ML18038A442

From kanterella
Jump to navigation Jump to search
Special Rept:On 881227,inoperability of Seismic Monitoring Instrumentation Occurred.Instrument Struck by Personnel Installing Insulation on Pipe or Performing Sys Walkdowns. Problem Rept Written on 890112 for Indications on Plates
ML18038A442
Person / Time
Site: Nine Mile Point Constellation icon.png
Issue date: 02/06/1989
From: Joseph Willis
NIAGARA MOHAWK POWER CORP.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NMP-44061, NUDOCS 8902090312
Download: ML18038A442 (8)


Text

IICCE~RATED DTRIBllTI04 DEMO%STTIO.'i SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)

ACCESSION NBR:8902090312 DOC.DATE: 89/02/06 NOTARIZED: NO DOCKET N

FACIL:50-410 Nine Mile Point Nuclear Station, Unit 2, Niagara Moha 05000410 AUTH.NAME AUTHOR AFFILIATION WILLIS,J.L.

Niagara Mohawk Power Corp.

RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk).

SUBJECT:

Special rept:on 881227,inoperability of seismic monitoring instrumentation occurred.

DISTRIBUTION CODE IE22D COPIES RECEIVED:LTR ENCL SIZE:

TITLE: 50.73 Licensee Event Report (LER), Incident Rpt, etc.

NOTES RECIPIENT ID CODE/NAME PD1-1 LA HAUGHEY,M INTERNAL: ACRS MICHELSON ACRS WYLIE AEOD/DSP/TPAB ARM/DCTS/DAB NRR/DEST/ADE 8H NRR/DEST/CEB 8H NRR/DEST/ICSB 7

NRR/DEST/MTB 9H NRR/DEST/RSB 8E NRR/DLPQ/HFB 10 NRR/DOEA/EAB 11 NRR/DREP/RPB 10 NUDOCS-ABSTRACT RES/DSIR/EIB RGN1 FILE 01 EXTERNAL: EG&G WILLIAMS,S H ST LOBBY WARD NRC PDR NSIC MAYS,G'OPIES LTTR ENCL 1

1' 1

1 1

1 1

1 1

1 1

1 1

1 1

1 1

1 1

1 1

1 1

1 1

2 2

1 1

1 1

1 1

4 4

1 1

1 1

1 1

RECIPIENT ID CODE/NAME PD1-1 PD BENEDICT,R ACRS MOELLER AEOD/DOA AEOD/ROAB/DSP DEDRO NRR/DEST/ADS 7E NRR/DEST/ESB 8D NRR/DEST/MEB 9H NRR/DEST/PSB 8D NRR/DEST/SGB 8D NRR/DLPQ/QAB 10 NRR/DREP/RAB 10 R~ ~

RES/DSR/PRAB FORD BLDG HOY,A LPDR NSIC HARRIS,J COPIES LTTR ENCL 1

1 1

1 2

2 1

1 2

2 1

1 1

0 1

1 1

1 1

1 1

1 1

1 1

1 1

1 1

1 1

1 1=-

1 1

1 1

1 R

I S

h NOTE 'IO ALL "RIDS" RECIPZBQS:

4 PLEASE HELP US 10 REDUCE HASTE!

CDMZACI'IHE DOCUMENI'ONIRDL DESK, ROOM Pl-37 (EXT. 20079)

TO ELIMINATE YOUR NAME FRY DIFHKBUTION LISTS FOR DOCUMEMIS YOU DON'T NEED)

TOTAL NUMBER OF COPIES REQUIRED:

LTTR 46 ENCL 45

NMP 44061 NIAGARAMOHAWKPOWER CORPORATION/300 ERIE BOULEVARDWEST. SYRACUSE. N.Y, I3202/TELEPHONE (315) 474-I5I I February 6, 1989 U. S. Nuclear Regulatory Commission Attention:

Document Control Desk washington, DC 20555 Re:.

Docket No. 50-410 SPECIAL REPORT Gentlemen:

In accordance with the Nine Mile Point Unit 2 (NMP2) Technical Specification -(TS) 3.3.7.2, ACTION statement a.,

we are submitting the following Speci"al Report concerning the inoperability of the Seismic Monitoring Instrumentation (Specifically - the Triaxial Peak Accelerograph, High Pressure Core Spray Piping).

EXECUTIVE

SUMMARY

'The Triaxial Peak Accelerograph (located on the High Pressure Core Spray (CSH) Piping) is installed and maintained as required by the NMP2 TS.

This unit has indications of high seismic accelerations in its present location due to non-seismic events.

Thus, no TS credit is being taken for this unit.

This triaxial peak accelerograph is being mounted in an alternate location designated by Niagara Mohawk Power Corporation (NMPC) Engineering.

This unit is expected to function properly and provide information on seismic activity.

The selected location is not the location specified in the NMP2 TS.

Thus, NMPC is not taking credit for meeting TS requirements with this accelerograph.

NMPC plans to identify an acceptable location for this accelerograph and to make the appropriate hardware and TS changes by the end of the first refueling outage.

EVENT DESCRIPTION On December 27, 1988 at 1647 hours0.0191 days <br />0.458 hours <br />0.00272 weeks <br />6.266835e-4 months <br /> with the reactor in cold shutdown (Operational Condition 4), reactor coolant at approximately 163 degrees Fahrenheit and atmospheric

pressure, the CSH Triaxial Peak Accelerograph (2ERS-PAC28) was declared inoperable.

It was found inoperable during the performance of procedure N2-ISP-ERS-R102 (Operating Cycle Channel Calibration of Seismic Monitoring Triaxial Peak Accelerographs Instrument Channels).

The vertical (v), transverse (t), and longitudinal (1) permanent record plates were found to have indications that did not result from seismic activity.

Page 2

NMP44061 CAUSE OF THE EVENT The cause of the indications on the v, t, 1 record plates is unknown.

It is hypothesized that the instrument was struck by personnel installing insulation on the pipe or performing system walkdowns.

ACTIONS TAKEN A Problem Report (PR) was written on January 12, 1989 for the indications on the v, t, 1 permanent record plates.

The PR was written to have NMPC Engineering consider relocating 2ERS-PAC2B.

The PR's Description states that:

During performance 'of TS required surveillances it was discovered that all record plates had two to four gravity accelerations (2 to 4g's) marks scribed on them.

This marking is the product of background noise.

This noise is of such a magnitude that had there been a design basis earthquake, it would not have been observable on the permanent record plates.

NMPC Engineering determined that CSH has been operated approximately twice during the time that the 2ERS-PAC2B was installed. (Inspection of the record plate etchings of 2ERS-PAC2B also. indicate 2 or 3 cycles).

Engineering also determined that the recorded 2 to 4g's (during these 2 or 3 cycles) were not the result of CSH operation.

This determination is based on the following observations:

CSH piping is filled with water at al.l times, including portions of the piping downstreams of the check valve 2CSH*AOV108.

Analyzed conditions, for all non-seismic transients, show accelerations less than 0.8 g in all directions.

Pre-operation te'sting and the power ascension vibration program, both produced satisfactory results on the same piping where the instrument is presently located.

A test has been performed in the Instrument 8 Control

( I8C) shop by'ngineering and I8C.

2ERS-PAC2B was firmly mounted with, fresh record plates and lightly tapped in all three directions with a human fist.

The results were measurements up to 4 g's in each direction.

This demonstrates the consequences had the instrument been accidentally struck by personnel installing insulation on the pipe or performing system walkdowns in the area.

NMPC Engineering will develop a temporary modification to move 2ERS-PAC2B to the CSH line just outside the primary containment penetration and just up stream of the CSH injection valve (2CSH*MOV107) on the 292 foot elevation of the. NMP2 Secondary Containment.

The I8C technicians will periodically examine the record plates (at 3 months and again at 6 months) to determine if this location has an acceptably low level of background vibration.

It is expected to be acceptable.

If it turns out to be so, 2ERS-PAC2B will remain at this location and a Technical Specification change will be submitted to the Nuclear Regulatory Commission to change Table 3.3.7.2-1, item 2.b to reflect this new location.

If it is not satisfactory, then another new location will be found.

Page 3

NMP44061 We expect to complete this process of determining the new location, making necessary hardware changes and submitting a

TS change before the end of the first refueling outage.

Si nc ere 1y, J.

L. Willis General Superintendent Nuclear Generation JLW/AD/cjm (1598u) xc: Regional Administrator, Region 1

W. A. Cook, Resident Inspector