ML18058A570

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Insp Rept 50-255/92-16 on 920421-0608.No Violations or Deviations Noted.Major Areas Inspected:Plant Operations, Radiological Controls,Maintenance,Surveillance & Licensee Plans for Coping W/Strike
ML18058A570
Person / Time
Site: Palisades Entergy icon.png
Issue date: 06/23/1992
From: Jorgensen B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML18058A571 List:
References
50-255-92-16, NUDOCS 9206300166
Download: ML18058A570 (11)


See also: IR 05000255/1992016

Text

  • -

U. S. NUCLEAR REGULATORY COMMISSION .

Report No. 50-255/92016(DRP)

Docket No. 50-255

'

-

'

'

Licensee: Consumers Power Company

, 212 West Michigan .Avenue

Jackson, MI

49201

REGION II I

License No. DPR-20

Facility Name:

Palisades Nuclear Generating Plant

Inspection At:* Palisades Site, Covert, MI

Inspection Conducted:

April 21 through June*a, 1992

. lnsp~ctors:

J~ K; Heller

J. R. Roton

Approved By:

Inspecti6n Summary.

2A

Inspection from April 21 through June 8. 1992

(Report No. 50-255/92016(0RP))

Areas Inspected:

Routine unannounced i nspe'ct ion* by the resident inspectors of

plant operations, radiological controls, maintenance, surveillance and licensee.

p-lans for coping* with a stHke. No Safety Issues Management System (SIMS) items

were reviewed.

Result~: No violations or deviations were identified in the areas inspected.

The strengths, *weaknesses and Open Items are discussed fo paragraph.*

9,

  • "Management Interview."

In summary:

Strengths were noted in event response.

Weaknesses were noted in equipment response to an event and in a surveillan~e

procedure's acceptance criteria.

9206300166*920623

PDR

ADOCK 05000255

G

PDR

DETAILS

1.

Persons Contacted

Consumers Power Company

  • G. B. Slade, Plant General Manager
  • R. M. Rice, Plant Operations Manager
  • R. D. Orosz, Nuclear Engineering & Construction Manager *
  • P. M. Donnelly, Safety & licensing Director

K. M. Haas, Radiological Services Manager *

J. L. Hanson, Operations Superintendent

~R. B. Kasper, Mairitenance Manager

.

  • K. E. Osborne, System Engineering Manager
  • C. S. Kozup, Technical Engineer

W. L. Roberts,' Senior Licensing Engineer

R. W. Smedley, Staff licensing Engineer

T. J. Palmisano, Administrative & Planning Manager

Nuclear Regulatory Commission (NRC)

W; D.

Shafe~, Chief, Reactor Projects Branch 2

B~ L. Jorgerisen, Chief, Reactor Projects Section 2A

  • J. K. Heller, Senior Resident Inspector

J. R. Roton, Resident Inspecto~

  • Denotes some of those present at the Management Interview on
  • June 17, 1992.

Other members of the pl ant staff, and several members of the

contract . security force, were al so contacted during the

inspection period.

2i

Operational Safety Verification (71707, 71710, 42700)

Routine facility operating activities were observed as conducted in.the.

plant and from the main ~ontrol room.

Plant steady power *operation was

observed a.s app 1 i cab.l ~.

-

The performance of reactor operators -and senior reactor operato~s, shift

engineers, and auxiliary equipment operators was observed and evaluated.

Included in the review were procedure*use and adherence, records and logs,

communications, shift/duty turnover, and the degree of professionalism of

control room activities.

  • *

Observations of the control room monitors, indicators, and recorders ~ere.

made to verify the operability of emergency systems, radiation monitoring

systems, and nuclear reactor protection systems. Reviews of surveillance;

equipment condition, and tagout logs w~re conducted.

Proper return to

. service of selected components was verified.

2

a.

General

The plant operated at essentially full power during this r~porting:

period, except as discussed below.

b.

Power Reduction

c.

On May 10, 1992, a rapid power reduction, to 70 percent, was

performed in response tQ a loss of condenser vacuum .. The loss of

condenser vacuum was caused by air in leakage through a Feedwater

Pump drain. trap which. was subsequently repaired.

The inspector

reviewed the following:

(1)

The licensee used the Post Trip Administrativ_e

Review

procedure to capture and evaluate -the pertinent information

for this event.*

(2)

The report documented, by graph and written statements, that

the recently implemented feedwater control modifications had

(3)

(4)

worked well.

. The onshift reactor operators responded effectively,* even

  • *though they were not in their normal a~signmen~s. The Reactor

Operator-I was a temporary upgrade from the Reactor Operator-2

position and the Reactor Operator-2 was a temporary upgrade

from * a 1 i censed Auxiliary Operator.

The upgraded * Reactor

Operator-2 had recently obtained his license and had only seen

feedwater and condenser vacuum transients on the simulator.

  • The response of this crew demonstrated the strength of the

operators training, both in hardware response and teamwork ..

Du~ing the power redOction, .two control rods were slow;

requiring . operator intervention to prevent

~ rod-to-group

deviation.

The problem was di_scussed with the System

Engineer.* A similar problem (but different _rod) occurred

during a power reduction in the previous fuel cycle.

That

problem was traced to a circuit card and resolved. The system

engineer evaluation continued.

Safety Injection Tank Partial Depre~surization

On May* 13, 1992, one of four Safety* Injection Tanks (SIT) rapidly

depressurized, * froni approximately 220 psig to approximately 170

psig.

This was 30 psig below the minimum Technical Specification

. limit for SIT cover gas pressure .. The operators declared the "B"

SIT inoperable and returned the cover gas p~essure to the Technical

Specification limit within the time limit of the limiting condition

for operation (LCO). During the recovery, the "B" SIT depressurized

a second time to approximately 170 psig.

The "B" SIT was declared

3

i noperab 1 e and recovery . operations comp 1 eted within the LCO ti me*.

limits.

The operators concluded that the tank would depressurize

. if the cover gas was increased above 210 psig {approximately).

During meetings condu~ted over the next several days, the licensee

considered several failure mechanisms and concluded that the most

likely cause was "B" SIT relief valve premature actuation. A.test

and outage pl~n was formulated~

  • *

The SITs are located in the top of the containment, such that the

p 1 ant must* be subcri ti ca 1 * to permit testing * and repair.

The

inspector discussed this event with the system engineer and several

reactor operator~~

  • *

. The system engineer provided a brief maintenance history of the SITS

and_ stated that engin~ering, maintenance and operations ~ersonnel

have implemented s~veral unsuccessful attempts to find and resolve

a slight cover gas pressure leak from the SITs. * Leak detection

activities had ruled out an external leak. One of these activities

included removal of "B" SIT relief valve tri confirm the leak tight .

integrity and. verify the relief valve set point. The integrity was

confirmed and the re 1 i ef setpoi nt was . verified . at the correct

setting of approximately.260 pounds.*

Pri~r tti this event the op~rators were adding cover gas to the SITs

about *every two and one half days.

After the event, the

118

11 SIT

required cover gas addition every* ~hift, ~hich indicated that.the

relief valve did not fully reseat.

The othef SITs remained on the

previous schedule.

The upper administrative p~essure limit for the "B" SIT wai reduced

from 250 pound to 207 pounds.

  • This assured {during cover gas

addition} that the upper _pressure alarmed before the relief valve.

actuated.

The 1 ower admi ni strati ve limit o*f 203 pounds a.ssured

that at least on~ shift of cover gas pressure was available before

the Technical Specification limit was violated.

Several operatots were interviewed.

They stated*that adding cover

gas eacb shift was not time consuming or difficult and was already.

addressed in a System Operating Procedure,

  • *

The plant manager did not implement the planned outage schedule

because the operators were able to maintain the "8

11 SIT pressure

within the required band without reproducing the May 13 event.

Additionally, there were sufficient controls in effect to as.sure

that. the pressure would not inadvertently be reduced below the

Technical Specification limit.

d.

Head/Pressurizer Vents

During the post* refueling outage plant

h~atup,

~he ind*cated

pressure on PIA-1066, " Gaseous Vent Pressure Gauge,

11 increased as

the primary coolant system was pressurized.

The pr_essure increase

4

lagged the primary coolant system pressurization by several minutes.

When steady state primary coolant system conditions were achieved,*

the

down

stream

isolation valves

were

cycled.

The* line

depressuriz~d~ but was tepressurized in several minutes~

Th~' vent system is conn~cted to both the reactor vessel h~ad and.

press.urizer.

The line. relieves to either the pressurizer quench

tank or directly to

th~ containment atmosphere.

The system

configuration p~ovides for dual isolation from either the head or

the pressurizer to the containment atmospher*e.

PIA'.'" 1066 is

ins ta 11 ed on the common piping between the first and second

isolation valves.

The increase of pressure at PIA-1066 indicated

that the second set of isolation valves were holding pressure. This

was confirmed by the stable pressurizer quench tank readings and by

stable containment atmospheric temperature/humidity readings.*

Inspection Reports 50-255/89012(DRP), 50-255/90015(DRP) and 50-

255/91009(DRP) documented that this problem has occurred* in the

three previous operating cycles.

The work order history for this

system indicated that system engineering, operations and maintenance

groups have made ~everal attempts to resolve the problem.

It was

unclear if the problem r~sults from misapplication of th~ valves,

the system configuration; maint~nance problems, or some combination.

The inspector reviewed the work order history and discussed the

problem with engineering, operations and maintenance personnel. The

re so l.ut ion of this problem is. considered an open i tern.

Si nee the

. re solution of the open item was not *cl ear, the inspector* has

requested a written response to this open item (Open Item 255/92016~

Ol(DRP)). *

.

.

e.

  • Zebra Mussels

/

.

.

.

-

The licensee successfully treated the firewater system with Betz

CJ amTro l.

This addressed a conc~rn that the inspector raised in

Inspection Report 50-255/92006(DRP) -paragraph 7 .d. In that reportt

the inspector expressed concern that previous attempts to treat the*

system were unsutce~sful and that a failure to treat this system,

could result in a Zebra Muss~l infestation of the emergency makeup

lines to the Auxiliary Feedwater Pumps.

f.

Diesel Generator Inoperabil ity

During the performance of a monttlly *diesel generator operability

surveillance test, the 1-1 di~~el generator was declared inoperable

on May 7, 1992, because of vo.ltage control problems that resulted in

. the current exceeding the maxi mu*m al low able l i m_it.

Th is occurred

while. the diesel generator was loaded and paralleled to the

associated safeguards bus. The voltage regulator was replaced. The

cause of the voltage regulator pr~blem was still being evaluated.

The shift supervisor started and loaded the 1-2 diesel generator to

5

...

g.

confirm that the voltage control problem was not common to that-*

diesel generator. When lOading a diesel generator by paralleling it

to the associated safeguards bus, the licensee considers the diesel

generator inoperable because the diesel generator voltage regulator

cannot compe~sate for certain grid voltage swings. With two diesel

generators inoperable, the licensee applied Technical Spe~ification

3.0.3. This was exited

appro~imately 50 minutes later when the

  • diesel generator was shut down.and placed in *automatic. Entry into

Technical Specification 3.0.3 is a condition that wa~ reported per*

10 CFR 50.73, "Licensee Event Reports." Additional reviews will be

performed when the Licensee event report is evaluated. -

The "inoperability" of the diesel generator when.it is paralleled to

the grid was ideritifiedduring licensee evaluatioris completed within

the last six months. Because the probability for this type of event

is very low, the licensee i_s continuing to evaluate whether a fix is

warranted or justified. This was discussed at the exit interview.

Plant Personnel Changes

-

.

The Operations Manager assumes the NPAD Director position on July 1,

1992.

The Administrative and Planning Manger will become the

Operations Manager

on June

22,

1992,

and will . retain his

responsibilities for

outage

management

1nd. planning.

The

Administrative and

Faciliti~s Superintendent

~ill become the

Adminfstrative Manager, assuming responsibility fo~ the remainder of

the Administrative and Planning Department except several areas that_

were assigned to the fl ant Controller~

No violations, deviations~ or unresolved items were identified. One open

item was identified relating to chronic alarming of a pressurizer/head *

head vent pressure monitor.

3.

Radiological Controls (71707)

During routine tours of radiologically controlled plant facilities or

areas, the inspector observed occupational .radiation safety practices by

.the radiation protection staff and other workers. Effluent releases were

routinely_ checked, including examination of on-line record~r traces ~nd

proper oper~tion of automatic monitoring equipment.

a.

Access Control Computer

b .

The licensee has enhanced the radiological area access control

compute~ to quiz individuals pertaining to pertinent information on

the RWP.

A question i~ randomly selected from a bank of questions *

associated with the RWP.

These questions can range from stay time

to dos.e entry limits.

The quiz is p~rformed while the individual

el~ctronically signs onto an RWP.

Plant Personnel Changes

6

The Radiological Services Department (RSD} was reorganized on June

1, 1992.

The department now has four major support areas.

These

are

radiological

services,

radiologiC:al

internal

support,

radiological technical support and radiation safety oversight. This

information was

pro~ided to Region Ill radiation * protection

.specialists for review during a future inspection.

No violations, deviations, unresol~ed or open items were identified.*

4.

Ma1nteriance (62703, 42700}

Mainten~nce activities in the plant were routinely inspected~ including.

both

corrective maintenance

(tepairs} * and

preventive maintenance.

Mechani~al, *electrical,. and instrµment* and contfol group

mai~ten~nce

activities were included as available.

The foc*us of the* inspection was to assure the mai'ntenance activities

reviewed were conducted. in accordance with approved procedures, regulatory* *

guides and industry codes or standards and in conformance with Technical

Specifications. The following items were considered during this review:

the Limiting Conditions for Operation were met while components or ~ystems

were removed .fro~ servtce; approvals were obtained prior to initiating the

work; activities were accomplished using approved procedures; and post .

maintenahce testing was performed as applicable. *

The following work rirder (WO) activities were inipected:

a.

WO 24200601, "Heater Drain Pump P-lOB,*Repack Pump and Rebuild

Stuffing Box~" *

b.

WO 24001183, "Electro Hydro/Gov Control Cabinet Installation and

Checkout."

c.

WO 24104858, "Steam Generator Feedwater Pump P-lA, Coupling and

Overspeed Trip Test."

-

.

d.

WO 24104859, "Steam Generator Feedwater Pump P-lB, Coupling and

Overspeed Trip Test."

e..

WO 24202199, "Replace Diesel Generator l~l voltage regLllatoi.

11

f.

WO 24201756, "Repair Steam Leak at Stuffihg Box for CV-0501."

.

.

. .

'

This stea~ leak occurred during the plant heatup and appeared on a

. valve that had been disassembled during the outage. The iteam leak

was rep~ired by injection of a sealant into the leaking gasket area.

The energy from the steam then hardens the material.

The inspector reviewed the administrative .program for repairing

steam lea ks.

The repair was performed by a contractor using p 1 ant *

7

procedures and the work. order system.

Since the repair. was

  • temporary, a second work order was writteri to implement permanent .

repairs when plant conditions permit.

No violations, deviations, unresolved or open items were

identified.

. .

.

.

.

.

.

.

.

.

5~

  • Surveillance (61726, 42700)

. The inspector reviewed Technical Specifications. required surveillance

testing as described below and verified that testing was performed in

accordance with adequate procedures. Additionally, test inst~umentation

was calibrated, Limiting Conditio~s for Operation were met, removal and

~estoration of the affected components were properly accomplis~ed, and

test results conformed with Technical Specifications and procedure

requirements.

The results were* reviewed by personnel. other than the

individual directing the test and deficiencies identified during the

testing were properly reviewed and resolved. by appropriate management

personnel.

The follbwing activities were irisp~cted:

a.

RT-SD, "Engineered Safeguards* System - Right Channel.

11

The inspector obse~ved the pre-surveillance briefing and performance

  • of the test~ The briefing was thorough and demonstrated a complete

understanding of the sequence of events expected to occur.

Personnel involved in the surveillance ~onducted a dry run prior to

actual performance of the surve.i 11 a nee.

The surveill.ance *was

completed satisfactorilyi

b.

R0~32-10, "LLRT - Locai Leak *R~te Test Procedure for Penetratibn

MZ-10."

.

The inspector performed a review of R0-32-10, using Technical.

  • Specification 4.5, "Containment Tests," Technical Spedfication 3.6,

"Containment Systems," Pi~ing ~nd Instrument Drawing 214, "Service

Air," .and R0~32-10 Basis Document as references.

The

i~spectdr's .

. observations are discussed below.

( 1)

(2)

(3)

The inspector performed a dimerisional check of the installed

piping configuration and calculated the volume between the

test boundary.

The results were in agreement with tho~e of

the licensee.

The inspector found a . typographical i neons i st ency between

Table 5.1.3 and Attachment 3. The table names the down stream

vent valve as MV-CA 655 and Attachment 3 contains a schematic

of the penetration and misidentifies the vent valve as MV-CA

555.

This was identified to the System Engineer.

Tables 5.1.2 and 5.1.3 verified the "as-found" test and "as-

.left" positions of the valves and pipe caps affected by the

8

test.

Steps 5.4.4.a and_ 5.4.6.a -require the positioner to

return _the valves and pipe caps to the "as found" position or

as directed by the Shift Supervisor. -The inspector recognized

the general rieed for flexibility but questioned if this should

-apply to the test tap, which must be closed and the pipe cap

i_nstalled whenever containment integrity is required. If the

"as found" position was open rir the vent ca~ not install~d,

returning to the "as found" position could result in an

inoperable containment penetration during heat-up.

The--

inspector was informed that containment integrity checklist

3.3, which is performed prior to post outage heat-up, assures

the proper position of the cap and vent valve. The inspector

considered it more appropriate* to maintain control of -the

valves during the test by restoring the valve and pipe cap to

the required position at the completfon of the test.

This

would make checklist 3.3 an independent verification to ensure

  • containment integrity.

c.

R0-119, "lnservice Testing of Engineeted Safeguards Valves CV-3027

and CV-3056 (lri se~ie~ recirculation valves to the Safety Injection

and Refueling Water (SIRW) storage tank)."

(1) - During the previous fuel cycle, the _licensee identified

potential leak paths which may exist for post accident primary

cool ant. - One path was by valve seat 1 eakage past two valves -

(CV-3027 and CV-3056) in ~eri~s to the SIRW tank.

The SIRW

tank .has-

an

unfiltered vent.

- This

was_ a previously

unidentified source term to the control room.

During a lo~s

of-cool ant accident with the maximum hypothetical core damage

and total leakage past these valves of greater than .0.1 gpm~

the_ Iodine design dose 1 imit to the control room _would be

exceeded.

This leak path would not result in unacceptable

- dose at the site boundary.

The _leak path was documented in

correspondence from Consumers Power Company dated J_une 14,

_ 1991, July 17, 1991, and January 10,

1992~

The licensee

committed to perform seat leakage testing of CV--3027 and CV-

3056 during thel992 refueling outage.* R0-119 performed this

testing. The results of R0-119 calculated the most restricted

leakage at .01 gpm.

Based on this information,-the integrity

of ~his leak path was confirmed.

(2)

The inspector reviewed R0-119 -and the accompanying basis

document.

The inspector confirmed that the va 1 ve 1 i neup _

proviqed an appropriate test boundary, the isolation valves

were tested individually and a vent path was established down

stream of CV-3027 and CV-3056.

(3)

The procedure trended performance to predict future results.

Step 5~4.5.6 required corrective action if a prdjecticin based

on three or more tests indicated that the next leakrate wduld

exceed the acceptance by 10 percent. The inspector questioned

this statement, since any leakage above O.l gpm would place

9

  • . ...
  • ,

..

the plant in ~n unacceptable condition. This was identified**

to the Inservice Inspection Supervisor who

revie~ed the

comments and agreed* to revise the acceptance criteria. This

was discussed at the exit interview.

No violations, de~iations, unresolved, or open items were identified.

7.

  • Licensee Plans For Coping With Strikes (92709)

The

company-wide union

contract with maintenance

(mechanical

and

. ~lectrical) and operation personnel* expired. on May 3I, I992. *

Th~

inspector, a Region III Branch Chief and a Region III Section Chief met

with the licensee on April 27, I992, to discuss the strike contingency

plans. The meeting fulfilled a verbal commitment from the licensee which

was documented in paragraph.II of Inspection Report 50-255/92006(DRP). On

May 3I, 1992, at IO:OO p~m., the inspector observed onshift activities by

nonunion and union members, as the midnight deadline approached ... The

II:30 p.m. shift turnover, between union* me~bers, was orderly and

routinely performed.

At II:45 p.m., the utility and union reached a

tentative agreement.

The shift meeting conducted by the shift supervisor,

(a non-union position) at I2:30 a.m. on June 2, I992, was orderly and

routine. At the completion of this reporting period, the contract had not

been approved by the uni on membership.

Unt i 1 this is accomplished~ the *

  • strike contingency remains in effect.

No violations~ deviations, unresolVed, or open items w~re identified.

~.

Open Items

Open Items are matters which have been discussed with the licensee, ~nd

wil 1 be reviewed further by the inspector.

These involve some action on

the part of the NRC or licensee or both .. An Open Item was disclosed

during* the inspection and is discussed in Paragraph 2.d.

9.

Management Interview (7I707)

The inspectors met with licensee representatives - denoted in Paragraph I

- on June I7, I992, to discuss the scope and findings of the inspection~

In addition, the likely informational content of the inspection report*

with regard to documents or processes reviewed by the inspectors~during

the inspection was also discussed. The licensee did not identify any such

documents or processes as proprietary.*

Highlights of the exit interview are discussed below:

a.

Strengths noted:

( l)

Use of the Post Trip procedure to eva 1 uate the 1 oss of

condenser vacuum

event (pa~agraph 2.b, "Operations - Power *

Reduction").

IO

y

. "

(2)

The response of the crew - which had not normally worked

together - to the. loss of condenser vacuum event demonstrated

strong team work and training (paragraph 2.b,* "Operations -

Power Reduction").

b.*

Weaknesses noted:

. (1)

(2)

During a power reduct(on, two control. rods

~ere slow,

. requiring operator intervention to prevent a rod-to-group

deviation.

The problem has occurred during previous power .*

reductions. (paragraph 2.b, "Operatioos -_Power Reduction").*

A surveillance procedure contained nonconservative acceptance

criteria (paragraph 5.c, "Surveillance").

c.

The SIT depressurization was discussed, *s was the decision not to

shut down to facilitate repairs. * The inspector did not identify a

saf~ty concern with continued power operation but cautioned the

d.

1 icensee *to be proactive to changing conditions (paragraph 2.c,

"Operations - Safety Injection Tank Depressurization").

The open i tern was* discussed.

response

on

the

docket

Head/Pressurizer Vents").

.

.

This inc 1 uded the request for a

(paragraph

2.d,

"Operations

e.

Plant* pers6nnel * chan~es in the Operations

and

Radiol~gical

Protection areas were* discussed .(paragraph 2.g, "Operations" and

paragraph 3.b, "Radiological Controls").

f..

Steam leaks were discussed, along with the heightened ~RC awareness

for problems

that* result from

steam leaks

(paragraph 4.f,

"Maintenance").

11