ML18059A686

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Forwards Insp Rept 50-255/93-32 on 931217-940128 & Notice of Violation
ML18059A686
Person / Time
Site: Palisades Entergy icon.png
Issue date: 02/22/1994
From: Miller L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To: Slade G
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.)
Shared Package
ML18059A687 List:
References
NUDOCS 9403010023
Download: ML18059A686 (19)


See also: IR 05000255/1993032

Text

Docket No. 50-255

License No. DPR-20

Consumers Power Company

ATTN:

Gerald B. Slade

General Manager

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION Ill

801 WARRENVILLE ROAD

LISLE. ILLINOIS 60532-4351

,*

FEB

-2 ~~ 1394

Palisades Nuclear Generating Plant

27780 Blue Star Memorial Highway

Covert; MI

49043-9530 * *

Dear Mr. Slade:

SUBJECT~ NOTICE OF VIOLATION (NRC INSPECTION REPORT NO. 50-255/93032)

This refers to the inspection conducted by Messrs. M. E. Parker and D. G.

Passehl of this office from December 17, 1993, through January 28, 1994.

The inspection included a review of authorized activities for your Palisades

Nuclear Generating* facility.

At the conclusion of the inspection, the

findings were discussed with those rnembers of your staff identified in the

~nclosed report.

Areas examined during the inspection are identified ip the report. Within

these areas, the inspection consisted of a selective examination of procedures

and representative records, interviews with personnel, and observation of

activities in progress.

The purpose of the inspection was to determine

whether activities authorized by the license were conducted safely and in

accordance with NRC

requir~ments.

Based on the results of this inspection, certain of your* activities appeared

to* be in violation of NRC requirements, as specified in the enclosed Notice of

Vi_olation (Notice).

The violation involves ineffective corrective actions to

preclude repetiti~e failures in submitting Licensee Event Reports (LER) within

thirty days as required by 10 CFR 50.73.

The untimely submittal of LERs have

occurred in April 1993, May 1992, February 1991, and November 1990.* Two of

  • .these late LER submittals (November 1990 and February 1991) were previously

documented in NRC violations.

We are concerned about the violation because it

indicates some persistent failures to correct this weakness.

-

You are required to respond to this letter and should follow the instructions

specified in the enclosed Notice when preparing your response.

In your

response, yo~ should document the specific actions taken and any additional

actions you plan to prevent recurrence. After reviewing your response to this

Notice, including your proposed corrective actions and the results of future

inspections, the NRC will determine whether further NRC enforcement action is

necessary to erysure compliance with NRC regulatory requirements.

9403010023 940222

PDR

ADOC~ 05000255

G

PDR

Consumers Power Company

2

~*

In accordance with 10 CFR 2. 790 of the NRC' s "Rules of Practice," a copy of

. this letter and its.enclosures will be placed in the NRC Public Document Room.

The responses directed by this lette~ and the enclosed Notice are not subject

to the clearance procedures of the Office of Management and Budget as required

by the Paperwork Reduction Act of 1980, Pub. L. No. 96.511.

Enclosures:

1. Notice of Violation

2. Inspection Report

No. 50-255/93032(DRP)

cc w/enclosure:

David P. Hoffman, Vice President

Nuclear Operations

David W. Rogers, Safety

and Licensing Director

OC/LFDCB

Resident Inspector, Rill

James R. Padgett, Michigan Public

Service Commission

Michigan Department of

Public Health

Palisades, LPM, NRR

SRI, Big Rock Point

G. E. Grant, Riil

Consumers Power Company

2

In accordance with 10 CFR 2.790 of the NRC's "Rules of Practice," a copy of

this .letter and its enclosures will be placed in the NRC Public Document Room.

The responses directed by this letter and the enclosed Notice are not subject

to the clearance procedures of the Office of Management and Budget as required

by the Paperwork Reduction Act of 1980, Pub. L. No. 96.511.

Enclosures:

1. Notice of Violation

2. Inspection Report

No. 50-255/93032(DRP)

cc w/enclosure:

David P. Hoffman, Vice President

Nu~lear Operations .*

David W. Rogers, Safety

and Licensing Director

OC/LFDCB

Resident Inspector, RIII

James R. Padgett, Michigan Public

Service Commission

Michigan Department of

Public Health

Palisades, LPM, NRR

SRI, Big Rock Point

G. E. Grant, RIII

bee: Public

WR

~i

. }..1'1('11 .

I RI I I

~v

Kropp

Sincerely,

fA1u)ruJtY.- ~)viJ/n .*

- 0~

L!

Lewis F. Miller, Jr., Chief

Reactor Projects Branch 2A

Mi 11 er

NOTICE OF VIOLATION

Consumers Power Company

Palisades Nuclear Generating Facility.

Docket No. 50-255

License No. DPR-20

During an NRC inspection conducted from December 17, 1993, through January 28,

.1994, a violation of NRC requirements was identified.

In accordance with the

"General Statement of Policy and Procedure for NRC Enforcement Actions,"

10 CFR Part 2, Appendix C, the violation is listed below:

10 CFR 50, Appendix B, Criterion XV[, requires that co~ditions adverse to

quality such as failures, deficiencies, deviations, defective m~terial and

equipment, and nonconformances are promptly identified and corrected. In the

case of significant conditions adverse to quality, measures shall ~ssure that

the cause of the condition is determined and corrective action taken to

preclude repetition.

10 CFR 50.73 (a)(2)(i)(B) requires that a licensee submit a Licensee Event

Report (LER) within 30 days of the discovery of.any operation ot condition

prohibited by the plant's Technical Specifications.

Contr~ry to .the above, the licensee has failed to take effective corrective

actions to preclude repetitive failures to submit LERs within 30 days of an

event in accordance with 10 CFR 50.73.

The lice~see failed to submit an LER

within 30 days in the following instances~

1. *

An LER for an April 27, 1993 event involvirg the simultaneous

inoperability of both emergency diesel generators was required to

be submitted by May 27, 1993, and was submitted on December 23,

1993.

2.

An LER for a May 6, 1992 ev~nt involving the simultaneous

inoperability of both emergency diesel generators was required to

be submitted by June 6, 1992, and was submitted on February 10,

1994.

3.

An LER for a February 24, 1991 event involving the unanticipated

start of an emergency diesel generator was required to be

submitted on March 26, 1991, and was submitted on June 30, 1991.

4.

An LER for a November 13, 1990 discovery of non-qualified

.electrical splices on equipment inside containment was required to

be submitted on December 13, 1990, and was submitted on January

28, 1991.

-

This is a Severity Level IV violation (Supplement I).

Pursuant to the provisions of 10 CFR 2.201, Consumers Power Company is hereby

required to submit a written statement or explanation to the U.S. Nuclear

Regulatory Commission, ATTN:

Document Control Desk, Washington, D.C. 20555

with a copy to the Regional Administrator, Region III, and a copy to the NRC

Resident Inspector at the facility that is the subject of this Notice, within

9403010029 940222

PDR

ADOCK 05000255

G

PDR

30 days of the date of the letter transmitting this Notice of Violation

(Notice).

This reply should be ~learly marked as a "Reply to a Notice of

Violation" and should include for each \\ifolation:

(1) the reason for the

violation, or, if contested, the basis for disputing the violation, (2) the

corrective steps that have been taken and the results achieved, (3) the

corrective steps that will be taken to avoid further violations, and (4) the

date when full compliance will be achieved., If an adequate reply is not

received within the time specified in this Notice, an order or a Demand for

Information may be issued to show cause why the license should not be

modified, suspend~d, or revoked, or why such other action as may be proper

should not be taken.

Where good cause is shown, consideration will be given

to extending the response ti~e.

Under the authority of Section 182 of the Act, 42 U.S.C. 2232, this response

shall be submitted under oath or affirmation.

Dated at Lisle, Illinois,

this ;;? day of {__&b, 1994

  • U. S. NUCLEAR REGULATORY: COMMISSION*

Report No. 50-255/93032(DRP)

Docket No. 50-255

Licensee: Consumers Power Company

212 West Michigan Avenue

Jackson, MI

49201

REG ION I I I

License No.

DP~-20

Facility Name:* Palisades Nuclear Generating Facility

Inspection At:

Palisades Site, Covert, Michigan

Inspection Conducted:

December 17,

1993~ thro~gh January 28, 1994

Inspectors:

M. f. Parker '.

D. G. Passehl

Approved By:

W. Kropp, Chief

Dat'e

7 *

Reactor Projects Section 2A

  • Inspection Summary

Inspection from December 17; 1993. through January 28, 1994

  • .,

(Report No.

50~255/93032(DRP))

.

Areas* Inspected: .Routine, unannounced inspection by the resident inspect~~~

of actions on licensee event report followup, followup of events, operational.

saf~ty verification, maintenance, surveillance, engineering and design issues,

regional requests, and report review:

No Safety Issues Management. System*

(SIMS) items were reviewed.

  • Results:* Of the eight areas inspected, no violations or deviations were
  • identified in six areas.

One violation:was identified *for failure to take

effective corrective action (paragraph 2:b) and one unresolved item was *

identified concerning a vacuum drying procedure (paragraph 7.a).

A strength was noted for the licensee's implementation of a comprehensive and

conservative inspection prog~am for in~pecting fuel assemblies destined for

dry fuel storage. A weakness was noted for submittal of an LER beyond the 30

day reporting requirement of 10 CfR 50.73(a)(l).

Further review found other

LERs not reported within the required time frame.

An unresolved item was

identified for the possible lack of adequate verification of the level of

vacuum obtained during the vacuum drying process used for Ventilated Storage

Casks (VSCs) 1 and 2.

9403010035 940222

PDR

ADOCK 05000255

0

PDR

.

.

1.

DETAILS

Management Interview (71707)

The inspectors met with licensee representatives (denoted in paragraph

11) on January 28, 1994, and informally throughout the inspection

period, to ~ummarize the sctipe and findings of the inspection

activities.

The inspectors also discussed the likely informational

content of the inspection report, with regard to documents or processes

reviewed by the inspectors.

The licensee did not identify any such

documents or processes as proprietary.* .

Highlights discussed during the exit interview were:

a.

Strengths noted:

The li~ensee has implemented a co~prehensive and

conservative insp~cti9n program fo~ inspecting fuel

assemblies destined for dry fuel storage (paragraph 4).

b.

Weaknesses noted:

An adequate verification of the level of vacuum obtained

during the vacuum drying procass used for Ventilated Storage

Casks (VSCs) 1 and 2 may not be available.

An unresolved

item was identified (paragraph 7.a).

An LER was submitted .beyond the 30 day reporting requirement*

of 10 CFR 50.73(a)(l). Further review found other LERs not

reported within the required time frame

(~aragraph 2.b).

2. *

Licensee Event Report Followup (92700, 92720)

The inspectors reviewed the following Licensee Event Report (LER) by*

means of direct observation, discussions with licensee personnel*, and

review of records.

The review addressed compliance to reporting

requirements and, as applicable, whether immediate corrective action and

appropriate action to prevent recurrence had been accomplished.-

The LER

discussed an event when both emergency diesel generators (DG) were .

simultaneously inoperable.

This LER was submitted beyond the 30 day

reporting requirement of 10 CFR 50.73(a)(l).

The licensee's corrective

  • actions to address the failure to submit a timely LER were considered a

separate issue.that is discussed in paragraph (b) below ..

a..

(Open) LER 255/93013:

Loss of Emergency Onsite AC Power Du~ To

Both Emergency Diesel Generators Being Simultaneously Declared

Inoperable:

On April 27, 1993, with the plant at 100 percent

power, DG 1-1 was test started and loaded to approxi~ately 500 kW

prior to removing DG 1-2 from service -to perform preventive

maintenance.

After approximately five minutes of operation, the

load on DG 1-1 dropped to zero and DG 1-1 was declared inoperable.

In accordance with the Technical Specifications, DG 1-2 was

started. and loaded to verify operability.

However, by paralleling DG 1-2 to the electrical distribution grid

to accept load, DG 1-2 was rendered inoperable. Specific types of

grid failures, occurring while a DG was paralleled to the grid,

The DG

would then be unavailable for automatic loading if the grid

failure should progress into a loss of offsite power.

Since the

specified function of the DG was to automatically start and load

upon loss of offsite power, the DG would.not be capable of

performing this specified function.

Therefore, the DG must be

declared inoperable whenever paralleled to the grid.

Since both DGs were simultaneously inoperable, Technical

Specification 3.0.3!

(~lant shutdown within one hour) was entered,

and an Unusual Event was declared in accordance with the emergency

operating procedures.

Correttive actions included submitting a rev1s1on to the

electrical section of the Technical Specifications to emulate

NUREG 1432, "Standard Technical Specificati~ns for CE Plants."

The proposed Standard Technical Specification provides enough time

to complete the test run of a DG and not declare both DGs

simultaneously inoperable.

The cause of the DG 1-1 failure was a defective fuel oil booster

pump.

A new pump was installed and satisfactorily tested.

Operating procedures were revised to more closely monitor the fuel

oil booster pump for degradation.

b.

Title 10 of the Code of Federal *Regulations, Part 50.73 (10 CFR

50.73 (a)(2)(i)(B)) requires that the licensee submit an LER

within* 30 days of the discovery of any operation or condition

prohibited by the plant's Technical Specifications. Therefor~. the

licensee was required to ~ubmit an LER within thirty days after

having both DGs inoperable on April 27, 1993.

The licensee did

not submit this LER until December 23, 1993, a period of 180 days.

Upon further review, the inspector noted the following previous

examples where the licensee failed to submit an LER within the

requ fred ti me:

(1)

LER 91-10 was submitted 80 days late for a February 24, 1991

unanticipated start of.an emergency diesel generator during

performance of a special test. This resulted in a violation

which was issued in Inspection Report No. 50-255/91012.

(2)

LER 91-02 was submitted 46 days late for a November 13, 1990

discovery of non-qualified electrical splices on equipment

inside containment, a condition outside the design basis of

the equipment.

This resulted in a violation which was

issued in Inspection Report No. 50-255/92004.

3

(3)

During the review of other potential late LER submittals,

the licensee di~covered another event similar to LER 93013,

involving simultaneous inoperability of both emergency

diesel generators in May 6, 1992 that should have been

reported. A licensee representative stated that the

licensee would report that event in a supplement to LER

93013.

.

Based on the above, the failure to report that both DGs were

simultaneously inoperable on April 27, 1993, with the plant at 100

percent power, represents a failure to take effective correction

action to preclude recurrence. This is considered a violation of

10CFR50, Appendix B, Criterion XVf (50-255/93032-0l(DRP)).

One violation was identified.

No deviation~, unresolved, or inspection

followup items were identified in this area.

3.

Followup of Events (93702)

During the inspection period, the licensee experienced two events, one

of which required prompt notification of the NRC pursuant.t6 10 CFR

50.72.

The inspectors verified that the notification was correct and

timely, that activities were conducted within regulatory requirements,

and that:corrective actions would prevent future recurre~ce. The events

are described below:

a.

On December 17, 1993, while attempting to restor~ the Cook -

.

b.

Palisades #1 345 kV circuit, Indiana & Michigan Power personnel' at

the D.C. Cook plant closed the Cook -.Palisades "Nl" automatic

circuit breaker (ACB}, with the three phas~ line grounds at

Palisades still attached.

The line grounds were in place to allow

performance of a preplanned outage for general maintenance on

transformers and associated motor operated airbreak switches at

Benton Harbor.

The Cook - Palisades #1 offsite power supply deenergized after the

ground was sensed.

However, as a result of a failed bre~ker relay

in the Palisades switchyard, both the Cook - Palisades #2 and the

Argenta - Palisades #2 sources supplying offsite power to

Palisades were lost. Thus, three of the six offsite power

  • supplies to the site were rendered unavailable at the same t1me.

Following repair of the failed breaker relay, power was restored

to the three offsite power sources later the same day.

On January 21, 1994, both the "A" and "B" trains 6f control room

HVAC were declared inoperable due to ice and snow clogging the

emergency air intake plenum.

Technical Specification 3.0.3 was

entered and a prompt telephone notification to the NRC pursuant to

10 CFR 50.72 was made. The inoperable condition lasted about 12

minutes, until utility workers could brush away the snow .

At the time of the event, plant operators were performing M0-33,

4

"Control Room Ventilation Emergency Operation," Rev.3, when a

positive pressure of 0.125 inches wg (water gauge) pressure could

not be maintained in the control room due to the clogged intake

plenum.

After unclogging the plenum, control room pressure

returned to 0.0250 inches wg.

The licensee issued a deficiency

report and will address preventive actions during future

performances of this surveillance test.

No violations, deviations, unresolved, or inspection followup items were

identified in this area.

4.

Operational Safety Verification (71707, 71710, 42700)

Routine facility operating activities were observed in the plant and

from the main control room.

Plant startup, steady power operation,

plant shutdown, and system lineup and operation were observed.

The performance of reactor operators and senior reactor operators, shift

engineers, and auxiliary equipment operators was observed and evaluated.

Included in the review were procedure use and adherence, records and

logs, communications, shift turnover, and the degree of professionalism

of control room activities.

Evaluation, corrective action, and response for off normal conditions

were examined.

This included compliance to any reporting requirements.

Observations of the control room monitors, indicators, and recorders

were made to verify the operability of emergency systems, radiation

monitoring systems, and nuclear reactor protection systems.

Revi~ws of

surveillance, equipment condition, and tagout logs were conducted.

Proper return to service of selected compone~ts was verified.

  • . Periodic verification of Engineered Safety Features status was conducted

by the inspectors.

Equipment alignment was verified against plant

procedures and drawings and detailed walkdowns selectively verified:

equipment labeling, the absence of leaks, housekeeping, calibration

dates, .operability of support systems, breaker and switch alignment, as

appropriate.

a.

General

The plant has been on line at essentially full power since the end

of the 1993 refueling outage. Activity levels of the primary

coolant system showed no significant adverse trends and were

closely monitored and reported daily. *

b.

Dry Fuel Storage Fuel Handling Inspections

The inspector observed selected portions of the licensee's fuel

inspection activities for the dry fuel storage project that

commenced on January 10, 1994.

The purpose of the inspections was

. to verify the identity and integrity of fuel assemblies destined

5

for dry fuel storage.

The inspections were performed visually and

ultrasonically.

The licensee_ intended to perform visual inspections (VT} and

ultrasonic inspections (UT} on 300 fuel assemblies.

In addition,

another 80 fuel assemblies that have already been visually

inspected were planned to have an.ultrasonic inspection.

The

inspections were scheduled to be performed over the next few

months.

A total of 264 fuel assemblies that satisfactdrily pass

the VT and UT testing were scheduled to be placed into dry fuel

storage in the current year.

The remaining fuel

ass~mblies that -

pass inspection were scheduled for a later date.

To date, visual examinations on 100 fuel assemblies had been

completed and no assemblies had been rejected. Several of the

assemblies had indications which will be evaluated and confirmed

by UT and dis~ositioned by engineering.

The inspector's review found that the licensee had implemented a

comprehensive and conservative inspection program for this

activity. Three licensed operators and three fuel inspectors had

been trained and dedicated to this task. There were daily pre-

and post-job briefings with the crew to identify any equipment

problems or other concerns.

The operators, fuel inspectors, their

supervisors, and the fuel handling system engineer wer~ all *

involved in the daily briefings.

-In addition, the licensee held an infrequent evolution pre_.,.job

briefing prior to start of the fuel inspections.

The brief was.

thorough, with good discussion between management and workers of

plans, procedures, safety precautions and ~anagement expectations.

  • Expected radiological conditions were discussed and stop work *

points ~ere clearly identified.

No violations, deviations, unresolved, or inspection followup items were

identified in this area.

5.

Maintenance (62703, 42700)

Maintenance activities in the plant were routinely inspected, including

both corrective and preventive maintenance.

Mechanical, electrical, and

instrument and control group maintenance activities were included.

The inspection was to assure the maintenance activities reviewed were

conducted in accordance with approved procedures, regulatory guides and

industry codes or standards, and in conformance with Technical

Specifications.

The following items were considered during this revi~w:_

the Limiting Conditions for Operation were met while components or

systems were removed from service; ~pprovals were obtained prior to

initiating the work; activities were accomplished using approved

procedures; and post maintenance t~sting was performed as applicable.

6

\\

The following maintenance activities were observed:

-

a.

Repack of Service Water Pump P-7A

b.

Service Water Pump P-7A breaker inspection

c.

Boric Acid Leak Walkdowns

The inspector performed a walkdown with maintenance department

representatives of areas where there was evidence-of boric acid

leaks. During the walkdown, the licensee's boric- acid program and

the associated procedure, EM-26, "Boric Acid-Leak Inspection,"

  • Rev.a, was discussed.

The purpose of the program was to perform

inspections of carbon steel components in all plant areas to

ensure no degradation exists due to boric *acid leakage:_--

Although some h6usekeeping concerns were identified, the-program

appeared to be effective.

Many areas showed overall improvement

since the end of the recent refueling outage when weaknesses

regardi~g the large amount of ~ontaminated areas and the excessive

use of catchments to dir~ct or contain boric acid leaks were

observed.

Th~ material condition of the east and west safeguards.

pump rooms had improved somewhat._

-

However, ther~ were ~till some wea~ areas sue~ as.removing the

boric acid buildup in catchments ~nd valve stem areas with boric

acid deposits. These obs~rvations were discussed.with the

maintenante personnel and plant management.

No violations, devia~ions, unresolved, or inspection followup items were

identified in this area.

-

.-

, .

. 6.

Surveillance (61726, 42700)

The inspector reviewed technical specifications required surveillance

testing as described below, and v~rified that testing was performed in

accordance with adequate procedures, test instrumentation was_

calibrated, and limiting conditions for operation were met.

The

inspector further verified that the removal and restoration of the

affected components were properly accomplished, test results conformed

with technical spe~ifications and procedure requirements,* test results

were reviewed by personnel other than the individual directing the test,

and deficiencies identified during the testing were properly reviewed

and resolved by appropriate management personnel.

a.

QE-35, "ED-01 and ED-02 Battery Checks - Quarterly," Rev. O

b.

Q0-14, "Inservice Test Procedute - Service Water Pumps," Rev.5

c.

RI-99, "Left Channel Nuclear Instrument Calibrations," Rev.2

d.

MI-2, "Reactor Protective Trip Units," Rev.37

7

._.

e.

. f.

M0-7, "Emergency Dies~l Generator 1-1 {K-6A)," Rev.29

Q0-30, "Engineered Safety Room Cooling and Ventilation-System,"*

Rev.a

No violations, deviation~, unresolved, or inspecti6n followup items were

identified in this area.

7.

Enqiheerinq and Design Issues (37700,92705)

The inspector monitored engineering and technical support activitjes at

th~ site including support from thJ corporate office. The purpose was *

to assess the adequacy of these functions in contribµting properly to

other functions such as operations, maintenance, testing, training, fire

protection, and configuration management.

a.

The inspector reviewed the licensee '.s calibration and procedure

controls for dry. fuel storage canisters after learning that

another nuclear utility may not have dried the canisters to the

vacuum pressure required by technical specifications. This review *

found that the plant specified tolerance for calibration of .the

Sensotec Digital *Gauge Pressure Instrument, used to measure the

level of vacuum in the dry fuel casks prior to helium backfill,.

~as plus or minus 0.25 percent of full scale (equal to. plus or

minus 0.063 psi a) ..

This toleran_ce was ]napprppriate s1nce the*

  • . required pressure tolerance needed per procedure was less th~n

. 0.060 psi a.

The licensee issued a deviatio~ repoit 6n the inspectors

observation,and had preliminarily ~oncluded that adeq~ate *

  • verification o_f the level *:of vacuum obtained during drying may not

'be-available._ However, the licensee's ,nalyses of existing

records showed no significant reduction in the effectiveness of

. the qry fuel* storage cask confinement system existed .. * According

  • to FHS-M-32~ "loading and Placing-the Ventilated Storage Cask into

Storage," Rev.I, the measured pressure readings following vacuum

drying for both Ventila~ed Storage Casks (VSCs) was 0.00 psia.

Therefore, assuming worst case tolerance, the VSC pressure could

have been 0.003 psi a greater than the required value.

The licensee sent the pressure instrument to an offsite

calibration laboratory for a rigorous comparison of true versus

  • indicated pressure measur~ments. Those results showed the

_

instrument to be more accurate than previously reported, to within

plus or minus 0.05 percent of full*scale, ~r plus or minus O.Of25

. psia.

However~ the inspector later learned that the pressure

instrument's digital readout was set to read 0.00 psia when

measuring any pressures below 0.10 psia. Therefore,* pressure in

the VSCs may have been as high as 0.1125 psia, almost twice as

high as required per procedure.

The licensee was reviewing

8

b.

additional logs and interviewing personnel to try to better

determine what level of vacuum was actually obtained.

Pending

further review by the licensee and NRC this matter 1s considered

an Unresolved Item

(50-255/93032-02 (DRP)).

The purpose of vacuum drying the VSCs was to evaporate any

moisture that could lead to degradation of the fuel cladding.

The

  • licensee contacted the VSC designer, who stated that the small

amount of overpressure that may have existed would not result in a

significant reductiori in .the effectiveness of the dry fuel storage

cask confinement system.

The inspector's review found weaknesses in the vacuum drying

procedure that failed to address the operating features-of-the~--------

instrument at pressures below 0.10 psia. There were apparent

weaknesses in personnel not quest~oning the adequacy of the

procedure, nor in questioning the suitability of the instrument

for use at the lciw pressures.

Althoug~ the instrument was

supplied by the cask manufacturer, the licensee failed to

thoroughly check its operating characteristics.

NRC .Region III mariagement and the Materials and Processes S~ction,

Engineering Branch, Division of Reactor Safety have reviewed the

existing open items for the Palisades Nuclear Power.Plant and have

determined that the fol~owing open items will be closed

administratively due to safety significance relative to emerging

priority issues and to the age of the item. lhe licensee ~s

reminded that commitments directly relating to these open items

are the responsibility of the licensee and should be met as

committed.

NRC Region III.will review licensee actions by

periodically sampling administratively tlosed items.

(1)

(Closed) 50-255/89007~01 through 11

50-255/89024-02 through 05, 50-255/90023-01. and

50-255/90025-01 through 24

These items .mainly pertain to*

the adequacy of design controls for large bore piping.

Inspection report number 50-255/89007 found a variety of

small errors indicative of w~ak design controls during the

modification process.

At the time, there were iridications

that the original I.E. bulletin (IEB) 79-14 program and the

seismic design bases were not sound.

The. 1 i censee

acknowledged the design control weaknesses and implemented

changes to *the process.

Inspection report number 50-

255/89024 reviewed modifications associated with the snubber

reduction project. During this inspection, additional

design control weaknesses were noted through the continued

assumption that the 79-14 calculations were correct. It was

eventually coricluded that the 79-14 calculations were

unreliable, both from an "as-built" as well as a

calculational accuracy perspective.

The licensee again

acknowledged the problem and committed to do a sample

9

program to evaluate the significance of the discrepancies.

Inspection report number 50-255/90025 reviewed the

modifications associated with the steam generator project.

In this instance, design control problems were noted with

the consultant performing the piping analyses.

In addition,

it was noted that the seismic design bases had been changed

or were not being met by CPCo.

As a result of this last

inspection- a comprehensive program was implemented by the

licensee to reconcile the design bases problems and to

reanalyze all of the safety-related pi~ing.

All of the above violations or unresolved items fall under

design control, procedures, or corrective actions.

Most

-individual -issues were- resolved prior to the end of the*

inspections, and all responses to violations were reviewed

and found acceptable.

NRC will periodically inspect the

licensee,s ongoing "Safety Related Piping Reverification

Program."

(2)

(Closed)S0-255/89026-01 through -03:

NRR had granted

interim relief for these items and the licensee s~bsequently

performed acceptable tests, therefore, these items can be

closed.

(3)

(Closed)50-255/92013-0l through 04:

These items were

duplicates of items tracked as 50-255/92012, that were

closed in Inspection Report 50-255/93005; therefore, these

items can be administratively closed.

No violations, deviations, o~ unresolved items were identified in

this area.

One Unresolved Item was identified ..

8.

Regional Requests (92705)

a.

Concerns:

The inspector reviewed the following three concerns.

1.

Concern:

There was a common practice for maintenance

personnel tri change the description of maintenance work

performed and equipmerit/consummables used for the work.

The inspectors interviewed maintenance department repairmen

and supervisors. Additionally, Administrative procedure

5.01, "Processing Work Request~/Work Orders," Rev. 12, was

reviewed.

Result:

The inspectors were unable to substantiate this

concern. Although uncommon, the "Summary of Work Performed"

section of completed work orders was sometimes clarified or

enhanced by maintenance personnel prior to being typed into

the licensee's computerized work order system.

Work orders

were copied on microfilm and retained for the life of the

plant.

The original work order "hardcopies" were destroyed .

10

Parts for safety related applications were specified

initially front by the mai_ntenance planners. Specific parts

needed for an activity were identified by stock number,

description, etc. There were occasions when specific parts

could not be identified because the exact equipment problem

could not be determined unti.l disassembly and inspection.

In these instances, parts were identified for safety related

work after disassembly.

Controlled material~ used were required to be listed on

completed work ord~r documentation for "Q-listed" work.

Components required to function during accident conditions,

and pressure retaining components as defined by the ASME

B&PV code, were required to have appropriate documentation

of materials used;

2.

  • Contern:

An employee was caught sleeping in the equipment

hatch area while assigned to hatch watch duty, on or about

November 19, 1989. The inspector interviewed the maintenance

supervisor who witnessed the employee sleeping.

No other

individuals were known to have witnessed. the employee

sleeping.

Result:

The inspector was unable to determine whether the

  • employee was sleeping.

However, the employee appeared to be

inattentive to his duties.

The maintenance supervisor stated he observed the employee

to be motionless for a period of time, resting against the

equipment hatch bulkhead.

He was unsure if the employee was

sleeping because he could not see his eyes.

The employee

was wearing utility-supplied dark safety glasses.

The

safety glasses were used to bl o.ck the glare from the new

high intensity lights that were installed on the polar

crane.

The maintenance supervisor informed the employee's

direct supervisor of the conduct and took disciplinary

action.

'

The equipment hatch watch was established during outages to

quickly shut the equipment hatch upon orders from plant

operators.

No plant conditions existed that required

closing the equipment hatch during this time period.

The

equipment hatch watch also typically serves the dual role as

crane operator.

3.

Concern:

Mechanical repairmen were recently laying around

the radiological controlled area (RCA). The inspector

interviewed several radiological protection (RP) technicians

and two RP supervisors. Specific questions asked to these

individuals were:

(a)

Did they observe any individuals laying or loitering

11

around the RCA during the last refueling outage that

began in June 1993;

(b}

What action did they take if any such individuals were

identified while in the plant; and

(c}

What were management's expectations.

Result: This concern was substantiated in that there was a

common practice for workers to pre-stage in a low dose area

while waiting for a job, such as welders waiting to start

work.

On a few occasions workers were asked to relocate

from a low dose rate area to* a lower dose rate ~rea. None

of the individuals interviewed identified anyone sleeping~

In addition, the resident inspectors have not identified any

cases of individuals sleeping in the RCA.

All of the RP personnel stated that if individuals were

confronted and did not obey directions to relocate, the

outage manager would be informed or other members of senior

plant management.

Job s~pervisors were expected to ensure

good ALARA practices were maintained.

Ultimately, the

responsibility of good ALARA practices rests with each

individual, as taught during General Employee Training .

. There were documented instructions that prohibit loitering

in the RCA.

Attached to every radiological work permit was

a page from administrative procedure 7.03, "Radiation Work

Permit,~ Rev.12, describing individual responsibilities for

proper radiation safety. Administrative procedure 7.03

provided specific direction not to loiter in radiation or

airborne areas, and tti use low dose areas as practicable to

accomplish work.

b.

The inspector followed up a Region III request to verify the

. satisfactory condition of the Palisades main turbine/generator.

The request came in response to .a main low pressure turbine

failure that occurred on December 25, 1993, at the Detroit Edison

Fermi Plant.

The overall condition of the*Palisades main turbine/generator was

good based upon bearing vibration level, generator.core vibration

level, and hydrogen usage.

The Palisades main turbine/generator has nine bearings that are

continuously monitored by an offsite contractor (Bently Nevada

System}.

The system alarms at seven mils (alert level} and at

fourteen mils (danger level}. The alarms activate both at the*

Bently Nevada System location and in the Palisades' main control

room.

At the time, there were no bearings in the alarmed state.

Also, there were no discernible differences in vibration levels

12

over the past year.

  • The Westinghouse "Gen-Aid" Sy~te~ continubusly monito~s ~ibration

of generator bearings seven through nine, as well as vibration on

the generator core. Direct communication between the Westinghouse

di~gnostic center and the main .control room would alert the

.

operators to any adverse trends.

No adverse vibration trends have

occurred in the past year.

Hydrogen usage was monitored daily by the plant operators.* No

significant increase in usage has been observed over the past

year, indicating steady generator hydrogen seal performance.

No violations, deviations, unresolved, or insp~~tion followup items were

identified in this area.

9.

  • Unresolved Items

Unresolved items are matters about which more information is required.in

6rder to ascertain whether they are acceptable items, violations, or

deviations.

An unresolved item disclosed during the inspectio~ is

discussed in paragraph 7.a.

10.

Report Review (90713)

During the inspection period, the inspectors reviewed the licensee's-

monthly operating report for December, 1993.

The. inspectors confirmed,

that the i~formation'provided met the reporting requirements of TS 6.9.1.C a~d Regulatory Guide 1.16, "Reporting of Operating_ information."

No violations, deviations, unresolv~d, or inspecti~n followup items wer~*

identified in this area.

11.

Person~. Contacted

Consumers Power Company

  • G. B. Slade, Plant General Manager

_

.*R. D. Orosz, Nuclear Engineering & Construction Manager

R. M. Rice, Director, NPAD

'D. D. Hice, Nuclear Training Manager

  • T. J. Palmisano, Plant Operations Manager

D. W. Rogers, Safety & Licensing Director

  • K. M. Haas, Radiological Services Manager

R. B. Kasper, Maintenance Manager

  • K. E. Osborne, System Engineering Manager

C. R.

Ritt~ Administrative Manager

J. C. Griggs, Human Resource Director

  • H. A. Heavin, Controller

J. L. Hanson, Operations Superintendent

13

D. J. Malone, Radiological Services Superintendent

J. H. Kuemin, Licensing Administrator

Nuclear Regulatory Commission CNRC)

M. E. Parker, Senior Resident Inspector

  • D. G. Passehl, Resident Inspe~tor
  • Denotes* those present at the exit meeting on Ja~uary 28, 1994.

In addition, the inspectors interviewed qther licensee personnel

including shift supervisors, control operators and engineering

personnel.

14