ML18053A478

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Discusses Inadequacies of Response to Notice of Violation from Insp Rept 50-255/88-08 Re Failure to Identify Conflict Between FSAR Classification & Actual Use of Containment Penetration 33 & Improperly Executed Surveillance Test
ML18053A478
Person / Time
Site: Palisades Entergy icon.png
Issue date: 07/29/1988
From: Greenman E
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To: Hoffman D
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.)
References
NUDOCS 8808120063
Download: ML18053A478 (3)


See also: IR 05000255/1988008

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Docket No. 50-255

  • Consumers Power Company

ATTN:

David P. Hoffman

Vice President

Nuclear Operations

212 West Michigan Avenue

Jackson, MI

49201

Gentlemen:

JUL 2 9 1988

NRC Inspection Report No.88-008 dated April 22, 1988 transmitted two Notices

of Violation and requested a written response.

Consumers Power Company

responded to these violations by letter dated May 23, 1988.

Violation l

pertains to containment penetration 33 and the failure to identify the conflict

between the FSAR classification and actual use as an unreviewed safety question

(URSQ).

V1olation 2 regards the performance of a surveillance test that was

improperly executed.

Several concerns and inadequacies with your response and corrective actions

were identified during the review of your response.

Our primary concern is

the appearance of the inability to conduct an adequate 10 CFR 50.59 evaluation.

These issues are enumerated in the attachment to this letter and it is requested

pursuant to 10 CFR 2.201 that you respond in writing within 30 days of the

date of this letter.

Sincerely,

63 960729

asoa1200

05000255

PDR

ADOC~

PNU

( Y!Odwf-G~irector

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Division of Reactor Project

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Attachment: Comments and

Questions on Violations 1 & 2

cc w/attachment:

Mr. Kenneth W. Berry, Director

Nuclear Licensing

Gerald B. Slade, General Manager

DCD/DCB (RIDS)

Licensing Fee Managemen~ Branch

Resident Inspector, RIII

Ronald Callen, Michigan

Public Service Commission

Michigan Department of

Public Health

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Violation 1

1.

In the section titled

11 Corrective Actions Taken and Results Achieved

11 of

you~ response to Inspection Report No. 88008 dated May 23, 1988, no

explanation is given relating to:

1) the cause for dropping, without

proper review, the proposed modification of January 6, 1982, which had

been initiated to resolve the conflict between FSAR commitments and

operational requirements; 2) why both the Safety Evaluation (SE) completed

at the time of the proposed modification and the revised SE completed on

March 13, 1988, failed to identify the issue as an Unresolved Safety

Question (URSQ).

2.

In the same section of your response, the reasoning used to determine that

an URSQ does not exist are both faulty and inaccurate.

rirst, the system

in question, though not directly connected to the primary coolant system

(PCS) as pointed out in your response, does not preclude the application

of 10 CFR 50, Appendix A design criteria to the penetration.

The level of

commitment to containment design criteria is not evident and further, it

is not clear given the leakage history of certain check valves, that this

line should be considered not connected to the PCS.* Second, administrative

controls are not

11 in place

11 that would require an operator to "remain at

the valve during flushing and sampling.

11

Third, the approval of only a

one hour LCO for a Safety Injection Tank operability indicated the high

significance placed on its safety function and does not indicate that the

NRC had reviewed the containment isolation aspect.

3.

Other concerns have also resulted from a critique of your 10 CFR 50.59

review and associated safety evaluation completed on the same date as the

response in question and which concluded that an URSQ does not exist.

a.

In the discussion of the first possible scenario (Item 2 of the SE)

where the operability of the Safety Injection Tank (SIT) system is

evaluated for consequences of an accident, the conclusion appears to

be based on subjective reasoning instead of quantitative analysis or

calculations.

b.

Several questions ne~d to be addressed relating to the discussion of

the second possible accident scenario (Item 2 of the SE) and in the

evaluation of the operability of the containment system.

(1) It is argued that postulating the failure of the presumably

unprotected drain line is not probable and no mention is made as

to how this event would relate to the design criteria to which

Palisades is committed.

(2)

In lieu of an evaluation on the impact on 10 CFR 100 limits, a

PRA analysis (which has neither been reviewed nor approved by

the NRC) is u~ed to argue that since containment is postulated

to fail early in the PRA analysis, the failure of this

penetration would have no effect on offsite dose, when in

reality, a two inch hole in containment provides a leakage

pathway far in excess of that allowed by the Palisades FSAR to

meet the 10 CFR 100 offsite dose limits.

1

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(3)

. ..

The NRC has not and would likely not approve the continued use

of an operator not -located in ready access to the isolation

valves and dedicated to the purpose of valve closure.

(4) Standard Technical Specifications (TS) make provisions for

opening certain manual isolation valves under administrative

control, but only after review and approval by the NRC.

Although

approval after review may seem likely, it is inappropriate for

an SE to presume approval or acceptability of an unreviewed

safety question and render a conclusion that the issue is not

an URSQ.

(5)

The second and third paragraphs of Item 2 have conflicting

statements with respect to the size of the penetration (one inch

flow restriction, two inch hole).

c.

Item 4 of the SE pertaining to the consequences of a malfunction of

equipment addressed only the operability of the Safety Injection Tank,

but not the consequences of the failure of the containment isolation

valves to isolate containment.

d.

Item 6 again presumes the acceptability of manual operation.of the

isolation v~lves. It is not clear whether the operability of the

containment system was considered.

e.

Item 7 discusses the margin of safety as reduced, but not

significant.

The logic of Item 2 does not adequately explain how it

can be considered insignificant.

The SE further states that the

basis for the.TS is affected (requires a change), yet does not

identify the issue as an URSQ.

Violation 2

1.

Corrective actions include training on MI-39 but no commitment was made

as to who will be included nor was a completion date established.

2.

Pleise advise us as to the status and completion dates of actions on the

QA and HPE recommendations.

2