Engineering CN 415 Trenton, NJ 08625 t
l
REF: NLR-N93077 STATE OF NEW JERSEY
) SS.
COUNTY OF SALEM )
J. J. Hagan, being duly sworn according to law deposes and says:
I am Vice President - Nuclear Operations of Public Service Electric and Gas Company, and as such, I find the matters set forth in the above referenced letter, concerning the Salem Generating Station, Unit Nos. 1 and 2, are true to the best of my knowledge, information and belief.
this day of111 Subscribed and Sworn to before me L/ i. "- l)'L._ ; 1993
~~1#~#--
Notary PUbli~New Jersey KIMBERLY JO BROWN NOTARY PUBLIC OF NEW JERSEY Mv Commission Expires April 21, 1998 My Commission expires on
NLR-N93077 1 LCR 93-17 ATTACHMENT 1 PROPOSED CHANGES TO TECHNICAL SPECIFICATIONS LICENSE AMENDMENT APPLICATION BORON CONCENTRATION REDUCTION FACILITY OPERATING LICENSES DPR-70 AND DPR-75 DOCKET NOS. 50-272 AND 50-311 I. Description of Change Technical Specification (TS) 3.1.1.1 action statement will be revised to increase the flow rate from 10 gallons per minute (gpm) to 33 gpm and to decrease the boron concentration from 20,000 parts per million (ppm) to ~6,560 ppm.
TS 3.1.1.2 action statement will be revised to increase the flow rate from 10 gpm to 33 gpm and decrease the boron concentration from 20,000-ppm boron to ~6,560-ppm boron.
TS 3.1.2.1 surveillance Requirements (SR) 4.1.2.1.a will be revised to include the required temperature monitoring for the boric acid flow path components and delete the heat trace requirement. The.monitoring temperature will be lowered from ~145°F to ~63°F for* boric acid tank and ~50°F for the pipe from recirculation line to the charging pump suction line.
TS 3.1.2.2 SR 4.1.2.2.a will be revised to include the required temperature monitoring for the boric acid flow path components and delete the heat trace requirements. The monitoring temperature will be lowered from ~145°F to ~63°F for boric acid tank and ~50°F for the pipe from recirculation line to the charging pump suction line.
TS 3.1.2.2 SR 4.1.2.2.d will be added for unit-1 only, to verify the operability of the flow path required by specification 3.1.2.2.a delivers at least 33 gpm to the Reactor Coolant System. TS 3.1.2.2 SR 4.1.2.2.d. (unit-2) will be revised to increase the flow rate from 10 gpm to 33 gpm.
TS 3.1.2.7.a (3.1.2.5.a Unit-2) will be revised to delete the heat trace requirement. Part 1 will have the required boric acid solution volume increased to 2,600 gallons. The concentration in Part 2 has been reduced to between 6,560 ppm and 6,990 ppm of boron, which correlates to approximately 3.75 to 4.0 percent by weight. Part 3 will now require the 63°F instead of 145°F.
NLR-N93077 2 LCR 93-17 TS 3.1.2.7.b (3.1.2.5.b Unit-2) will be revised to increase the required borated water volume in the refueling water storage tank (RWST) from 12,500 gallons to 37,000 gallons.
TS 3.1~2~7 SR 4.1.2.7 (TS 3.1.2.5 SR 4.1.2.5. Unit-2) The format of* the surveillance statement will be revised to separate the boric acid storage system (labeled a) and the RWST (labeled b) requirements.
TS 3.1 .* 2.7 SR 4*.i*.2.7b '(TS 3 *. 1.2.5 SR 3.1.2.5.b Unit-2) will be revised to add the Surveillance for the boron concentration and borated water volume for RWST.
TS 3.1.2.8 wording for unit-1 will be revised to be similar to TS 3.1.2.6 (Unit-2). Typographical correction will be made to TS 3.1.2.6 (Unit-2) to correct the referenced TS from 3 . i. 1
TS 3.1.2.8.a (3.1.2.6.a Unit-2) will be revised to delete the heat trace requirement and indicate the required volume and concentration of boric acid in the boric acid storage system. Figure 3.1-2 has been added to provide the variable relation between concentration and volume. The solution temperature of 145°F has been reduced to 63°F.
TS 3.1.2.8. SR 4.1.2.8 (3.1.2.6 SR 4.1.2.6 Unit-2) will be revised similar to SR 4.1.2.7 (4.1.2.5 Unit-2).
TS 3.9.1 action statement will be revised to increase the flow rate from 10 gpm to 33 gpm and to decrease the boron concentration from 20,000-ppm boron to ~6,560-ppm boron. The footnote will be revised for unit 1 to be same as the unit 2 footnote.
TS 3.10.1 Action Statements a and b will be revised to increase the flow rate from 10 gpm to 33 gpm and to decrease the boron concentration from 20,000-ppm boron to ~6,560-ppm boron.
The bases for the boration system will be revised to delete the reference to the heat trace system. Additionally, the volumes and concentrations of borated water have been changed to reflect the calculated values shown in Attachment
- 3. New statements have been added to describe (1) how the temperatures on the boric acid tank water source is being monitored and maintained and (2) how the RWST shutdown margin volume requirements are determined.
NLR-N93077 3 LCR 93-17 II. REASON FOR THE PROPOSED CHANGES The original design of Salem required, the boron concentration in the BATs to be approximately 12 percent by weight. This concentration presently creates two major operational problems. First, the high temperature and high concentration create a reliability/availability issue with a boric acid system components including BAT pump seals, boric acid evaporator and small instrument lines. Second, the heat tracing requirements for the eves are extensive and require significant maintenance to maintain them operable. If a heat trace failure is undetected, the pipe blockage because of boric acid solidification may render one of the flow paths inoperable, impacting safety system availability. By reducing the concentration to between 3.75 and 4.0 percent by weight and maintaining the appropriate temperature to at least 63°F, the previously listed problems are eliminated.
Based upon the changes in the required volumes, concentration and solution temperature, the associated SRs were changed to include the new parameters to be monitored.
For additional clarification, the format was revised.
The borated water volume required in the RWST for Modes 5
- and 6 has been increased to 37,000 gallons to provide for the new boration requirements to maintain shutdown margins and additional instrument inaccuracies.
III JUSTIFICATION FOR THE CHANGE The boric acid storage system borated water volume and boron concentration minimum values presently specified in the Salem TS are based upon the ability to borate the reactor coolant system (RCS) to the required cold shutdown boron concentration. The present method used to achieve cold shutdown is to borate the RCS to the required concentration to obtain the TS shutdown margin of 1.6 percent delta k/k at 200°F before starting the plant cooldown. The eves is then required to provide adequate makeup of sufficiently borated water to compensate for shrinkage as the RCS temperature is lowered to cold shutdown.
The proposed boric acid concentration reduction in the BATs will be accomplished by making a change to the plant boration and cooldown procedures. Attachment 3 reevaluates the original requirements for the BAT boric acid concentration to show the acceptability of the new methodology of boration-to-cold shutdown with the reduced boron concentration. The new method of boration-to-cold shutdown allows for boration during the cooldown process.
NLR-N93077 4 LCR 93-17 When cooldown is started, makeup from the BAT is provided until such time as the required BAT volume is discharged into the RCS. At this time, additional volume from the second BAT, or from batching operations, or from the RWST is provided. The above combination or the RWST alone provides an adequate supply of borated water to ensure the required shutdown margin is maintained.
To operate at the proposed lower boric acid concentrations, the minimum required delivery rate will be increased to 33 gpm to ensure that the same net boration rate will be supplied as required by the current TS. Salem will be modifying the flow path from the boric acid tank to the boric acid blender to allow for the higher-required flow rate and the recalibration of the BAT level transmitter to allow for the maximum utilization of the BAT volume.
Additionally, the heat trace system will be disconnected.
As a precaution tqe heaters on the boric acid tank, the batching tank and the concentrates holding tank will be maintained. The settings for the heaters will be lowered to automatically maintain an approximate range of 65 to 75°F.
This will ensure that no significant amount of boric acid precipitates out in case there is an abnormal low Auxiliary Building temperature~
The volume of borated water required to provide adequate shutdown margin for Modes 5 and 6 (i.e., RCS less than 350°F) is, 7,100 .gallons from the RWST. Attachment 3 provides calculations to support this new volume require-ment. The proposed TS requires 37,000 gallons. This quantity was derived from a combination of: (1) the location of the lower tap.for the level transmitters on the RWST, (2) additional instrument inaccuracies, (3) conservatism to provide for gage legibility in the control room, (4) 7,100 gallons provided for shutdown margin, and (5) additional 140 gallons due to rounding up.
When performing batching operations, the boric acid batching tank is heated well above 63°F to ensure the boric acid will enter into solution easily. This will ensure that when the boric acid solution is transferred.to the BAT, it is at an elevated temperature relative to the area ambient temperature.
The 63°F temperature was selected to provide* sufficient margin to ensure the boric acid will remain in solution.
For the "worst-case" condition when there is a 4.0 percent solution, the boron still will not precipitate out until the
NLR-N93077 5 LeR 93-17 temperature falls below 58°F. The margin established of at least 5° is considered sufficient since the BAT and eves piping are housed in areas that are normally above the 63°F minimum.
UFSAR Section 9.4.2.1 describes the capabilities of the auxiliary building ventilation system. Based upon an expected range of external temperatures the system is capable of maintaining the building temperature from 60°F to 105°F. There is the possibility that air temperature in the auxiliary building may drop to approximately 60°F. As part of the modification, continuous temperature monitoring of the boration flow paths and components will be provided with an alarm. in the control. ro9m to annunciate whenever temperature *drops below 63°F. This alarm will be used to initiate additional monitoring to ensure that the solution temperature remains at or above the 63°F requirement.
Should ambient temperature decrease below 63°F, the boric acid tank heaters, in conjunction with boric acid pump recirculation, are capable of maintaining the boric acid in the tank and the pump at or above 63°F. A small amount of boric acid in the flowpath between the boric acid recirculation line and the suction line to the charging pump will precipitate out, but it will not cause flow blockage even with temperature below 50°F. At 50°F, 3~5% by weight will remain in solution. The small amount which precipitates out will not cause flow blockage. As soon as the temperature is retained to normal, the precipitated boric acid will go back into solution.
By revising the format of SRs 4.1.2.7 (Salem-2 SRs 4.1.2.5) and 4.1.2.8 (4.1.2.6 Salem-2), the actual SRs were not changed (except for those proposed by this submittal), but were aligned with the TS requirements and action statements.
This change will eliminate any confusion that was introduced in the original format.
In summary, the proposed revision to reduce the required BAT boron concentration will maintain shutdown margin requirements, and will eliminate the operational problem associated.with maintaining high boron concentrations.
Footnote for section 3.9.1 for unit 1 will be revised to be compatible with the definitions operational modes stated in TS table 1.1.
j
NLR-N93077. 6 LCR 93-17 IV. Significant Hazards Consideration In accordance with 10CFR50.92,PSE&G has reviewed the proposed technical specification (TS) changes and concluded the proposed changes do not involve a significant hazards consideration because the proposed changes would not:
- 1. Involve a significant increase* in the probability or consequences of an accident previously evaluated.
The reduction of the boric acid concentration in the boric acid tanks (BAT) and elimination of requirements for the associated heat trace circuits will not significantly increase the probability or consequence of an accident previously evaluated. Only minor modifications are planned, and while operating procedures will revised to reflect the new boration method, the capability to safely shut down has not been changed or modified. TS controls have been placed on the boric acid tank to ensure that the lack of heat tracing does not result in the boron precipitating out of solution. Originally, Salem had the ability to borate at 10 gallons per minute (gpm) with boron solution of 20,000 parts per million (ppm). With the proposed change, Salem will provide the ability to borate at 33 gpm with a solution of between 6,560-ppm to 6,990-ppm boron. This will ensure that the boron addition rate remains essentially the same. In addition, boron addition from the BAT is not taken credit for in any accident analysis.
Two independent and redundant boration flow paths with appropriate borated water are provided to compensate for reactivity changes and all expected transients throughout core life. The sources of borated water are the BATs and the Refueling Water Storage Tank (RWST)
- The RWST is necessary for ECCS requirements. The current Technical Specification Bases covers using feed and bleed from the RWST alone. The design bases used to establish the required volume and boron concentration in the BAT have been examined, and the results are presented in attachment 3.
The existing boric acid tank heaters, with the BAT pumps on recirculation, will ensure that there is no precipitation of boric acid in the majority of the safety related portion of the boric acid injection system. This includes.the boric acid tanks, the BAT pumps, and most of the process lines.
NLR-N93077 7 LCR 93-17 The exception is on the injection paths between the BAT pump recirculation line and the suction line to the charging pumps. A 4% boric acid solution will not cause line blockage even with temperatures well below 50°F. At 50°F, 0.125 or less, of the boric acid will precipitate out creating a small film at the bottom of the piping. Since this portion of the flowpath does not contain a significant amount of 4% boric acid solution, there is no significant amount of boron precipitating out.
- Also, this film will not adhere to the piping and will not cause the blockage of the flow path. When ambient temperature is restored, the film will go back very quickly into solution. Based upon this analysis, this change does not involve a significant increase in the probability or consequences of any accident previously evaluated.
- 2. create the possibility of a new or different kind of accident from any previously ~nalyzed.
The original Salem design required heat trace circuits to ensure the boron, which was at 12% by weight, would remain in solution and be available for reactor coolant system reactivity control throughout core life. By lowering the boron concentration to 3.75 to 4.0 percent by weight, there is no possibility of boron precipitating out of solution as long as the boric acid solution remains above 58°F. The auxiliary building, where this equipment is located normally, remains well above 58°F. Continuous monitoring of the required.area temperatures, in conjunction with an alarm in the main control room, will allow for operator actions to ensure the solution temperature remains above the TS-required temperature of greater than or equal to 63°F. By eliminating the need for the heat trace, there is an
- increase in the availability of the boric acid storage system. This stored volume remains adequate to bring the unit to a safe, cold shutdown. Therefore, the removal of requirements for heat trace circuits and the reduction of the boron c,oncentration in the BATs do not create the pos~ibility of a new or different kind of accident from any previously analyzed.
- 3. Involve a significant reduction in a margin of safety.
The margin of safety requirements is not affected by the removal of the heat trace circuits and reduction of the boric acid concentration in the BATs. The required flow paths and borated water sources are still
NLR-N93077 8 LCR 93-17 available as before. The required quantity of borateQ water is still available based upon the new evaluation, and the ability to deliver this borated water remains the same. As stated previously, the reduction of the boric acid concentration in the BATs will ensure that the boric acid remains in solution at the normal room temperature in the auxiliary building. To ensure this, temperature will be continuously monitored at the control room. With the above changes, there will be a net improvement in system reliability and, accordingly.
Therefore, the proposed changes do not involve a sicjnif ica,nt reduction in any margin of safety.
- v. Conclusions Based on the information presented above, PSE&G has concluded there is no significant hazards consideration.