ML18036B255

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Insp Repts 50-259/93-07,50-260/93-07 & 50-296/93-07 on 930218-0319.Violations Noted.Major Areas Inspected: Surveillance Observation,Maint Observation,Operational Safety Verification,Mods & Reportable Occurrences
ML18036B255
Person / Time
Site: Browns Ferry  
Issue date: 04/14/1993
From: Kellogg P, Patterson C
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18036B253 List:
References
50-259-93-07, 50-259-93-7, 50-260-93-07, 50-260-93-7, 50-296-93-07, 50-296-93-7, NUDOCS 9304300055
Download: ML18036B255 (27)


See also: IR 05000259/1993007

Text

P0

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W.

ATLANTA,GEORGIA 30323

Report

NoseI

50-259/93-07,

50-260/93-07,

and 50-296/93-07

Licensee:

Tennessee

Valley Authority

6N 38A Lookout Place

1101 Market Street

Chattanooga,

TN

37402-2801

Docket Nos.:

50-259,

50-260,

and 50-296

License Nos.:

DPR-33,

DPR-52,

and

DPR-68

Facility Name:

Browns Ferry Units 1,

2,

and

3

Inspection at Browns Ferry Site near Decatur,

Alabama

Inspection

Conducted:

February

18

March 19,

1993

Inspector:

a terson,

Sen>or

esi

ent

nspector

ate

igne

Accompanied

by:

J.

Hunday,

Resident

Inspector

R. Husser,

Resident

Inspector

J. Hathis, Project Inspector

E.

, License

Examiner

Approved by:

au

Re

tor Proj ct

, Section

4A

Division of Reactor Projects

SUMMARY

ate

Soigne

Scope:

This routine resident

inspection

included surveillance

observation,

maintenance

observation,

operational

safety

- verification, modifications, Unit 3 restart activities,

radiological controls,

and reportable

occurrences.

One hour of backshift coverage

was routinely worked during the

work week.

Deep backshift inspections

were conducted

on

February

21,

February

22,

and March 6,

1993.

9304300055

9304ib

PDR

" ADOCK 05000259

PDR

Unit 2 was in day 50 of a

100 day refueling outage at the end of

the report period,

paragraph

four.

The schedule

was

changed

from

119 days to 100 days

due to the shutdown .of other

TVA nuclear

plants.

No work scope reductions

were made.

One violation was identified for failure to comply with radiation

protection procedures,

paragraph

seven.

Three

examples of failing

to comply with radiation work permits were observed

by a

NRC

inspector during

a single day.

. One unresolved

item was identified concerning the need for a

10

CFR 50.59 evaluation for the recirculation

pump shaft replacement,

paragraph five.

The licensee

procedure

allows replacement

of a

like for like component without an evaluation.

However, the

procedure

may not be adequate

to address

the specifics

from a

safety standpoint.

This issue will require further evaluation to

determine

the adequacy of the licensee's

program.

REPORT DETAILS

Persons

Contacted

Licensee

Employees:

  • J
  • O

J.

  • J
  • R

D.

  • M
  • J
  • M

+A.

  • C
  • Q
  • J

A.

Bynum, Vice President,

Nuclear Operations

Zeringue,

Vice President

Scalice,

Plant Manager

Rupert,

Engineering

and Modifications Manager

Baron, Site guality and Licensing Manager

Nye, Recovery Manager

Herrell, Operations

Manager

Maddox,

Engineering

Manager

Bajestani,

Technical

Support Manager

Sorrell, Special

Programs

Manager

Crane,

Maintenance

Manager

Pierce,

Acting Licensing Manager

Corey, Site Radiological

Control Manager

Brittain, Site Security Manager

Other licensee

employees

or contractors

contacted

included licensed

.

reactor operators,

auxiliary operators,

craftsmen,

technicians,

and

public safety officers;

and quality assurance,

design,

and engineering

personnel.

NRC Personnel:

  • P'. Kellogg, Section Chief
  • C. Patterson,

Senior Resident

Inspector

  • J. Munday, Resident

Inspector

  • R. Musser,

Resident

Inspector

  • J. Mathis, Project Inspector

"Attended exit interview

Acronyms

and initialisms used throughout this report are listed in the

last paragraph.

Surveillance Observation

(61726)

'

The inspectors

observed

and/or reviewed the performance of required SIs.

The inspections

included reviews of the SIs for technical

adequacy

and

conformance to TS, verification of test instrument calibration,

observations

of the conduct of testing,

confirmation of proper removal

from service

and return to service of systems,

and reviews of test data.

The inspectors

also verified that

LCOs were met, testing

was

accomplished

by qualified personnel,

and the SI's were completed within

the required frequency.

The following SIs were reviewed during this

reporting period:

O-SI-4.10.c.2,

Fuel

Pool Coolant Chemistry

On February

21,

1993, the inspector

performed

a review of

previously performed surveillance instructions for the chemical

analysis of the spent fuel pool.

This procedure,

O-SI-4.10.c.2;-

satisfies

TS requirement

4. 10.c.2 for all three units.

More

specifically, the fuel pool coolant is analyzed for chloride ion

concentration

and conductivity.

The limits -for conductivity and

chloride ion concentration

specified in the

TS are

10 pS/cm

and

0.5

ppm respectively.

While reviewing the data from the February

20,

1993 analysis,

the chloride ion concentration for all three

units was entered

as greater

than

.5ppm (approximately

.Sppm).

Previous

days readings

were noted to be much lower (by a factor of

one thousand).

The inspector

brought this matter to the attention

of the Chemistry Shift Supervisor.

The supervisor

informed the

inspector that the entries

in question

were in error in that the

actual chloride ion concentration

analyses

were performed in ppb

and the chemistry technician

had not converted the data to ppm.

The supervisor

on shift informed the inspector that the data would

be corrected to reflect the proper units.

The improper data

had

been

approved

as satisfactory

by the

technician

and the chemistry shift supervisor.

The inspector

, discussed

this matter with the Chemistry Superintendent

the

following morning.

The Chemistry Superintendent

indicated that

the data

had

one final review to be performed before being turned

into the surveillance coordinator.

He felt that this deficiency

would have

been detected

at this time.

To prevent another

occurrence of this type, the Chemistry Superintendent

discussed

this matter with the appropriate

chemistry personnel

and changed

procedure 0-SI-4. 10.c.2 to specifically convert the chloride ion

concentration

from ppb to ppm.

The inspectors will continue to

monitor surveillances

performed within the chemistry area.

SI-4.2.K.2.A(FT), Reactor Building Vent Exhaust Monitor

2-RH-90-250, Detector Channel

Functional Test

On March 11,

1993 the inspector

observed

the performance of

portions of the SI-4.2.K.2.A(FT), Reactor Building Vent Exhaust

Monitor 2-RH-90-250, Detector Channel

Functional Test.

This test

provides for the instrument functional test of the Reactor

Building Exhaust

Noble Gas Monitor Detector Channel

and partially

the requirements

specified in TS Tables 3.2.K and 4.2.K.

The

inspector noted that the current revision of the procedure

was

being used

and was being followed properly.

The test performers

appeared

knowledgeable

on the system

and the procedure.

The

inspector reviewed the completed surveillance

procedure

and noted

the surveillance

was completed satisfactorily

and

had received the

appropriate

reviews,

The inspector noted

no deficiencies

in this

area.

No violations or deviations

were identified in the Surveillance

Observation

area.

1

Haintenance

Observation

(62703)

Plant maintenance activities were observed

and/or reviewed for selected

safety-related

systems-

and components

to ascertain

that they were

conducted

in accordance

with requirements.

The following items were

considered

during these

reviews:

LCOs maintained,

use of approved

procedures,

functional testing and/or calibrations

were performed prior

to returning components

or systems

to service,

gC records

maintained,

activities accomplished

by qualified personnel,

use of properly

certified parts

and materials,

proper

use of clearance

procedures,

and

implementation of radiological controls

as required.

'I

Work documentation

(HR,

WR,

and

WO) were'eviewed

to determine

the

status of outstanding

jobs

and to assure

that priority was assigned

to

safety-related

equipment

maintenance

which might affect plant safety.

The inspectors

observed

the following maintenance activities dut ing this

reporting period:

a

~

Hydraulic Control Unit Haintenance

Op Harch 9,

1993 the inspector

observed

maintenance

being

performed

on hydraulic control units 42-51

and 46-51.

The scram

pilot valves were being rebuilt and their internals

replaced.

The

'aintenance

personnel

were knowledgeable

about the task

and

had

no

difficulties in its performance.

The job foreman

was present

to.

verify foreign material

exclusion

and proper placement of valve

internals.

The inspector noted

no discrepancies.

b.

Underground

Leak

During this period

an underground

leak developed

at the north side

of the

RHRSW building.'

tower crane

had

been

parked in this

location

and was

assumed

to be the cause of the leak.

The

inspector

was

aware that the 'tower crane loading

had

been

reviewed

as part of the lifting performed for the Unit 3

CCW pump

refurbishment.

The inspector

reviewed

DCN S-17560

and calculation

CD-(I0303-

921562,

4100M Crawler Hounted

Crane Evaluation for Lifting Unit 3

CCW Pumps.

The inspector

was particularly concerned

that

underground

safety piping as the

RHRSW piping could be the source

of water.

The

DCN determined that the lifting was acceptable

provided the crane

was located at a'ertain position indicated

on

a drawing

and the foundation

was prepared.

The preparation

consisted of placement

and compaction of crushed

stone and-

placement of timbers underneath

the crane tracks for load

distribution.

The foundation preparation

was necessary

because

of

the combined weight of the

CCW pump and crane.

V

'

However,

in this case

the unloaded

crane

was not parked to use the

benefit of the foundation preparation.

On page

25 of the

calculation,

the worst case

loading

on the

CCW conduit

w'as

evaluated

to occurr when the crane

was not loaded

and the matting

was not considered.

This would occur

as the crane

was

moved into

or out of position.

The loading of the crane,

in this worse

case

condition,

was still below loading of a proposed railroad tracks

considered

in the original design.

The licensee

moved the crane

away from the north side of the

RHRSW

building near the road.

An incident investigation

was initiated

for the leak.

, In the calculation the following embedded

items were reviewed:

1)

intake conduits

2)

18 inch

EECW pipe

3)

24 inch

RHRSW pipe

4)

3 inch demineralized

water pipe

5)

12 inch drain pipe

It was determined that both the

18 inch

EECW pipe

and

24 inch

RHRSW pipes

have protective sleeves.

The

18 inch

EECW pipe has

a

24 inch di'ameter sleeve.

The 24 inch

RHRSW pipe= has

a 30 inch

diameter'sleeve.

The'alculations

performed concluded that the

stresses

were significantly below the allowed.

The inspector

concluded that the crane loading

on the

embedded

piping and

particularly safety piping had

been considered.

The inspector

will continue to follow this issue with completion of the leak

repair

and II completion.

No violations or deviations

were identified in the Maintenance

Observation

area.

Operational

Safety Verification (71707)

The

NRC inspectors

followed the overal,l plant status

and any significant

safety matters related to plant operations.

Daily discussions

were held

with plant management

and various 'members of the plant operating staff.

The inspectors

made routine visits to the control

rooms.

Inspection

observations

included instrument readings,

setpoints

and recordings,

status of operating

systems,

status

and alignments of emergency

standby

systems,

verification of onsite

and offsite power supplies,

emergency

power sources

available for automatic operation,

the purpose of

temporary tags

on equipment controls

and switches,

annunciator

alarm

status,

adherence

to procedures,

adherence

to LCOs, nuclear instruments

operability, temporary alterations

in effect, daily journals

and logs,

stack monitor recorder traces,

and control

room manning.

This

inspection activity also included

numerous

informal discussions

with

operators

and supervisors.

General

plant tours were conducted.

Portions of the turbine buildings,

each reactor building',

and general

plant areas

were visited.

Observations

included valve position

and system alignment,

snubber

and

hanger conditions,

containment isolation alignments,

instrument

readings,

housekeeping,

power supply

and breaker alignments,

radiation

and contaminated

area controls,

tag controls

on equipment,

work

activities in progress,

and radiological protection controls.

Informal

discussions

were held with selected

plant personnel

in their functional

areas

during these tours.

a

~

Unit Status

Unit 2 was in day 50 of a

100 day refueling outage at the

end of

the report period.

The outage

schedule

was changed

from 119 days

to 100 days during this period.

The next major milestone will be

e'stablishment

of secondary

containment

scheduled for April 10,

1993.

b.

C.

Clearance

Tag Placement

on Electrical

Breakers

While touring the turbine building on March 3,

1993,

the inspector

noted

an electrician working inside

a 480 volt breaker

which had

a

clearance

tag hanging

on the compartment

door.

The inspector

had

been told by the Operations

Manager.

several

weeks before that if a

breaker door had

a clearance

tag hanging

on it, the door could not

be opened.

The inspector questioned

the electrician

and

he stated

that this was true for 4

kV breakers

but not for 480 volt

breakers.

A memorandum written by the Operations

Superintendent

dated

February

7,

1993, stated that if a clearance

tag is placed

on

a breaker

compartment

door, the door becomes

the clearance

boundary.

The Maintenance

Manager

was also

asked

about accessing

a breaker

compartment with a clearance

tag hanging

on it and

he

stated that it was all right.

He further stated that discussions

held with the Operations

Superintendent

resulted

in the

aforementioned

memorandum

and the intent was to allow maintenance

to access

breakers

with clearance

tags

hanging

on the door so that

maintenance

could

be performed.

SSP-12.3,

Equipment Clearance

Procedure,

does not contain instructions that specify where to

hang the tag

on breakers.

This matter

was brought to the

attention of the Operations

Manager

who generated

a new memorandum

dated

March 15,

1993,

which stated that if a breaker

door= had

a

clearance

tag

on it, the door could not be opened.

If access

to

the inside of the compartment

was

needed

Operations

would move the

tag to the inside.

This memorandum

should provide the additional

guidance

needed to ensure

safe operation

and breaker

maintenance.

Annual Operating

Report

The inspector

reviewed the Browns Ferry Nuclear Plant Units 1, 2,

and

3 Annual Operating

Report for January

1,

1992 through

December

31,

1992.

The report included

a summary of safety evaluations for

FSAR changes,

procedure

changes,

special

operating conditions,

6

E

special

tests,

temporary alterations,

and plant modifications.

It

also included the

1992 Radiological

Release

Summary,

Occupational

Exposure

Data,

Challenges

to Hain Steam Relief Valves,

and the

Reactor

Vessel

Fatigue

Usage Evaluation.

This report satisfies

the

requirements

of 10

CFR 50.59,

Regulatory

Guide 1. 16 Sections

1.b.(1),

(2),

and

(3)

and

TS Sections 6.9. 1.2

and 6.9.2. 1.

Housekeeping

During the inspection period,

the inspector

performed

an audit of

the licensee's

control of housekeeping.

As a part of this audit,

the inspector evaluated

the'implementation

of procedure

SSP-12.7,

Housekeeping/Temporary

Equipment Control.

This site standard

practice

procedure

delineates

the housekeeping

control practices

and requirements for the plant.

One of the specific requirements

of the procedure

is the designation of a material

control/housekeeping

coordinator.

As

a part of the inspection

effort, the inspector

reviewed the housekeeping

program with this

individual.

The housekeeping

coordinator

and the inspector discussed

the

plant's

housekeeping

program in detail.'

major aspect of the

housekeeping

program is the inspections

performed

by plant

personnel.

The Unit 2 reactor building, turbine building, diesel

generator

buildings

and the intake structure

are divided into 35

zones for daily inspection.

Each

zone

has

a zone inspector,

whose

name is prominently displayed in the zone,

tasked with this daily

inspection.

Once

a week, the inspection of the various

zones

are

documented

on Appendix

C of SSP 12.7

and turned into the

housekeeping

coordinator.

This documentation

is to include

deficiencies

discovered

and associated

corrective actions.

The

appendix

(C) contains

a comprehensive list of housekeeping

deficiencies that the zone inspectors

are to use

as

a guide

when

inspecting their zones.

The inspector

reviewed the results of these

inspections for the

period of November ll, 1992 - Harch 8,

1993.

A mixture of

inspection results

was noted.

While it appeared

that

many zone

inspections

are performed

and documented

thoroughly, other

housekeeping

inspection reports .indicated that documentation

of

inspections

was weak.

The inspector

expressed

this concern to the

housekeeping

coordinator.

The coordinator stated

her awareness

of

this matter

and indicated that the zones

which appeared

from

review of inspection

documentation

to get the least attention

during inspections

were frequently chosen to be inspected

during

the plant managers

weekly walkdown.

Another'spect of this evaluation

was th'e inspector's

walkdown of

the plant for general

housekeeping

practices.

Currently, Unit 2

is in the midst of its cycle

6 refueling outage

and

a great

amount

of equipment is spread

throughout the plant.

Host prevalent of

this equipment is scaffolding.

The inspectors will continue to

tour the plant during the outage

and ensure that the majority of

scaffolding is removed

from above safety related

equipment prior

to startup.

Other items noted during plant tours were welding

bottles that are not currently being utilized.

These

items were

brought to the attention of the licensee.

The overall condition

of housekeeping

for the last 2-3 months

appears

to be in somewhat

of a decline

due to outage activities in Units

2 and 3.

The

inspectors will continue to inspect the licensees'ousekeeping

program to ensure plant conditions

are brought

up to pre-outage

standards.

As the current outage

comes to an end,

the inspectors

will more closely monitor housekeeping

practices

and conditions in

order to help ensure

proper

operation of plant equipment.

e.

Fire Door Blocked Open

On March 10,

1993, at approximately

1730, during

a routine tour of

the control

bay, the inspector

noted that door ¹464,

the Computer

Room fire door on the

1C elevation,

was cracked

open.

The

internal door knob was missing

and the door blocked. open

so that

personnel

could exit the computer

room.

Since the door was fire

rated,

the inspector

asked the

ASOS whether

a

LCO had

been written

on the door.

The

ASOS requested

plant fire protection

personnel

to make this determination.

Plant fire protection determined that

a

LCO was not in effect for the door in question.

Fire Protection

personnel

initiated plant form "Attachment

F" documenting

the

condition.

An hourly fire watch,

as required

by TS 3. 11.G. l.a,

was established.

At the time of the event, all three

Browns Ferry

units were defueled

and this event

was of minor safety

significance.

Plant personnel

need to be reminded that fire rated

assemblies

should not be defeated

without the proper compensatory

actions taken.

Spent

Fuel

Pool

The inspector performed

a review of the licensee's

controls for

the spent fuel pool during the inspection period.

The inspection

effort was performed to ensure that adequate

controls were in

place for the control of spent fuel pool parameters

and that

TS

requirements

for the

SFP being met.

A complete core off load had

been

completed at the

end of the previous inspection period for

the Unit 2 cycle

6 refueling outage.

The inspector

reviewed

TS surveillance

requirements

for the spent

fuel pool water.

TS 4. 10.c. I requires that whenever irradiated

fuel is stored in the spent fuel pool, the water level

and

temperature

shall

be recorded daily.

The inspector verified that

the temperature

of the pool

was being recorded daily in accordance

'ith

procedure

2-SI-2,

Instrument

Check

and Observations.

The

same procedure

contained

the requirements for the recording of the

SFP water level,

however, it did not specify that

a specific water

level

be recorded.

Rather than record

a specific water level, the

procedure directs operations

personnel

to check

a control

room

8

annunciator

("Fuel

Pool

System Abnormal" ) and if the annunciator

is not illuminated, record the

SFP water level 'as normal.

The

fuel pool level switches

and skimmer surge tank level switches

input into this annunciator

and

no direct reading of fuel pool

level is currently available.

The

NRC

questioned

the adequacy of

the

SFP level documentation

with respect

to TS 4. 10.c. l.

The

licensee

has

agreed

to submit

a

TS change to clarify the method

by

which SFP water level will be monitored.

No violations or deviations

were identified in the Operational

Safety

Verification area.

Modifications (37700,

37828)

The inspectors

maintained

cognizance of modification activities to

support the restart of Unit 2.

This included reviews of scheduling

and

work control, routine meetings,

and observations

of field activities.

Throughout the observation of modifications being performed in the field

gC inspectors

were observed

monitoring and documented verification at

work activities.

a

~

Fire Protection Modifications

The inspector

reviewed the

DCNs associated

with the fire protec-

tion system

upgrades.

This is

a commitment

made

by the licensee

to meet

NFPA standards.

The upgrade

includes installation of new

fire detection

systems

in the plant.

The

DCNs and location for

each

are

as follows.

W17911

WI7909

W17910

W17907

W17906

W17908

W17904

Local System at the Intake Structure

Local System in Unit I/2

DG Building

Local System in Unit 3

DG Building

Local System in Unit 2 Reactor Building

Local System in Cable Spreading

Room

Local System, in Unit 3 Reactor Building

Installs central

computers

and interconnection

of all local systems.

In addition,

W18213 will be implemented to power down

and

decommission

the existing detection

systems.

Typical of components

installed at each location are addressable

smoke detectors,

thermal detectors,

manual pull stations,

local

fire alarm and control panels,

and local horn/strobe

alarms.

In

the

DG building, additional

equipment

was provided for the carbon

dioxide systems.

After completion of the installation, there is

a testing window in

the schedule.

Each local panel will have

a loop checkout

performed

as

soon

as the local detection

systems

are functional.

After all work has

been completed,

there is

a four-day vendor

setup of the system followed by a

25 day post modification test

window.

The inspector

reviewed several

of the

DCN packages

with emphasis

on W17904 for the interconnection of all local systems.

These

activities will continue to be monitored

as the modifications are

worked.

Hardened

Wetwell Vent

Installation of the hardened

wetwell vent continued throughout the

inspection period.

The majority of the work effort in the Unit 2

reactor building involved the completion of the saddle

weld which

joins the

14 inch hardened

wetwell vent line to the existing

20

inch line from. the torus.

The licensee

experienced

numerous

problems in process

of completing the weld.

A number of failures

during

NDE of the weld caused

the licensee

to excavate

portions of

the joint for repair.

,Final

acceptance

of this weld joint

occurred

on March 18,

1993.

In addition, discrepancies

with the

licensee's

welding process

were identified during

a Region II

based

inspection

(see

IR 259,

260,

296/93-05)

performed during

this inspection period.

Work continued

on the outside

common portions of the-hardened

vent.

Excavation in the vicinity of the plant stack for a vent

drain line and its associated

valve pit progressed

during the

inspection period.

The inspectors will continue to monitor the

licensee's

work on the hardened

wetwell vent

and ensure

adequate

post modification testing is performed prior to the completion of

the outage.

Small

Line Cracks

During Unit 2 Cycle

6 operation three

small lines inside the

containment

experienced

cracks.

The inspector reviewed the

licensee

plans to mitigate the risk of similar events

in the

future.

Technical

support identified 43 test,

vent, drain,

and

instrument lines attached

to the recirculation

and

RHR lines

inside the containment.

Eight lines are

no longer needed.

These

will be cut and capped'he

remaining lines will undergo

an

analyses

of the existing configuration for adequate

supports.

Also,

a visual

and liquid penetrant

inspections of -the welds will

be performed to determine

any other necessary

repairs or

corrective action.

The inspector will continue to follow these

activities

as the systems

are returned to service.

Unit Battery

3 Replacement

During the inspection period; the inspectors

monitored the

replacement

of 250

VDC Unit Battery 3 in accordance

with DCN

W17274.

Unit Battery

3 is

a 120 cell

250

VDC which is being

replaced

in anticipation of multi-unit operation

and

because

the

10

existing battery cells were nearing the end of design life.

The

new battery cells have

a higher capacity than

do the existing

cells due to an increase

in the number plates

per cell.

Although,

the

new cells will contain

an increased

number of plates,

the size

of cell container wi.ll be the

same

as the existing cells.

The

increase

in number of plates

caused

a corresponding

increase

in

cell weight

and necessitated

the replacement

of the battery racks.

The inspector

reviewed the installation of the

new battery racks

and installation of the

new battery cells.

Testing of the

new

battery is expected

to occur in the near future

and will be

monitored

by the inspectors.

Recirculation

Pump Rotating Element

Replacement

The inspector

reviewed

and witnessed

the replacement

of the

recirculation

pumps rotating elements

during refueling outage

cycle

6 for Unit 2.

The shafts

were replaced

due to an industry

problem with thermal fatigue cracking.

The replacement

of .the

pump shafts

were done under work orders

92-6679300

(2B pump)

and

92-6640400

(2A pump) respectively.

The recirculation

pump design

had

been

upgraded

from the original

design.

The upgrade affected the rotating element,

cover/heat

exchanger,

hydrostatic bearing

and material

composition.

The

upgrades

were due to thermal cracking problems

experienced

by

other

BWRs and

PWRs.

During the review process

of the work packages,

the inspector

noted that

a safety evaluation

had not been

performed

by the

licensee

in accordance

with 10

CFR 50.59 requirements.

10 CFR Part 50, Appendix B, Criterion IV, states

that design

changes,

including field changes,

shall

be subject to design control

measures

commensurate

with those applied to the original design

and

be approved

by the organization that performed the original

design

unless

the applicant designates

another responsible

organization.

Furthermore,

measures

shall also

be established

for

the selection

and review for suitability of application of

materials,

parts,

equipment,

and processes

that are essential

to

the safety-related

functions of the structures,

systems

and

components.

The licensee

'considered

the upgrade of the

recirculation

pumps

a like-for-like replacement

thereby

a safety

analysis

was not warranted.

The equivalency test (fit, form and

function) is satisfied

according to the licensee.

Procedure

PI-89-06,

Design

Change Control, step 13.5.d states

that

if a replacement

item meets

the criteria where the item is part of

equipment

designed

by a vendor for the specific plant application

and the vendor certifies that the replacement

item is equivalent,

the item can

be ordered with no further justification.

The staff

agrees

that the upgraded recirculation

pump rotating element,

cover/heat

exchanger

and hydrostatic bearing

may meet the original

11

fit and function requirement of the equivalency test,

however it

does

not meet the form requirements.

The material for the shaft,

impeller, hydrostatic bearing etc... all have

been

changed.

The

physical materials

have

changed therefore

form requirements

are

not satisfied.

This issue requires further

NRC review and will be

tracked

as

URI 259,

260,

296/93-07-01,

Safety Evaluation for

Recirculation

Pump Shaft Replacement.

Unit 3 Restart Activities

(30702)

The inspector

reviewed

and observed

the licensee's

activities involved

with the Unit 3 restart.

This included reviews of procedures,

post-job

activities,

and completed field work; observation of pre-job field work,

in-progress field work, and gA/gC activities; attendance

at restart

craft level, progress

meetings,

restart

program meetings,

and management

meetings;

and periodic discussions

with both

TVA and contractor

personnel,

skilled craftsmen,

supervisors,

managers

and executives,

a.

Unit Status

Limited activities continue

on Unit 3 recovery.

A schedule

review

process

is ongoing to determine

a credible schedule

to be

announced

at the end-.of the Unit 2 Cycle 6.outage.

Activities

were drywell steel

work and return to service of the

RWCU system.

b.

Drywell Tour

On March 5,

1993, the inspector

made

a tour of the Unit 3 drywell.

Overall the drywell was clean

and free of combustible material.

The inspector

noted that many hot jobs were in progress

which re-

quired firewatches.

Each job had its

own firewatch.

Blankets

and

catch

pans

were

used in many places to prevent slag from dropping

to

a lower elevation.

The inspector

reviewed the welding and

grinding permits posted

and verified the information required

was

documented

properly.

The inspector

found no deficiencies.

Radiological Controls

(83724)

a

~

Drywell Cameras

The Radiation Control

Group has installed approximately twenty

cameras

throughout the Unit 2 drywell which input to fifteen

monitors located at

a manned post outside the drywell.

In

addition,

intercom stations

have

been established

in the drywell

which can communicate with the manned post.

If a person

in the

drywell needs

assistance

they can talk via an intercom with the

person monitoring this post.

The monitor can then adjust the

camera to see the person requesting

assistance

and also alert the

HP stationed

in the drywell.

On 3/16/93,

the inspector toured the

drywell and noted that while this arrangement

is

a good idea,

the

stations

in the drywell are not easily identifiable.

In addition

the drywell radiological control technician

was not aware that

~

12

they even existed.

The cameras

also provide for a much larger

surveillance

area

by radiological controls without expending

any

additional radiation dose.

Three

VCRs are available which are

used to filivarious jobs or job sites

and then viewed outside the

drywell in low radiation areas

to resolve

problems that

may arise.

The films are also often used during shift change

or for training

purposes.

In addition to the drywell, cameras

have

been installed

in the steam tunnel

and the

RWCU heat exchanger

and

pump rooms.

The estimated

dose savings,

by the licensee,

resulting from the

use of the cameras

is 16.8 Nan-Rem.

Radiological

Control

Work Practices-

On February

25,

1993, during the performance of daily rounds,

the

inspectors

observed

work activities

on the 664'levation

(refuel,

floor) of the Unit 2 reactor building.

A particular work activity

observed

consisted of two individuals performing maintenance

on

the fuel support piece lifting tool.

While,one worker with a face

shield

was manipulating the hose

connected

to the lifting tool,

the other worker without

a face shield

was bending

down on his

knees

and handling the lifting tool.

Shortly after the

observation of this incident, the two workers switched their work

positions.

After holding

a discussion

with the radiological

control technician

on shift, the inspector identified that the

worker without the face shield was not signed

on the

RWP to

perform work activities

on the fuel support piece lifting tool.

Furthermore,

a face shield

was required per radiological control

directions to perform work activities

on fuel support piece

lifting tool.

Later the

same day, another inspector performing

a routine tour of

the Unit 2 turbine building observed

maintenance

being performed

on the turbine stop valves.

Individuals performing the work

activity were dressed

in anti-contamination clothing as specified

by radiological controls

and

RWP 93-2-60002-01-00

as the area in

question

was being controlled

as

a contamination

zone.

As the

maintenance

progressed,

the inspector

observed

(as did the

radiological control technician monitoring the job)

an individual

remove his anti-C hood

and surgeons

cap while still in the

contamination

zone.

This action

was taken prior to the individual

climbing from the "valve pit" to the C-zone exit.

The

radiological control technician

ensured that the individual exited

the C-zone,

undressed

and proceeded

to the frisking station.

A

few minutes later, the inspector

observed

another individual in

the C-zone

don

an anti-C hood which had

been lying on

a steam line

within the C-zone.

The inspector

informed radiological control of

his observation.

Radiological control instructed the individual

to exit the C-zone

and perform

a whole body frisk.

In both

instances,

the individuals were found not to be contaminated.

TS 6.8. I.l.a requires that written procedures

shall

be

established,

implemented

and maintained covering the applicable

13

procedures

recommended

in Appendix A of Regulatory

Guide 1.33,

Revision 2, February

1978.

Regulatory

Guide 1.33,,section

7.e. l.,

requires

Radiation Protection

Procedures

covering Access Control

to Radiation Areas including

a Radiation

Work Permit Systems.

RCI-9, Radiation

Work Permits,

is the implementing procedure for

this requirement.

Failure to comply with RCI-9, Radiation

Work

Permits,

section 6.5. 1, which holds the individual worker

responsible

to ensure

the correct

RWP for the job is used,

and

section 6.5.3.'which requires individuals using

a

RWP comply with

all of the requirements

of the

RWP as 'well as the verbal

instructions given by radiological control personnel

so far as

.

those instructions pertain to radiological matters,

is

a violation

of TS Section 6.8. 1, Procedures.

This matter is identified as

violation 259,

260, 296/93-07-02,

Failure to Comply with Radiation

Protection

Procedures.

One violation was identified in the radiological control work practices-

area;

8.

Reportable

Occurrences

(92700)

The

LER listed below was reviewed to determine if the information

provided met

NRC requirements.

The determinations

included the

verification of compliance with TS and regulatory requirements,

and

addressed

the adequacy of the event'escription,

the corrective actions

taken,

the existence of'otential generic

problems,

compliance with

reporting requirements,

and the relative safety significance of each

event.

Additional in-plant reviews

and discussions

with plant

personnel,

as appropriate,

were conducted.

(CLOSED)

LER 259/86-14,

Inadvertent

ESF Actuation Leads to Water

Spillage

This item was originally identified when in May 1986,

an inadvertent

- actuation of an

ESF occurred

in Unit I and

was twice repeated.

The

actuation

was caused

by a false high drywell signal

due to an electrical

short.

All eight

DGs and two

EECW pumps started automatically.

Since

CS and

RHR pump motor breakers

were tagged,

no

ECCS

pumps started.

However, the

CS injection valves opened,

which allowed water from the

condensate

storage

system to flood the reactor cavity.

Water over

flowed into the vents

on the periphery of the refuel,ing well and

some

spillage occurred

from the ventilation ductwork on the lower elevations

of Unit I reactor building before the valves

were discovered

open.

The

electrical short,

caused

by moisture in two high drywell pr essure

switches,

was believed to be due to

a spurious actuation of fire spray

valves in the area of these

switches earlier in the week of the event.

Inspection

Report 90-27

and

LER 259/86-14

addressed

this issue

and

closed this item for Unit 2 only.

The Unit 2 Reactor Building Fire

Spray System

had

been modified to a preaction type system which operates

on the fused

head

spray valve design.

When

an actuation

occurs,

the

system floods with water,

and only those

spray valves

where the fuse

head

has disengaged will actually spray water.

Spurious actuations will

only cause

the system to flood with water without actual

spraying.

The

systems for Unit I and Unit 3 had not been modified.

The inspector

was

concerned

whether

any equipment of Unit I and/or Unit 3 could affect

Unit 2 system operability.

Inspection

Report 92-16,

VIO 259,

260,

296/87-33-01,

Failure to Seal

Conduit,

addressed

that the licensee

took

actions to correct this problem with Appendix

R modifications

and the

sealing of all required conduits

and conjunction boxes.

Based

on the review of the closure

package,

applicable

LERs and

violation to this item, the inspector considers this

LER for Unit I and

Unit 3 closed.

Exit Interview (30703)

The inspection

scope

and findings were summarized

on March 19,

1993,

with those

persons

indicated in paragraph

I above.

The inspectors

described

the areas

inspected

and discussed

in detail the inspection

findings listed below.

The licensee

did not identify as proprietary

any

of the material

provided to or reviewed

by the inspectors

during this

inspection.

Dissenting

comments

were not received

from the licensee.

Item Number

Des'cri tion and Reference

259,

260,

296/93-07-01

259,

260,

296/93-07-02

URI, Safety Evaluation for Recirculation

Pump Shaft Replacement,

paragraph five.

VIO, Failure to Comply with Radiation

Protection

Procedures,

paragraph

seven.-

Acronyms

and Initialisms

CCW

CS

CSS

CW

DCNs

DG

ECCS

EECW

ESF

FSAR

IVVI

LER

LCO

HR

NFPA

NRR

PPB

Condenser Circulating Water

Core Spray

Chemistry Shift Supervisor

'irculating

Water

Design

Change Notices

Diesel Generator

Emer'gency

Core Cooling Systems

Emergency

Equipment Cooling Mater

Engineered

Safety Feature

Final Safety Analysis Report

In-Vessel

Visual Inspection

Licensee

Event Report

Limiting Condition for Operation

Maintenance

Request

National Fire Protection Association

Nuclear Reactor Regulation

Parts

Per Billion

Licensee

management

was informed that I

LER was closed.

PPH

QA

QC

RCI

RHR

RHRSW

RWCU

RWP

SFP

SI

TS

URI

VIO

WO

WR 15

Parts

Per Million

Quality Assurance

Quality Control

Radiological

Control Instruction

Residual

Heat

Removal

Residual

Heat

Removal Service

Water

Reactor

Water Cleanup

Radiological

Work Permit

Spent

Fuel

Pool

Surveillance Instruction

Technical Specification

Unresolved

Item

.Violation

Work Order

Work Request

~,

~

0