ML18093B375
| ML18093B375 | |
| Person / Time | |
|---|---|
| Site: | Salem |
| Issue date: | 12/30/1988 |
| From: | Labruna S Public Service Enterprise Group |
| To: | NRC OFFICE OF ADMINISTRATION & RESOURCES MANAGEMENT (ARM) |
| References | |
| IEB-88-008, IEB-88-8, NLR-N88212, NUDOCS 8901090149 | |
| Download: ML18093B375 (3) | |
Text
Public Service Electric and Gas Company Stanley LaBruna Public Service Electric and Gas Company P.O. Box 236, Hancocks Bridge, NJ 08038 609-339-4800 Vice President - Nuclear Operations December 30, 1988 NLR-N88212 United States Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Gentlemen:
CONFIRMATORY LETTER NRC BULLETIN 88-08 SALEM GENERATING STATION, UNIT NO. 2 DOCKET NO.
~0-311 PSE&G hereby submits supplemental information to NRC Bulletin 88-08.
This information, provided in the enclosure to this letter, was developed during the Salem Unit 2 Fourth Refueling Outage as.required by the subject Bulletin.
Should yob have any questions with regard to this transmittal, please do. not hesitate to contact us.
"sincerely, Enclosure C
Mr. J. c. Stone, Licensing Project Manager Ms. K. Halvey Gibson, Senior Resident Inspector Mr. W. T. Russell, Administrator Region I Ms. J. Moon, Interim Chief New Jersey Department of Environmental Protection Division of Environmental Quality Bureau of Nuclear Engineering CN 415 Trent9n, NJ 08625 0
_I
STATE OF NEW JERSEY COUNTY OF SALEM
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REF: NRC BULLETIN 88-08 SS.
0 Stanley LaBruna, being duly sworn according to law deposes and says:
I am Vice President - Nuclear Operations of Public Service Electric and Gas Company, and as such, I find the matters set forth in our letter dated December 30, 1988, concerning the Salem Generating Station, Unit No. 2, are true to the best of my
~nowledge, information and belief.
me Subscrib~ and sworn t~ bef ~e this Jt1 day of ~
, 1988 11~ ~"""----
NOtary P66lic of New Jersey My Commission expires on lARAINE Y. BEARD Notary Public of New Jency My Commission Expires May 1, h9l
CONFIRMATORY LETTER NRC BULLETIN 88-08 ENCLOSURE SALEM GENERATING STATION, UNIT NO. 2 DOCKET NO. 50-311 e.
Bulletin 88-08 requested that we review our reactor coolant systems to identify any connected, unisolable piping that could be subjected to temperature distributions due to valve leakage which would result in thermal stresses not evaluated in the design analysis of the piping.
The bulletin agdressed both fatigue cracking induced by thermal cycling and piping distortion caused by thermal stratification.
our' respqnse, dated September 23, 1988, identified three locations in each of the Salem plants where thermal cycling could possibly induce fatigue cracking.
The response also discussed the* possibility of piping distortion of our pressurizer surge lines as described in the bulletin *.
During the fourth refueling outage for Unit No. 2, we performed NDE examination of the three locations in question.
The examinations included 2 11 and 3 11 eves piping, 1.5 11 safety injection piping and the 14" pressurizer surge line.
The NDE results did not identify any recordable indications *.of flaws.
We resolv~d our concern for leakage past the SJ71 valve by removing thi~ valve from Unit No. 2 as part of the BIT tank removal design change modification.
We also conducted a field walkdown of the pressurizer surge line to verify support and HEBA restraint clearances.
This walkdown did not identify any indicative piping deflection.
As described in our September 23, 1988 response to the bulletin, PSE&G will perform the NDE inspections of the suspect locations and verification walkdowns of the pressurizer surge*lines for a minimum of two consecutive outages on each unit to provide continuing assurance of system integrity.
Accordingiy, confirmatory letters will be provided within 30 days of completion of the outages describing the NDE results and all actions taken.