Letter Sequence Approval |
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MONTHYEARML18043A8062000-04-19019 April 2000 April 19 2000 - Issuance of Amendments 149 and 140 Re Revised Elevated F-STAR Distance for Steam Generator Tubes Project stage: Approval 2000-04-19
[Table View] |
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Category:Letter
MONTHYEARML24298A0552024-10-30030 October 2024 Response to Alternative RR-10, Auxiliary Feedwater Valve Testing IR 05000282/20244032024-10-25025 October 2024 – Security Baseline Inspection Report 05000282/2024403 and 05000306/2024403 05000282/LER-2024-001-01, Auxiliary Building Special Ventilation System Inoperable During Movement of Irradiated Fuel Assemblies2024-10-22022 October 2024 Auxiliary Building Special Ventilation System Inoperable During Movement of Irradiated Fuel Assemblies L-PI-24-044, Application to Revise Technical Specifications to Adopt TSTF-591, Revise Risk Informed Completion Time (RICT) Program2024-10-21021 October 2024 Application to Revise Technical Specifications to Adopt TSTF-591, Revise Risk Informed Completion Time (RICT) Program ML24277A1012024-10-0303 October 2024 Closure of Interim Report of a Potential Deviation or Failure to Comply Associated with Bentley Systems Incorporated Autopipe Software ML24221A3622024-09-27027 September 2024 Issuance of Amendment Nos. 245 and 233 Revise Technical Specification 3.8.1, AC Sources-Operating, Surveillance Requirement 3.8.1.2, Note 3 ML24241A1682024-09-23023 September 2024 Transmittal Letter Amendment No. 13 to Materials License No. Special Nuclear Material-2506 for the Prairie Island Independent Spent Fuel Storage Installation 05000282/LER-2024-001, Auxiliary Building Special Ventilation System Inoperable During Movement of Irradiated Fuel Assemblies2024-09-16016 September 2024 Auxiliary Building Special Ventilation System Inoperable During Movement of Irradiated Fuel Assemblies IR 05000282/20243012024-09-13013 September 2024 NRC Initial License Examination Report 05000282/2024301 and 05000306/2024301 IR 05000282/20240052024-08-28028 August 2024 Updated Inspection Plan and Assessment Follow-Up Letter for Prairie Island Nuclear Generating Plant, Units 1 and 2 (Report 05000282/2024005 and 05000306/2024005) L-PI-24-040, Post-Submittal Package Letter2024-08-23023 August 2024 Post-Submittal Package Letter IR 05000282/20245012024-08-0505 August 2024 Emergency Preparedness Inspection Report 05000282/2024501 and 05000306/2024501 ML24213A1592024-07-31031 July 2024 Operator Licensing Examination Approval - Prairie Island Nuclear Generating Plant IR 05000282/20240022024-07-30030 July 2024 Integrated Inspection Report 05000282/2024002 and 05000306/2024002 ML24208A1502024-07-26026 July 2024 Independent Spent Fuel Storage Installation - Submittal of Quality Assurance Topical Report (NSPM-1) ML24197A2012024-07-15015 July 2024 Notification of NRC Baseline Inspection and Request for Information; Inspection Report 05000282/2024004 IR 05000282/20240102024-06-28028 June 2024 Comprehensive Engineering Team Inspection Report 05000282/2024010 and 05000306/2024010 L-PI-24-036, – Preparation and Scheduling of Operator Licensing Examinations2024-06-28028 June 2024 – Preparation and Scheduling of Operator Licensing Examinations ML24158A5912024-06-0606 June 2024 CFR 50.46 LOCA Annual Report L-PI-24-031, Independent Spent Fuel Storage Installation, Supplement to License Amendment Request to Revise Independent Spent Fuel Storage Installation (ISFSI) License Conditions 23(a), 24(A)(2), and 24(B)(2)2024-06-0505 June 2024 Independent Spent Fuel Storage Installation, Supplement to License Amendment Request to Revise Independent Spent Fuel Storage Installation (ISFSI) License Conditions 23(a), 24(A)(2), and 24(B)(2) L-PI-24-014, License Amendment Request to Revise the Technical Specification Definition of Reactor Trip System (RTS) Response Time and Apply Response Time Testing to RTS Trip Functions with Time Delay Assumption2024-06-0303 June 2024 License Amendment Request to Revise the Technical Specification Definition of Reactor Trip System (RTS) Response Time and Apply Response Time Testing to RTS Trip Functions with Time Delay Assumption 05000306/LER-2024-001-01, Reactor Trip and Auto-Start Actuation of Auxiliary Feedwater Due to Loss of Suction to the 22 Main Feedwater Pump2024-05-31031 May 2024 Reactor Trip and Auto-Start Actuation of Auxiliary Feedwater Due to Loss of Suction to the 22 Main Feedwater Pump ML24155A1922024-05-31031 May 2024 Refueling Outage Unit 2 R33 Owners Activity Report for Class 1, 2, 3 and Mc Inservice Inspections ML24262A1992024-05-29029 May 2024 L-PI-24-018 PINGP 75 Day Letter ML24149A3712024-05-29029 May 2024 (Ping) - Information Request for the Cyber-Security Baseline Inspection, Notification to Perform Inspection L-PI-24-030, Response to Request for Additional Information Regarding License Amendment Request to Revise Technical Specification 3.8.12024-05-22022 May 2024 Response to Request for Additional Information Regarding License Amendment Request to Revise Technical Specification 3.8.1 ML24141A1292024-05-22022 May 2024 Northern States Power Company - Use of Encryption Software for Electronic Transmission of Safeguards Information ML24141A0452024-05-20020 May 2024 Information Request to Support the NRC Annual Baseline Emergency Action Level and Emergency Plan Changes Inspection ML24128A2572024-05-16016 May 2024 ISFSI A13 Acceptance Letter IR 05000282/20240012024-05-15015 May 2024 Integrated Inspection Report 05000282/2024001 and 05000306/2024001 ML24130A2362024-05-0909 May 2024 Independent Spent Fuel Storage Installation - 2023 Annual Radiological Environmental Monitoring Program Report ML24130A2392024-05-0909 May 2024 2023 Annual Radioactive Effluent Report ML24071A1162024-05-0101 May 2024 Issuance of Amendment Nos. 244 and 232 Revise TS 3.7.8, Cooling Water (Cl) System ML24128A0882024-04-30030 April 2024 Submittal of Updated Safety Analysis Report (Usar), Revision 38 05000306/LER-2024-001, Reactor Trip and Auto-Start Actuation of Auxiliary Feedwater Due to Loss of Suction to the 22 Main Feedwater Pump2024-04-29029 April 2024 Reactor Trip and Auto-Start Actuation of Auxiliary Feedwater Due to Loss of Suction to the 22 Main Feedwater Pump ML24089A2382024-04-29029 April 2024 Summary of Nuclear Property Insurance IR 05000282/20244012024-04-25025 April 2024 – Security Baseline Inspection Report 05000282/2024401 and 05000306/2024401 ML24100A8042024-04-24024 April 2024 – Alternative Request RR-09 for Safety Injection and Volume Control System Category C Check Valve Inservice Testing ML24114A0882024-04-23023 April 2024 Annual Report of Individual Monitoring for the Prairie Island Nuclear Generating Plant (PINGP) ML24113A1182024-04-12012 April 2024 NRC Letter Re NRC Office of Investigations Report No. 3-2023-004 ML24100A1212024-04-0909 April 2024 Submittal of Revised Pressure and Temperature Limits Report ML24093A2832024-04-0202 April 2024 Nuclear Material Transaction Report L-PI-24-012, Independent Spent Fuel Storage Installation - License Amendment Request: Revise Independent Spent Fuel Storage Installation (ISFSI) License Conditions 23(a), 24(A)(2), and 24(B)(2)2024-04-0202 April 2024 Independent Spent Fuel Storage Installation - License Amendment Request: Revise Independent Spent Fuel Storage Installation (ISFSI) License Conditions 23(a), 24(A)(2), and 24(B)(2) ML24089A2402024-03-29029 March 2024 Guarantee of Payment of Deferred Premiums ML24060A1232024-03-27027 March 2024 To Request 1-RR-5-10 and 2-RR-5-10 Regarding Reactor Pressure Vessel Welds and Nozzle Welds 05000282/LER-2023-001-01, Reactor Trip, Auxiliary Feedwater and Emergency Service Water System Actuation Due to Electrical Transient in DC Control Power Cables2024-03-21021 March 2024 Reactor Trip, Auxiliary Feedwater and Emergency Service Water System Actuation Due to Electrical Transient in DC Control Power Cables ML24262A1512024-03-15015 March 2024 L-PI-24-011 150 Day Letter 2024 PINGP ILT NRC Exam ML24010A0582024-03-0505 March 2024 Amendment No. 12 to Materials License No. Special Nuclear Material-2506 for the Prairie Island Independent Spent Fuel Storage Installation L-PI-24-004, Independent Spent Fuel Storage Installation - Annual Effluent Report, January Through December 20232024-02-29029 February 2024 Independent Spent Fuel Storage Installation - Annual Effluent Report, January Through December 2023 IR 05000282/20230062024-02-28028 February 2024 Annual Assessment Letter for Prairie Island Nuclear Generating Plant, Units 1 and 2 (Report 05000282/2023006 and 05000306/2023006) 2024-09-27
[Table view] Category:License-Operating (New/Renewal/Amendments) DKT 50
MONTHYEARML24221A3622024-09-27027 September 2024 Issuance of Amendment Nos. 245 and 233 Revise Technical Specification 3.8.1, AC Sources-Operating, Surveillance Requirement 3.8.1.2, Note 3 ML24185A0912024-07-0101 July 2024 Acceptance of LAR to Revise TS Definition of Reactor Trip System (RTS) Response Time and Apply Response Time Testing to RTS Trip Functions with Time Delay Assumptions in the Accident Analyses ML24071A1162024-05-0101 May 2024 Issuance of Amendment Nos. 244 and 232 Revise TS 3.7.8, Cooling Water (Cl) System ML24088A1012024-03-29029 March 2024 Summary of March 6, 2024, Public Meeting with NSPM Regarding Planned LAR to Modify Technical Specifications Definitions and Incorporate Plant-Specific Methods for Response Time Testing for Prairie Island Nuclear Plant, Units 1 & 2 ML24059A4042024-03-0606 March 2024 March 6, 2023, Presubmittal Meeting for License Amendment Request to Modify Technical Specifications Definitions & Approve Plant-Specific Methods for Response Time Testing (EPID L-2024-LRM-0034) - Slides ML23356A0032024-01-17017 January 2024 Issuance of Amendments Revise Technical Specification 5.6.6, Reactor Coolant System (RCS) Pressure and Temperature Limits Report (PTLR) ML23115A4072023-04-26026 April 2023 Correction of License Amendment Nos. 226 and 214 Adoption of TSTF-425, Revision 3, Relocate Surveillance Frequencies to Licensee Control - RITSTF Initiative 5B ML22357A1002023-03-31031 March 2023 And Prairie Island Nuclear Generating Plant, Units 1 and 2 - Issuance of Amendments Standard Emergency Plan and Consolidated Emergency Operations Facility ML22300A2232022-11-0101 November 2022 Issuance of Amendments 241 and 229 TSTF-577 Revised Frequencies for Steam Generator Tube Inspections ML22181A0002022-08-17017 August 2022 Issuance of Amendments Reactor Trip System Power Range Instrumentation Channels ML22188A0852022-07-15015 July 2022 Correction Letter for Amendments 238 and 226 to Renewed Facility Operating Licenses ML22061A2062022-04-0101 April 2022 Issuance of Amendments TSTF-471, Rev. 1, TSTF-571-T, and Administrative Changes to Technical Specification Section 5.0 ML21312A0212021-11-23023 November 2021 Issuance of Amendment Nos. 237 and 225 Inoperable Cooling Water System Supply Header ML21008A0012021-03-19019 March 2021 Issuance of Amendment Nos. 236 and 224 Low Temperature Overpressure Protection ML20346A0202021-03-15015 March 2021 Issuance of Amendment Nos. 235 and 223, Adoption of Technical Specifications Task Force Traveler TSTF-505, Revision 2, Provide Risk-Informed Extended Completion Times - RITSTF Initiative 4b ML20356A0022021-02-0505 February 2021 Issuance of Amendment Nos. 234 and 222, Revise Technical Specifications 3.2.1 and 5.6.5 Identified in Westinghouse Nuclear Safety Advisory Letters NSAL-09-05, Revision 1, and NSAL-15-1 ML20283A3422020-11-18018 November 2020 Issuance of Amendment Nos. 233 and 221 Adoption of Technical Specifications Task Force Traveler TSTF-547, Clarification of Rod Position Requirements ML20217L1852020-10-0202 October 2020 Issuance of Amendment Nos. 232 and 220 Increase the Integrated Leak Rate Test Program Type a and Type C Test Frequency ML20210M0142020-09-0808 September 2020 and Prairie Island Nuclear Generating Plant, Units 1 and 2 - Issuance of Amendment Nos. 204, 231, and 219 TSTF-529 Clarify Use and Application Rules ML19276F6842019-11-12012 November 2019 Issuance of Amendments 230 and 218 Issuance of Amendments Adoption of 10 CFR 50.69 - Risk Informed Caterization and Treatment of Structure, Systems and Components of Nuclear Power Reactors ML19232A1512019-11-0707 November 2019 Issuance of Amendments Modifying the Design Basis for Quality Classification of Certain Fuel Handling Equipment ML19255H2012019-09-19019 September 2019 Correction Letter for Amendment Nos. 228 and 216 to Renewed Facility Operating License Nos. DPR-42 and DPR-60 ML19225D2172019-08-24024 August 2019 Correction Letter for Amendment Nos 228 and 216 to Renewed Facility Operating License Nos. DPR-42 and DPR-60 ML19140A4472019-07-30030 July 2019 Issuance of Amendments Revision to National Fire Protection Association (NFPA) Standard NFPA 805 Modifications ML19128A1332019-06-0606 June 2019 Issuance of Amendments TSTF-439 Eliminate Second Completion Times Limiting Time from Discovery of Failure to Meet an LCO ML19045A4802019-04-16016 April 2019 Issuance of Amendment Nos. 226 and 214 Adoption of TSTF-425, Revision 3, Relocate Surveillance Frequencies to Licensee Control - RITSTF Initiative 5B ML19029A0942019-01-29029 January 2019 Issuance of Amendment No. 213, One-Time Technical Specification Change to Extend Completion Time for EDGs D5 and D6 (Emergency Circumstances) ML18100A7882018-05-0101 May 2018 Issuance of Amendment Special Heavy Lifting Device Nondestructive Examination Frequency (CAC Nos. MG0072 and MG0073; EPID L-2017-LLA-0280) ML17346A3612018-03-0606 March 2018 Issuance of Amendment Nos. 224 and 211 to Adopt Changes to the Emergency Plan ML17362A2022018-03-0505 March 2018 Issuance of Amendment Concerning Revision to the Prairie Island Nuclear Generating Plant, Units 1 and 2 Emergency Plan (CAC Nos. MF9345 and MF9346; EPID L-2017-LLA-0175) ML17334A1782017-11-30030 November 2017 Issuance of Amendment Request Related to Spent Fuel Pool Criticality Technical Specification Changes (CAC Nos. MF7121 and MF7122, EPID L-2015-LLA-0002) Non-Proprietary ML17310B2392017-11-28028 November 2017 and Prairie Island Nuclear Generating Plant, Units 1 and 2 - Issuance of Amendment Unit Staff Qualifications (CAC Nos. MF9545, MF9546, and MF9547; EPID L-2017-LLA-0195) ML17163A0272017-08-0808 August 2017 Issuance of Amendments Transition to NFPA-805 Performance-Based Standard for Fire Protection for Light Water Reactor Electric Generating Plants ML17130A7162017-06-20020 June 2017 Issuance of Amendments Technical Specification 3.8.7 Inverters-Operating ML16256A5142016-10-13013 October 2016 Issuance of Amendment One-Time Extension for Technical Specification Surveillance Requirement 3.8.4.3. DC Sources - Operating ML16133A4062016-06-16016 June 2016 Issuance of Amendment Nos. 217 and 205, Adoption of Technical Specifications Task Force TSTF-523, Revision 2, Generic Letter 2008-01, Managing Gas Accumulation (CAC Nos. MF6449 and MF6450) ML15264A2092015-11-30030 November 2015 Issuance of Amendment Nos. 216 and 204 Regarding Revisions to Technical Specification 3.3.3 and Renewed Facility Operating License ML15229A1762015-08-26026 August 2015 Issuance of Amendment Nos. 215 and 203 Regarding Revision to Licensing Basis Analysis for a Waste Gas Decay Tank Rupture ML15086A0462015-05-21021 May 2015 Issuance of Amendment Nos. 214 and 202 Regarding Revisions to Technical Specification 3.8.1, AC Sources - Operating ML15062A0132015-05-20020 May 2015 Issuance of Amendments 213 and 201 to Revise TS 3.5.3, ECCS - Shutdown ML14239A2572014-11-28028 November 2014 and Prairie Island Nuclear Generation Plant, Units 1 and 2 - Issuance of License Amendments Regarding Cyber Security Plan Implementation Schedule Milestones ML14296A6662014-11-19019 November 2014 Issuance of Amendments Regarding Nuclear Methodology References ML13270A2792014-01-25025 January 2014 Issuance of Amendments Emergency Plan Changes ML13175A2082013-09-11011 September 2013 Issuance of Amendment Exception to Technical Specification 5.5.14 Testing Requirements Associated with Steam Generator Replacement ML13241A3832013-08-29029 August 2013 Issuance of Amendments Spent Fuel Pool Criticality Changes ML13113A4002013-07-0202 July 2013 License Amendments TSTF-510 ML13093A3442013-05-0909 May 2013 License Amendments for Fuel Oil System and TSTF-501 ML1129011152011-12-0101 December 2011 Issuance of Amendments Revision of Technical Specifications 5.2.1, Onsite and Offsite Organizations and TS 5.3, Plant Staff Qualifications. ML1122008562011-10-27027 October 2011 Operating Plant, Units 1 and 2 - Issuance of Amendments Request to Exclude the Dynamic Effects Associated with Certain Postulated Pipe Ruptures from the Licensing Basis Based Upon Application of Leak-Before-Break Methodology ML1119904692011-08-16016 August 2011 Issuance of Amendments Changes to Security Plan 2024-09-27
[Table view] Category:Safety Evaluation
MONTHYEARML24221A3622024-09-27027 September 2024 Issuance of Amendment Nos. 245 and 233 Revise Technical Specification 3.8.1, AC Sources-Operating, Surveillance Requirement 3.8.1.2, Note 3 ML24071A1162024-05-0101 May 2024 Issuance of Amendment Nos. 244 and 232 Revise TS 3.7.8, Cooling Water (Cl) System ML24100A8042024-04-24024 April 2024 – Alternative Request RR-09 for Safety Injection and Volume Control System Category C Check Valve Inservice Testing ML24060A1232024-03-27027 March 2024 To Request 1-RR-5-10 and 2-RR-5-10 Regarding Reactor Pressure Vessel Welds and Nozzle Welds ML23356A0032024-01-17017 January 2024 Issuance of Amendments Revise Technical Specification 5.6.6, Reactor Coolant System (RCS) Pressure and Temperature Limits Report (PTLR) ML23215A1672023-12-15015 December 2023 Acceptance of Requested Licensing Action Amendment Request to Revise Surveillance Requirement 3.8.1.2 Note 3 ML23115A4072023-04-26026 April 2023 Correction of License Amendment Nos. 226 and 214 Adoption of TSTF-425, Revision 3, Relocate Surveillance Frequencies to Licensee Control - RITSTF Initiative 5B ML22357A1002023-03-31031 March 2023 And Prairie Island Nuclear Generating Plant, Units 1 and 2 - Issuance of Amendments Standard Emergency Plan and Consolidated Emergency Operations Facility ML22300A2232022-11-0101 November 2022 Issuance of Amendments 241 and 229 TSTF-577 Revised Frequencies for Steam Generator Tube Inspections ML22270A3252022-09-30030 September 2022 (Prairie Island), Unit 2 - Authorization and Safety Evaluation for Alternative Request No. RR-08 ML22181A0002022-08-17017 August 2022 Issuance of Amendments Reactor Trip System Power Range Instrumentation Channels ML22166A3892022-07-28028 July 2022 Issuance of Amendments 239 and 227 24-Month Operating Cycle ML22061A2062022-04-0101 April 2022 Issuance of Amendments TSTF-471, Rev. 1, TSTF-571-T, and Administrative Changes to Technical Specification Section 5.0 ML21312A0212021-11-23023 November 2021 Issuance of Amendment Nos. 237 and 225 Inoperable Cooling Water System Supply Header ML21008A0012021-03-19019 March 2021 Issuance of Amendment Nos. 236 and 224 Low Temperature Overpressure Protection ML20346A0202021-03-15015 March 2021 Issuance of Amendment Nos. 235 and 223, Adoption of Technical Specifications Task Force Traveler TSTF-505, Revision 2, Provide Risk-Informed Extended Completion Times - RITSTF Initiative 4b ML20356A0022021-02-0505 February 2021 Issuance of Amendment Nos. 234 and 222, Revise Technical Specifications 3.2.1 and 5.6.5 Identified in Westinghouse Nuclear Safety Advisory Letters NSAL-09-05, Revision 1, and NSAL-15-1 ML20283A3422020-11-18018 November 2020 Issuance of Amendment Nos. 233 and 221 Adoption of Technical Specifications Task Force Traveler TSTF-547, Clarification of Rod Position Requirements ML20217L1852020-10-0202 October 2020 Issuance of Amendment Nos. 232 and 220 Increase the Integrated Leak Rate Test Program Type a and Type C Test Frequency ML20276A0032020-10-0202 October 2020 Request to Use a Provision of a Later Edition of the American Society of Mechanical Engineers Boiler and Pressure Vessel Code, Section XI ML20210M0142020-09-0808 September 2020 and Prairie Island Nuclear Generating Plant, Units 1 and 2 - Issuance of Amendment Nos. 204, 231, and 219 TSTF-529 Clarify Use and Application Rules ML20230A0512020-09-0303 September 2020 Reactor Vessel Material Surveillance Capsule Withdrawal Schedules ML20153A4012020-06-0101 June 2020 and Prairie Island Nuclear Generating Plant, Units 1 and 2 - Relief from the Requirements of the ASME Code ML20134H9582020-05-29029 May 2020 and Prairie Island Nuclear Generating Plant, Units 1 and 2 - Relief from the Requirements of the ASME Code ML20135G9922020-05-29029 May 2020 and Prairie Island Nuclear Generating Plant, Units 1 and 2 - Relief from the Requirements of the ASME Code ML19276F6842019-11-12012 November 2019 Issuance of Amendments 230 and 218 Issuance of Amendments Adoption of 10 CFR 50.69 - Risk Informed Caterization and Treatment of Structure, Systems and Components of Nuclear Power Reactors ML19232A1512019-11-0707 November 2019 Issuance of Amendments Modifying the Design Basis for Quality Classification of Certain Fuel Handling Equipment ML19140A4472019-07-30030 July 2019 Issuance of Amendments Revision to National Fire Protection Association (NFPA) Standard NFPA 805 Modifications ML19177A3802019-07-0303 July 2019 Reactor Vessel Material Surveillance Capsule Withdrawal Schedules ML19128A1332019-06-0606 June 2019 Issuance of Amendments TSTF-439 Eliminate Second Completion Times Limiting Time from Discovery of Failure to Meet an LCO ML19045A4802019-04-16016 April 2019 Issuance of Amendment Nos. 226 and 214 Adoption of TSTF-425, Revision 3, Relocate Surveillance Frequencies to Licensee Control - RITSTF Initiative 5B ML19046A1662019-02-25025 February 2019 Relief from the Requirements of the ASME Code ML19029A0942019-01-29029 January 2019 Issuance of Amendment No. 213, One-Time Technical Specification Change to Extend Completion Time for EDGs D5 and D6 (Emergency Circumstances) ML18270A0152018-10-19019 October 2018 and Prairie Island Nuclear Generating Plant, Units 1 and 2 - Relief from the Requirements of the ASME OM Code ML18100A7882018-05-0101 May 2018 Issuance of Amendment Special Heavy Lifting Device Nondestructive Examination Frequency (CAC Nos. MG0072 and MG0073; EPID L-2017-LLA-0280) ML17346A3612018-03-0606 March 2018 Issuance of Amendment Nos. 224 and 211 to Adopt Changes to the Emergency Plan ML17362A2022018-03-0505 March 2018 Issuance of Amendment Concerning Revision to the Prairie Island Nuclear Generating Plant, Units 1 and 2 Emergency Plan (CAC Nos. MF9345 and MF9346; EPID L-2017-LLA-0175) ML17334A1782017-11-30030 November 2017 Issuance of Amendment Request Related to Spent Fuel Pool Criticality Technical Specification Changes (CAC Nos. MF7121 and MF7122, EPID L-2015-LLA-0002) Non-Proprietary ML17310B2392017-11-28028 November 2017 and Prairie Island Nuclear Generating Plant, Units 1 and 2 - Issuance of Amendment Unit Staff Qualifications (CAC Nos. MF9545, MF9546, and MF9547; EPID L-2017-LLA-0195) ML17163A0272017-08-0808 August 2017 Issuance of Amendments Transition to NFPA-805 Performance-Based Standard for Fire Protection for Light Water Reactor Electric Generating Plants ML17130A7162017-06-20020 June 2017 Issuance of Amendments Technical Specification 3.8.7 Inverters-Operating ML17110A2752017-05-0404 May 2017 Safety Evaluation Regarding Implementation of Mitigating Strategies and Reliable Spent Fuel Pool Instrumentation Related to Orders EA-12-049 and EA-12-051 ML16320A0212016-11-28028 November 2016 and Prairie Island Nuclear Generating Plant, Units 1 and 2 - Review of Changes to the Northern States Power Company Quality Assurance Topical Report ML16256A5142016-10-13013 October 2016 Issuance of Amendment One-Time Extension for Technical Specification Surveillance Requirement 3.8.4.3. DC Sources - Operating ML16246A2002016-10-0404 October 2016 Request for Relief 1RR-4-11 and 2-RR-4-11 Associated with Certain Inservice Inspection of Component Welds for the Fourth 10-Year Interval ML16133A4062016-06-16016 June 2016 Issuance of Amendment Nos. 217 and 205, Adoption of Technical Specifications Task Force TSTF-523, Revision 2, Generic Letter 2008-01, Managing Gas Accumulation (CAC Nos. MF6449 and MF6450) ML15264A2092015-11-30030 November 2015 Issuance of Amendment Nos. 216 and 204 Regarding Revisions to Technical Specification 3.3.3 and Renewed Facility Operating License ML15229A1762015-08-26026 August 2015 Issuance of Amendment Nos. 215 and 203 Regarding Revision to Licensing Basis Analysis for a Waste Gas Decay Tank Rupture ML15196A2132015-08-17017 August 2015 Requests 1-RR-4-9 and 2-RR-4-9 Associated with the Fourth Ten-Year Interval for the Inservice Inspection Program ML15196A2412015-08-12012 August 2015 Requests 1-RR-5-6 and 2-RR-5-6 Associated with the Fifth Ten-Year Interval for the Inservice Inspection Program 2024-09-27
[Table view] |
Text
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. . REC'D A PR 2 5 2000 UNITED STATES NUCLEAR REGULATORY COMMISSION WASHINGTON, D.C. 20555-0001 April 19, 2000 55401
SUBJECT:
PRAIRIE ISLAND NUCLEAR GENERATING PLANT, UNITS 1 AND 2 -
ISSUANCE OF AMENDMENTS RE: REVISED ELEVATED F-STAR (EF*)
DISTANCE FOR STEAM GENERATOR TUBES (TAC NOS. MA7126 AND MA7127)
Dear Mr. Wadley:
The Commission has issued the enclosed Amendment No. 149 to Facility Operating License No. DPR-42 and Amendment No. 11i.o to Facility Operating License No. DPR-60 for the Prairie Island Nuclear Generating Plant, Units 1 and 2, respectively. The amendments consist of changes to the Technical Specifications (TSs) in response to your application dated November 10, 1999, as supplemented February 25, 2000.
The amendments revise the EF' distance for the steam generator tubes specified in TS 4.12.D.1.(1) following a correction to a minor error in the calculations supporting "the current EF* distance.
A copy of our related safety evaluation is also enclosed. The Notice of Issuance will be included in the Commission's biweekly Federal Register notice.
Sincerely, Tae Kim, Senior Project Manager, Section 1 Project Directorate Ill Division of Licensing Project Management Office of Nuclear Reactor Regulation Docket Nos. 50-282 and 50-306
Enclosures:
- 1. Amendment No. 149 to DPR-42
- 2. Amendment No. 140 to DPR-60
- 3. Safety Evaluation cc w/encl: See next page
UNITED STATES NUCLEAR REGULATORY COMMISSION WASHINGTON, D.C. 20555-0001 SAFETY EVALUATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION RELATED TO AMENDMENT NO. 149 TO FACILITY OPERATING LICENSE NO. DPR-42 AND AMENDMENT NO. 140 TO FACILITY OPERATION LICENSE NO. DPR-60 NORTHERN STATES POWER COMPANY PRAIRIE ISLAND NUCLEAR GENERATING PLANT, UNITS 1 AND 2 DOCKET NOS. 50-282 AND 50-306
1.0 INTRODUCTION
By a letter dated November 1O, 1999, as supplemented February 25, 2000, Northern States Power Company (NSP or the licensee) requested changes to the Technical Specifications (TSs) for the Prairie Island Nuclear Generating Plant, Units 1 and 2. The licensee proposed to change TS Section 4.12, "Steam Generator Tube Surveillance," to incorporate the revised acceptance criterion for elevated F-star (EF*) distance. The proposed change is the result of corrections made to tubesheet bending calculations, which are documented in Westinghouse Topical Report WCAP-14255, Revision 2 (proprietary), "F* and Elevated F* Tube Plugging Criteria for Tubes with Degradation in the Tubesheet Region of the Prairie Island Units 1 and 2 Steam Generators."
Current TS 4.12.0.1.(1) specifies the EF* distance of 1.62 inches in accordance with Amendment Nos. 137 and 128, respectively for Prairie Island, Units 1 and 2, issued on August 13, 1998. The licensee proposed to revise the EF* distance to 1.67 inches.
The February 25, 2000, supplemental letter provided clarifying information that did not change the staff's initial proposed no significant hazards consideration determination and did not expand it beyond the scope of the original Federal Register notice.
2.0 EVALUATION The steam generators at Prairie Island, Units 1 and 2, are Westinghouse Model 51 steam generators. The steam generator tubes were fabricated with mill-annealed alloy 600 material.
The segment of tube in the tubesheet has a factory-installed partial hardroll expansion joint, which occupies a length of about 2.75 inches from the tube end.
Over time, degradation has occurred at the original factory-installed hardroll expansion joints of the tube inside the tubesheet. Degraded expansion joints can be repaired by instal!ing additional hardroll expansion joints in the tube inside the tubesheet above the original factory-installed expansion joints. The additional hardroll expansion joint is installed by a mechanical
expander (roller) that is inserted into the tube. At the intended location, the expander pushes the tube wall circumferentially against the tubesheet bore to form a roll expansion joint. T he roller has an effective length of 1.8 inches. In actual practice, the field-installed hardroll expansion joint is 2 inches long.
The EF* criteria are applicable to the hardroll expansion joints installed above the midplane of the tubesheet. One element of the criteria is the EF* distance. The EF* distance, as defined in TS 4.12.D.1.(1), is the distance from the bottom of the upper hardroll transition toward the bottom of the tubesheet. The EF* criteria require that tube defects are not permitted within the EF* distance.
The technical basis for the EF* criteria is that a defect-free region having a length equal to the EF* distance in the expansion joint will provide sufficient structural strength to resist axial pullout loads developed by pressure, thermal, and/or mechanical forces during normal operation, test, upset and faulted conditions. The axial pullout loads acting on the tub~s are resisted by frictional forces developed by the elastic preload that exists between the tube and the tubesheet at the hardroll expansion joint. Westinghouse has performed structural calculations and conducted tests on mockups to qualify the current EF* distance (1.62 inches).
The licensee has also demonstrated that EF* tubes have adequate integrity in terms of primary-to-secondary side leakage. The staff approved the EF* criteria, including the current EF* distance of 1.62 inches, via Amendment Nos. 137 and 128.
Subsequent to the issuance of Amendment Nos. 137 and 128, the licensee determined that the EF* distance requires a revision as necessitated by correcting a minor error in calculating the EF* distance. In the original tubesheet bending calculations, the secondary side pressure was incorrectly applied to the tubesheet hole surface, resulting in a higher contact pressure than necessary and yielded an EF* distance that was slightly shorter than desired (1.62-inches rather than 1.67 inches). The difference is 0.050 inches or about 3 percent of the revised EF*
distance. The licensee stated that there is sufficient safety margin in the original EF* distance calculation which more than offsets the difference of 0.050 inches.
Nevertheless, the licensee proposed that the EF* distance, as specified in TS 4.12.D.1.(1), be revised from the current 1.62 inches to 1.67 inches based on the revised calculations. The staff finds that the revised EF* distance of 1.67 inches is acceptable since it was calculated in accordance with the previously approved analytical methodology as described in the staff's safety evaluation supporting Amendment Nos. 137 and 128. Also, the licensee has shown that a tube with the revised EF* distance applied to the additional hardroll expansion joint satisfies the safety margins in Regulatory Guide 1.121, "Bases for Plugging Degraded PWR Steam Generator Tubes," issued in August 1976.
Currently, there are 19 EF* tubes remaining in service in Prairie Island, Unit 1, and none in service in Prairie Island, Unit 2. The 19 EF* tubes are located in steam generator 11 with a 2.0-inch roll expansion joint. The licensee has inspected field-installed hardroll expansion joints and found no degradation. The licensee verified that each field-installed hardroll expansion joint in the EF* tubes has a length of 2.0 inches. The expansion joint length of 2.0 inches in the existing EF* tubes is greater than the proposed EF* distance of 1.67 inches; therefore, the existing EF* tubes with defect-free hardroll joints meet the structural integrity requirements of TS 4.12.
The EF* distance in the current TS excludes measurement uncertainty. The licensee stated that the measurement uncertainty was not included in the TS because the additional hardroll expansion joint has a physical length of 2.0 inches, which is a function of the roller tooling and is longer than the EF* distance of 1.67 inches. In addition, the licensee conducted a study to determine accuracy of flaw location measurements relative to the bottom of the upper roll transition. The study contained 16 flaw samples with the participation of 5 data analysts. The study found that flaw location measurements were less than the actual distance from the bottom of the hardroll upper transition to the crack tip. Thus, the measured distance of the defect-free region of the hardroll expansion joint (i.e., EF* distance) is expected to be less than the actual defect-free region of the hardroll expansion joint. The measured EF* distance is, therefore, believed to be conservative. The average difference between the measured and actual EF* distance was about 0.2 inches.
The licensee stated that any tube with a crack indication less than 1.87 inches (i.e., the EF*
distance of 1.67 inches plus measurement uncertainty of 0.2 inches) below the bottom of the upper hardroll would be repaired or removed from service. The licensee stated that, in practice, if a de.feet exists anywhere in the additional hardroll expansion joint, the affected tube is repaired or plugged. The staff finds that the licensee's approach to disposition degradation in the additional hardroll joints bounds the EF* distance plus measurement uncertainty and, therefore, is acceptable.
3.0 STATE CONSULTATION
In accordance with the Commission's regulations, the Minnesota State official was notified of the proposed issuance of the amendments. The State official had no comments.
4.0 ENVIRONMENTAL CONSIDERATION
The amendments change a requirement with respect to installation or use of a facility component located within the restricted area as defined in 10 CFR Part 20. The NRG staff has determined tha,t the amendments involve no significant increase in the amounts, and no significant change in the types, of any effluents that may be released offsite, and that there is no significant increase in individual or cumulative occupational radiation exposure. The Commission has previously issued a proposed finding that the amendments involve no significant hazards consideration and there has been no public comment on such finding (65 FR 9010). Accordingly, the amendments meet the eligibility criteria for categorical exclusion set forth in 10 CFR 51.22(c)(9). Pursuant to 10 CFR 51.22(b), no environmental impact statement or environmental assessment need be prepared in connection with the issuance of the amendments.
5.0 CONCLUSION
The Commission has concluded, based on the considerations discussed above, that (1) there is reasonable assurance that the health and safety of the public will not be endangered by operation in the proposed manner, (2) such activities will be conducted in compliance with the Commission's regulations, and (3) the issuance of the amendments will not be inimical to the common defense and security or to the health and safety of the public.
Principal Contributor: J. Tsao Date: Apr i l 19 , 2000
Prairie Island Nuclear Generating Plant, Units 1 and 2 cc:
J. E. Silberg, Esquire Site Licensing Shaw, Pittman, Potts and Trowbridge Prairie Island Nuclear Generating Plant 2300 N Street, N. W. Northern States Power Company Washington, DC 20037 1717 Wakonade Drive East Welch, MN 55089 Plant Manager Prairie Island Nuclear Generating Plant Tribal Council Northern States Power Company Prairie Island Indian Community 1717 Wakonade Drive East ATTN: Environmental Department Welch, MN 55089 5636 Sturgeon Lake Road Welch, MN 55089 Adonis A. Neblett Assistant Attorney General Site General Manager
- office of the Attorney General Prairie Island Nuclear Generating Plant 455 Minnesota Street Northern States Power Company Suite 900 1717 Wakonade Drive East St. Paul, MN 55101-2127 Welch, MN 55089 U.S. Nuclear Regulatory Commission Resident Inspector's Office 1719 Wakonade Drive East Welch, MN 55089-9642 Regional Administrator, Region Ill U.S. Nuclear Regulatory Commission 801 Warrenville Road Lisle, IL 60532-4351 Mr. Stephen Bloom, Administrator Goodhue County Courthouse Box 408 Red Wing, MN 55066-0408 Commissioner Minnesota Department of Commerce 121 Seventh Place East Suite 200 St. Paul, MN 55101-2145 January 2000
UNITED STATES NUCLEAR REGULATORY COMMISSION WASHINGTON, D.C. 20555-0001 NORTHERN STATES POWER COMPANY DOCKET NO. 50-282 PRAIRIE ISLAND NUCLEAR GENERATING PLANT, UNIT 1 AMENDMENT TO FACILITY OPERATING LICENSE Amendment No. 149 License No. DPR-42
- 1. The Nuclear Regulatory Commission (the Commission) has found that:
A. The application for amendment by Northern States Power Company (the licensee) dated November 1O, 1999, as supplemented February 25, 2000, complies with the standards and requirements of the Atomic Energy Act of 1954, as amended (the Act), and the Commission's rules and regulations set forth in 10 CFR Chapter I; B. The facility will operate in conformity with the application, the provisions of the Act, and the rules and regulations of the Commission; C. There is reasonable assurance (i) that the activities authorized by this amendment can be conducted without endangering the health and safety of the public, and (ii) that such activities will be conducted in compliance with the Commission's regulations; D. The issuance of this amendment will not be inimical to the common defense and security or to the health and safety of the public; and E. The issuance of this amendment is in accordance with 10 CFR Part 51 of the Commission's regulations and all applicable requirements have been satisfied.
- 2. Accordingly, the license is amended by changes to the Technical Specifications as indicated in the attachment to this license amendment, and paragraph 2.C.(2) of Facility Operating License No. DPR-42 is hereby amended to read as follows:
Technical Specifications The Technical Specifications contained in Appendix A, as revised through Amendment No. 149 , are hereby incorporated in the license. The licensee shall operate the facility in accordance with the Technical Specifications.
- 3. This license amendment is effective as ot its date of its issuance and shall be implemented within 30 days of the date of issuance.
FOR THE NUCLEAR REGULATORY COMMISSION G}~()__ w. -~ ~
Claudia M. Craig, Chief, Section 1 Project Directorate Ill Division of Licensing Project Management Office of Nuclear Reactor Regulation
Attachment:
Changes to the Technical Specifications Date of Issuance: April 19, . 2000
ATTACHMENT TO LICENSE AMENDMENT NO. 149 FACILITY OPERATING LICENSE NO. DPR-42 DOCKET NO. 50-282 Replace the following page of the Appendix A Technical Specifications with the attached revised page. The revised page is identified by amendment number and contains a marginal line indicating the area of change.
REMOVE INSERT TS 4.12-5 TS 4.12-5
TS.4.12-5 (j) F* Distance is the distance from the bottom of the hardroll transition toward the bottom of the tubesheet that has been conservatively determined to be 1 . 07 inches (not including eddy current uncertainty). The F* distance applies to roll expanded regions below the midplane of the tubesheet (k) F* Tube is a tube with degradation, below the F* distance ,
equal to or greater than 40%, and not degraded (i . e., no indications of cracking) within the F* distance.
(1) EF* Distance is the distance from the bottom of the upper hardroll transition toward the bottom of the tubesheet that has been conservatively determined to be 1.67 inches (not including eddy current uncertainty),
- EF* distance applies to roll .
expanded regions when the top of the additional roll expansion is 2 . 0 inches or greater down from the top of the tubesheet (m) EF* Tube is a tube with degradation , below the EF* distance, equal to or greater than 40%, and not degradedh~i.e., no indications of cracking) within the EF* . distance.
- 2. The steam generator shall be determined OPERABLE after completing the corresponding actions (plug or repair by sleeving all tubes exceeding the repair limit and all tubes containing through-wall cracks or classify as F* or EF* tubes) required by Tables TS . 4.12-1 and TS . 4.12-2.
3 . . Tube repair, after April 1, 1999 , using Combustion Engineering welded sleeves shall be in accordance with the methods described in the following: .
CEN-629-P, Revision* 03-P, "Repair of Westinghouse Series 44 and 51 Steam Generator Tubes Using Leak Tight Sleeves":
4 . Tube Support Plate Repair Limit is used for the disposition of a steam generator tube for continued service that is experiencing predominantly axially oriented outside diameter stress corrosion cracking confined within the thickness of the tube support plates.
At tube support plate intersections, the repair limit is based on maintaining steam generator serviceability as described below: *
- a. Steam genera-tor tubes, whose degradation is attributed to outside diameter stress corrosion cracking within the bounds of the tube support plate with bobbin voltages less than or equal to 2.0 volts will be allowed to remain in service.
- b. Steam generator tubes, whose degradation is attributed to outside diameter stress corrosion cracking within the bounds of the tube support plate with a bobbin voltage greater than 2.0 volts, will be repaired or plugged, except as noted in Specification 4.1~ . D.4.c below.
PRAIRIE ISLAND UNIT~ Amendment No. U'*,149 PRAIRIE ISLAND UNIT 2 Amendment No. tiZ,140
UNITED STATES NUCLEAR REGULATORY COMMISSION WASHINGTON, D.C. 20555-0001 NORTHERN STATES POWER COMPANY DOCKET NO. 50-306 PRAIRIE ISLAND NUCLEAR GENERATING PLANT. UNIT 2 AMENDMENT TO FACILITY OPERATING LICENSE Amendment No. 140 License No. DPR-60
- 1. The Nuclear Regulatory Commission (the Commission) has found that:
A. The application for amendment by Northern States Power Company {the licensee) dated November 1O, 1999, as supplemented February 25, 2000, complies with the standards and requirements of the Atomic Energy Act of 1954, as amended (the Act), and the Commission's rules and regulations set forth in 10 CFR Chapter I; B. The facility will operate in conformity with the application, the provisions of the Act, and the rules and regulations of the Commission; C. There is reasonable assurance (i) that the activities authorized by this amendment can be conducted without endangering the health and safety of the public, and (ii) that such activities will be conducted in compliance with the Commission's regulations; D. The issuance of this amendment will not be inimical to the common defense and security or to the health and safety of the public; and E. The issuance of this amendment is in accordance with 10 CFR Part 51 of the Commission's regulations and all applicable requirements have been satisfied.
- 2. Accordingly, the license is amended by changes to the Technical Specifications as indicated in the attachment to this license amendment, and paragraph 2.C.{2) of Facility Operating License No. DPR-60 is hereby amended to read as follows:
Technical Specifications The Technical Specifications contained in Appendix A, as revised through Amendment No. 140 , are hereby incorporated in the license. The licensee shall operate the facility in accordance with the Technical Specifications.
- 3. This license amendment is effective as of its date of its issuance and shall b$
implemented within 30 days of the date of issuance.
FOR THE NUCLEAR REGULATORY COMMISSION
~~a:.~f:~~
Project Directorate Ill Division of Licensing Project Management Office of Nuclear Reactor Regulation
Attachment:
Changes to the Technical Specifications Date of Issuance: April 19, 2000
ATTACHMENT TO LICENSE AMENDMENT NO. 140 FACILITY OPERATING LICENSE NO. DPR-60 DOCKET NO. 50-306 Replace the following page of the Appendix A Technical Specifications with the attached revised page. The revised page is identified by amendment number and contains a marginal line indicating the area of change.
REMOVE INSERT TS 4.12-5 TS 4.12-5
. (
TS.4 . 12-5 (j) F
- Distance is the distance from the bottom of the hardrol l transition toward the bottom of the tubesheet that has been conservatively determined to be 1.07 inches (not including eddy current uncerta~nty). The F* distance applies to roll expanded regions below the midplane of the tubesheet (k) F* Tube is a tube with degradation, below the F* distance, equal to or greater than 40% , and not degraded (i.e., no indications of cracking) within the F* distance.
(1) EF
- Distance is the distance from the bottom of the upper hardroll transition toward the bottom of the tubesheet that has been conservatively determined to be 1.67 inches (not including eddy current uncertainty).
- EF* distance applies to roll .
expanded regions when the top of the additional roll expansion is 2 . 0 inches or greater down from the top of the tubesheet (m) EF* Tube is a tube with deg~adation, below the EF* distance, equal to or greater than 40% , and not degraded,/i . e., no indications of cracking) within the EF* distance. . .
- 2. The steam generator shall be determined OPERABLE after completing the corresponding actions (plug or repair by sleeving all tubes exceeding the repair limit and all tubes containing through - wall cracks or classify as F* or EF* tubes) required by Tables TS.4.12-1 and TS.4.12-2.
- 3. Tube repair, after April 1 , 1999, using Combustion Engineering welded sleeves shall be in accordance with the methods described in the following: .
CEN-629-P, Revision 03-P, "Repair of Westinghouse Series 44 and 51 Steam Generator Tubes Using Leak Tight Sleeves";
- 4. Tube Support Plate Repair Limit is used for the disposition
- of a steam generator tube for continued service that is experiencing predominantly axially oriented outside diameter stress corrosion cracking confined within the thickness o~ the tube support plates.
At tube support plate intersections , the repair limit is based on maintaining steam generator serviceability as described below:*
- a. Steam genera.tor tubes, whose degradation is attributed to outside diameter stress corrosion cracking within the bounds of the tube support plate with bobbin voltages less than or equal to 2.0 volts will be allowed to remain in service.
- b. Steam generator tubes, whose degradation is attributed to outside diameter stress corrosion cracking within the bounds of the tube support plate with a bobbin voltage greater than 2.0 volts, will be repaired or plugged, except as noted in Specification 4.1~ . D.4 . c below.
PRAIRIE ISLAND UNIT 1 Amendment No. t~~,149 PRAIRIE ISLAND UNIT 2 Amendment No. t'/J$,140