ML18054A798
| ML18054A798 | |
| Person / Time | |
|---|---|
| Site: | Palisades |
| Issue date: | 05/31/1989 |
| From: | Goralski G, Mlynarek M CPC INTERNATIONAL INC. |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| NUDOCS 8906210072 | |
| Download: ML18054A798 (4) | |
Text
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~mflner POWERINli MICHlliAN'S PRDliRESS Palisades Nuclear Plant: 27780 Blue Star Memorial Highway, Covert, Ml 49043 June 12, 1989 US Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 LICENSEE REPORT OF MONTHLY OPERATING DATA DPR-20, DOCKET NO 50-255 Enclosed is a copy of the Monthly Operating Data and a Sununary of Operating Experience for the Palisades Nuclear.Plant for the month of May, 1989.
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George Goralski Reactor Engineer CC: DPHoffman, P26-117B KMHaas, Palisades ABDavis, USNRC KWBerry/RRFrisch, P24-614B CSKozup, Palisades Resident Inspector, Palisades DLHackett, Pll-420B DRHahn, Div of Rad Health Services, Lansing, MI SLHall, Michigan Dept of Labor, Lansing, MI RCallen, Michigan Public Service Conunission Records Center, INPO, Atlanta, GA RWTaylor, CE, Palisades AAAlatalo, Palisades LLBumb, P21-324 GBSzczotka, P-21-311B HRSnider, P-21-326 Administrator, USNRC Document Control, 950*22*35*10/L MGM89*015 OC0185-0001A-OP03 A CMS ENERGY COMPANY 1
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OPERATING DATA REPORT DOCKET NO 50-255
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DATE 06-12-89 COMPLETED BY MGMlynarek TELEPHONE (616)764-8913 OPERATING STATUS NOTES
- 1.
Unit Name: Palisades
'-:---~~"---~~~~~~~~~~~~~
- 2.
Reporting Period:
890501-890531
- 3.
Licensed Thermal Power (MWt):
2530
- 4.
Nameplate Rating (Gross MWe):
811.7
- 5.
Design Electrical Rating (Net MWe):
805
- 6.
Maximum Dependable Capacity (Gross MWe): *"k770
- 7.
Maximum Dependable Capacity (Net MWe):
- 730
- 8.
If Changes Occur in Capacity Ratings (Items Number 3 through 7) since last report, give reasons:
- 9.
Power Level to Which Restricted, if any (Net MWe):
623 (80%)
- 10.
Reasons for Restrictions, if any:
80% power limitation implemented based upon administrative guidelines with intent to improve steam generator reliability (not
- 11.
- 12.
- 13.
- 14.
- 15.
- 16.
- 17.
- 18.
- 19.
- 20.
- 21.
- 22.
- 23.
- 24.
- 25.
- 26.
based upon regulatory requirements).
Hours In Reporting Period Number of Hours Reactor Was Critical Reactor Reserve Shutdown Hours Hours Generator On-Line Unit Reserve Shutdown Hours This Month 744.0 744.0 744.0 Yr-to-Date 3,623.0 2,907.9 2,891.0 Gross Thermal Energy Generated (MWH) 1,499,736 5,797,920 Gross Electrical Energy Generated (MWH) 483,750 1,875,950 Net Electrical Energy Generated (MWH) 454,190 1,760,287 Unit Service Factor 100.0 79.8 Unit Availability Factor 100.0 79.8 Unit Capacity Factor (Using MDC Net) 83.6 66.6 Unit Capacity Factor (Using DER Net) 75.8 60.4 Unit Forced Outage Rate 0.0 20.2 Cumulative 152,966.0 81,915.3 78,013.1 164~348,925 51,420,435 48,412,536 51.0 51.0
- 48.5 39.3 34.6 Shutdowns Scheduled Over Next Six Months (Type, Date and Duration of Each):
45 day scheduled maintenance outage for steam generator repair to start October 1 1989.
If Shut Down at End of Report Period, Estimated Date of Start Up:
Units in Test Status (Prior to Commercial Operation):
INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION
- Based on condenser backpressure Forecast
- Weighted Average (635 MWe used as MDC Net prior to October 1985)
Achieved OC0185-0001B-OP03
r
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,AVERAGE DAILY UNIT POWER LEVEL DOCKET NO 50-255 UNIT Palisades DATE 06-12-89 COMPLETED BY MGMlynarek TELEPHONE (616)764-8913 MONTH ____
MA_Y_l..;;9_8""""9 __ _
DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)
(MWe-Net) 1 518 17 605 2
618 18 609 3
619 19 606 4
619 20 605 5
620 21 618 6
623 22 609 7
623 23 610 8
620 24 605 9
619 25 606 10 619 26 610 11 619 27 614 12 618 28 612 13 618 29 609 14 617 30 604 15 618 31 599 16 617 INSTRUCTIONS:
On this format, list the average daily unit power level in MWe-Net for each day in the reporting month.
Compute to the nearest whole megawatt.
OC0185-0001C-OP03
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SUMMARY
OF OPERATING EXPERIENCE FOR MAY, 1989 Palisades began the month of May with power being maintained at 80%.
On May 1, at approximately 0700, a plant upset occurred while removing the dilution water pump P40B from service.
Air leakage into the East Main Condenser Waterbox re-duced circulating water flow through the condenser, resulting in a decreasing condenser vacuum.
An emergency power reduction (from 80% to 35% in 7 minutes) using control rods was utilized to spare the plant from a low vacuum trip.
An increase in power began at 0930 with 80% power being reached at 1945.
Reactor power was then maintained at 80% for the remainder of the month.
OC0185-0001E-OP03