ML18036A768

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Insp Repts 50-259/92-21,50-260/92-21 & 50-296/92-21 on 920516-0616.Violations Noted.Major Areas Inspected:Maint Observation,Operational Safety Verification,Measuring & Test Equipment Program & Restart Activities
ML18036A768
Person / Time
Site: Browns Ferry  Tennessee Valley Authority icon.png
Issue date: 06/30/1992
From: Kellogg P, Patterson C
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18036A766 List:
References
50-259-92-21, 50-260-92-21, 50-296-92-21, NUDOCS 9207140102
Download: ML18036A768 (35)


See also: IR 05000259/1992021

Text

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION

11

101 MARIETTASTREET, N.W.

ATLANTA,GEORGIA 30323

+>>**~

Report Nos.:

50-259/92-21,

50-260/92-21,

and 50-296/92-21

Licensee:

Tennessee

Valley Authority

6N 38A Lookout Place

1101 Market Street

Chattanooga,

TN

37402-2801

Docket Nos.:

50-259,

50-260,

and 50-296

License Nos.:

DPR-33,

DPR-52,

and

DPR-68

Facility Name:

Browns Ferry Units 1,

2,

and

3

Inspection at Browns Ferry Site near Decatur,

Alabama

Inspection

Conducted:

May 16

June

16,

1992

Inspector:

atterso

,

nidor

ent

nspector

4Po

W~

a

e

S gne

l

Accompanied

by:

E. Christnot,

Resident

Inspector

W. Bearden,

Resident

Inspector

Approved by:

e

o

R actor

, Section

4A

Divis

of Reactor Projects

Date

gne

SUMMARY

Scope:

This routine resident

inspection

included maintenance

observation,

operational

safety verification, measuring

and test

equipment

program, Unit 3 restart activities, Unit

1 activities, licensing

activities, reportable

occurrences,

and action

on previous

inspection findings.

One hour of backshift coverage

was routinely worked during the

work week.

Deep backshift inspections

were conducted

on May 30

and June

6.

Results:

Unit:2 operated

at power during this report period

and

was on-line

for 47 days at the

end of the period,

paragraph

three.

The

licensee

met

a commitment to implement Revision Four of the

9207140102

920702

PDR

ADOCK 05000259

9

PDR

Emergency Operating Instructions

on June

15,

1992.

New control

room furniture for the unit operator

and assistant shift

operations

supervisor workstations

were installed providing ample

space

to use the

new flowcharts.

A temporary waiver of compliance

from technical specifications for

the control

room emergency ventilation system

was granted to

permit

a test necessary

to determine

adequate

capacity for the

system fan, paragraph

three.

All conditions of the waiver were

m'et.

The testing indicated additional capacity is needed.

A violation.was identified by the inspector for failure to

.adequately

disposition nonconforming measuring

and test equipment,

paragraph

four.

Programmatic

problems

were identified with

timely, incomplete,

and

adequate

disposition of nonconformance

evaluations.

There

was

a lack of ownership of the program

and

insufficient management

oversight.

Licensee

management

was

responsive

to these findings

and initiated

a comprehensive

corrective action program.

A non-cited violation was identified for a drawing error in

a

reactor water cleanup

system drawing,

paragraph

three.

Due to the

incorrect disposition of a previous drawing discrepancy

an

unexpected

system isolation occurred

when

a fuse

was pulled.

The

licensee

conducted

a thorough review of this event

and initiated

actions to correct the problem.

An inspector followup item was identified concerning

a scaffold in

place

around the torus,

paragraph

three.

Scaffolding was erected

to the torus

and concrete wall without any clearance,

possibly

restricting

movement of the torus in

a blowdown.

The licensee

is

conducting

an evaluation of the possible

consequences.

A declining trend in complete

and accurate

licensing submittals to

the

NRC was identified, paragraph

seven.

Three licensee

event

reports

and two replies to notice of violations required

resubmittal

due to missing or inaccurate

information.

This

indicated

a lack of attention to detail in preparation

of the

.

submittals.

Unit 3 work activities are proceeding with cooling tower

.

refurbishment,

condenser

retubing, reactor water cleanup

and

recirculation

system piping replacement,

and control

room design

review, paragraph

six.

Unit

1 work activities consisted

of scaffold erection for

walkdowns

and in-vessel

inspections.

Walkdowns

commenced for

information needed

to, support work in Unit

1 during the Unit 2

Cycle

6 refueling outage.

This must

be accomplished

to prevent

a

multi-unit defueling outage

at

a later date.

REPORT

DETAILS

Persons

Contacted

Licensee

Employees:

  • 0. Zeringue,

Vice President,

Browns Ferry Operations

H. McCluskey, Vice President,

Browns Ferry Restart

  • J. Scalice,

Plant Manager

J. Rupert,

Engineering

and Modifications Manager

  • J. Swindell, Restart

Manager

H. Herrell, Operations

Manager

  • J. Haddox,

Project Engineer

  • H. Bajestani,

Technical

Support

Manager

R. Jones,

Operations

Superintendent

A. Sorrell, Special

Programs

Manager

  • C. Crane,

Maintenance

Manager

G. Turner, Site guality Assurance

Manager

R. Baron, Site Licensing Manager

  • P. Salas,

Compliance Supervisor

  • J. Corey, Site Radiological

Control

Manager

  • A. Brittain, Site Security Manager

Other licensee

employees

or contractors

contacted

included licensed

reactor operators,

auxiliary operators,

craftsmen,

technicians,

and

public safety officers;

and quality assurance,

design,

and engineering

personnel.

NRC Personnel:

P. Kellogg, Section Chief

  • C. Patterson,

Senior Resident

Inspector

  • E. Christnot,

Resident

Inspector

W. Bearden,

Resident

Inspector

  • Attended exit interview

Acronyms

and initialisms used throughout this report are listed in the

last paragraph.

Maintenance.Observation

(62703)

Plant maintenance

activities were observed

and/or reviewed for selected

safety-related

systems

and components

to ascertain

that they were

conducted

in accordance

with requirements.

The following items were

considered

during these

reviews:

LCOs maintained,

use of approved

procedures,

functional testing and/or calibrations

were performed prior

to returning

components

or systems

to service,

gC records maintained,

activities accomplished

by qualified personnel,

use of properly

certified parts

and materials,

proper

use of clearance

procedures,

and

implementation of radiological controls

as required.

'

Work documentation

(HR,

WR,

and

WO) were reviewed to determine

the

status of outstanding

jobs

and to assure that priority was assigned

to

safety-related

equipment

maintenance

which might affect plant safety.

The inspectors

observed

the following maintenance activities during this

reporting period:

a ~

b.

c ~

Unit

1

RHR System

Loop Outage

The inspectors

followed licensee activities associated

with the

scheduled

outage for Loop II of the Unit

1

RHR System.

This loop

is required

by TS to be available for crosstie

operations

to

support Unit 2 operations.

Only Unit

1

and

RHR crosstie

components

were affected

by the outage.

The

RHR loop was

removed

from service

on June

9,

1992,

under hold order 1-92-88.

LCO 2-92-

155-3.5.B. 13 was entered,to

track the

10 day

LCO while the loop

was unavailable.

Various scheduled

preventive

and corrective

action items

on

HOVs and other components

were accomplished

during

this outage.

The loop was returned to service

on June

12,

1992.

Post maintenance

testing in accordance

with 1-SI-4.5.B. 11,

RHR

Unit

1 Crosstie for Unit 2 Operability,

was accomplished prior to

declaring the loop operable.

The inspectors

did not identify any

deficiencies

during this scheduled

system outage.

Relay

Room

Fan Vibration

An inspector followed licensee activities associated

with WOs 91-

32000-00

and 92-53881-00.

These

scheduled

work activities were

written to correct various deficiencies

including excessive

fan

vibration for the Relay

Room "A" Air Handling Unit located

on the

3C elevation of the Control

Bay.

The inspector

observed

selected

activities including installation of a

new shaft coupling

and

reassembly

of other components.

The inspector

reviewed the two

uncompleted

work packages

and determined that each provided

adequate

instructions

and guidance to support the intended

work

activity.

The inspector did not identify any deficiencies

during

observation of the work activity.

Drywell Pressure

Transmitter

An inspector

observed

portions of licensee activities

on May 19,

1992,

associated

with

WO 91-29039-00,

which replaced

Drywell

Pressure

Transmitter,

2-PT-64-0160A, with a refurbished

transmitter.

The inspector

observed

portions of the actual

transmitter

replacement

and reviewed the uncompleted

work package.

The inspector determined that the

WO provided adequate

instructions

and guidance to support the intended

work activity.

NSI-0-000-PR0001;

Cleanliness

of Fluid Systems,

and SII-0-XX-00-

3014, Troubleshooting

and Configuration Control of

Instrumentation,

were also in use

by the maintenance

personnel

during the work.

Post maintenance

test

was specified to be

performed in accordance

with 2-SI-4.2.F-21(A), Drywell Pressure

Wide Range

(Div. I).

The inspector did not identify any

deficiencies

during observation of the work activity.

No violations or deviations

were identified in the Haintenance

Observation

area.

Operational

Safety Verification (71707)

The

NRC inspectors

followed the overall plant status

and

any significant

safety matters related to plant operations.

Daily discussions

were held

with plant management

and various

members of the plant operating staff.

The inspectors

made routine visits to the control

rooms.

Inspection

observations

included instrument readings,

setpoints

and recordings,

status of operating

systems,

status

and alignments of emergency

standby

systems,

verification of onsite

and offsite power supplies,

emergency

power sources

available for automatic operation,

the purpose of

temporary tags

on equipment controls

and switches,

annunc'iator

alarm

status,

adherence

to procedures,

adherence

to LCOs, nuclear instruments

operability, temporary alterations

in effect, daily journals

and logs,

stack monitor recorder traces,

and control

room manning.

This

inspection activity also included

numerou's

informal discussions

with

operators

and supervisors.

General

plant tours were conducted.

Portions of the turbine buildings,

each reactor building,

and general

plant areas

were visited.

Observations

included valve position

and system alignment,

snubber

and

hanger conditions,

containment isolation alignments,

instrument

readings,

housekeeping,

power supply

and breaker alignments,

radiation

and. contaminated

area controls,

tag controls

on equipment,

work

activities in progress,

and radiological protection controls.

Informal

discussions

were held wi'th selected

plant personnel

in their functional

areas

during these tours.

Unit Status

During this

IR period the unit operated

at power.

At the

end of

the report period the unit had

been

on line for 47 days.

New

control

room furniture was installed in Unit 2. 'he licensee

met

a commitment to implement revision four of the

EOIs

on June

15,

1992.

b.

Temporary Waiver of Compliance

On Hay 22,

1992,

the licensee

was granted

a temporary waiver of

compliance

from the requirements

of TS 3.7.E. 1,

CREV system.

The

waiver permitted relief from TS 3.7.E. 1 for a total of 16 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br />

between

Saturday,

Hay 23,

1992,

and Honday,

Hay 25,

1992, to

perform testing necessary

to determine

adequate

capacity for the

CREV units.

The test

was required to support the long lead time

for procurement to support

any future activities for additional

CREVs capacity if necessary.

During the test,

the system

was not

operable

since several

manual

actions

were required in place of

the normal automatic actuation.

0

Compensatory

measures

in effect for the duration of the waiver

were dedicated test personnel

trained

on procedures

for manual

actions

necessary

to initiate the

CREVs.

The inspector verified

the conditions of the waiver were specified in special test

procedure

O-ST-91-07,

Control

Bay Habitability Zone Leakage

Rate.

The procedure

contained

a list o'f dedicated

tested

personnel,

required training,

and detailed actions.

CREVs was

made

inoperable

at 1:20 a.m.,

on Hay 23,

1992,

and the test

and

equipment restoration to normal

completed

at 8:30 a.m.,

on May 23,

1992.

All conditions of the waiver were followed during the test.

The

inspector

reviewed the completed test procedure.

The capacity

necessary

to obtain

one eighth inch positive water pressure

in the

control

bay was around

1900 cfm and

2370 cfm at one quarter

inch

pressure.

This testing indicated additional capacity

was needed.

The exact size will be evaluated.

The electrical

load will have

to be

added to the

DGs.

The inspector will continue to review the

licensee

actions until the

CREVs is restored

to

a fully operable

basis.

RWCU Isolation

A unanticipated

automatic isolation of the Unit 2

RWCU system

occurred

on April 24,

1992, during placement of an equipment

clearance

associated

with

WO 91-43482-00.

This

WO had -been

written to allow replacement

of RWCU pressure

switch,

2-PS-69-15B.

The isolation occurred

when fuse FUI-69-15A was pulled.

Work

associated

with this pressure

switch replacement

was immediately

stopped,

the fuse replaced,

and the

RWCU system restored

to

operation.

After troubleshooting

the licensee

determined that

RWCU nonregenerative

heat exchanger outlet temperature

indicating

switch, 2-TIS-69-11,

also would become

deenergized

whenever this

fuse

was pulled.

This had caused

an isolation of the

RWCU system

as designed to prevent overheating

protection for the

RWCU

demineralized resin.

Elementary diagrams,

2-730E922-2,

for the

RWCU system

and 2-730E927,

sheet

13, for the

PCIS system did not

show this fuse in the power supply circuit for 2-TIS-69-11.

The inspector

reviewed incident investigation report,

II-B-92-028,

which documented

the licensee's

investigation into this event.

In

that report the licensee attributed the event to

a failure by

licensee

personnel

to properly disposition drawing discrepancy,

2-

87-1225,

during performance of ECN P7082 which was completed

in

1988.

That

ECN moved instruments

2-TIS-69-4A and

4B and revised

the

power feed

and panel location

on drawing 2-730E922-2,

figure

3.

When these

instruments

were relocated

from panel

2-25-2 to

panel

2-25-5-1, figure

3 was changed to reflect this,

but

a

new

figure was not developed

to show the power feed for .panel 25-2,

which contains

2-TIS-69-11.

DD 2-87-1225

had previously

been

added to the drawing to document that 2-TIS-69-11

was

powered

from

the panel

2-25-2 power supply,

but that

DD was removed

when the

ECN changed

the panel

number.

Without this change

there

was

no

ready method of identifying the power feed from fuse FUI-69-15A to

2-TIS-69-11, without doing extensive

research

on the connection

diagrams.

Connection

diagrams

are secondary

drawings that are not

available in the control

room.

The inspector reviewed the details

associated

with this drawing error and determined that the error

appeared

to be

an isolated

case with no safety significance.

The

licensee

had taken

immediate corrective actions to investigate

the

problem

and the drawing error was corrected prior to performing

additional

work in the affected panels.

This violation will not be cited because it meets

the criteria of

Section VII.B of the Enforcement Policy.

NCV 260/92-21-01,

RWCU

Drawing Error, will be issued to document this failure to properly

update

the drawing.

Plant Tours

During

a routine tour on Hay 19,

1992, the inspectors

identified

some

housekeeping

concerns

in the area

around the Unit 2 Torus.

Personnel

were working in the overhead within a contamination

area

established

over the torus.

The following items were found:

Anti-contamination clothing in overhead

Loose pieces of insulation or lagging were

seen

hanging

from

the overhead.

One piece of sheetmetal

used to cover lagging was

seen

in

the overhead

jammed

between

a pipe

and the torus.

There were several

wet areas

along the floor below the

torus.

These observations

were discussed

with plant management.

The

licensee

took immediate action to have the affected

area

cleaned.

Another concern identified was associated

with a section of

scaffolding erected

in the area next to the Unit 2 Torus.

One end

of a horizonal scaffolding restraints

was in direct contact with

the concrete

wall and the other end of that restraint

was in

direct contact with the torus wall.

The specific concern is that

this restraint could possibly interfere with any movement of the

torus that occurs

anytime there is

a large

blowdown to the torus.

The ladder that provided access

to the scaffolding had

a tag which

provides

Radcon concurrence

with working in an overhead

area.

Personnel

are required to check that radcon

surveys

have

been

performed of the affected

overhead

areas within the last

seven

days prior to climbing scaffolding or ladders.

That tag

had not

been

signed

since

March 3,

1992.

The inspector

reviewed O-TI-264, Scaffolds

and Temporary

Platforms,

and determined that although

no specific mention of

clearance

requirements

relating directly to the Torus were

referenced,

Section 3.5 requires that restraints

shall

have

a

minimum clearance

of six inches

from all safety-related

items.

The inspector discussed

this concern with the licensee civil

engineer that

has responsibility for review and approval of

scaffolds

and temporary platforms prior to use

by craft personnel.

The engineer

stated

an evaluation of potential effects

on the

torus would be made

by Nuclear Engineering.

The inspector

noted

that the scaffolding was removed

by the licensee within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />

after the above discussion.

The inspector

was later informed that

the licensee

had determined that, the scaffolding

was

no longer

needed.

This item will remain

open

as IFI 260/92-21-02,

Adequacy

of Scaffolding Review,

pending review of the licensee's

evaluation

of this issue.

e.

Control

Room Design

Review

The inspector

observed

the field activities associated

with the

BFNP

CRDR, Unit's

2 and 3.

Little visible field work has occurred

on Unit 3 during this reporting period.

Two control

room panels

have

had minor work, dealing mostly with switch relocation

and

labeling.

Field work in this control

room is expected

to increase

dramatically in the upcoming weeks.

The bulk of the control

room

activity, relative to

CRDR,

has

been

on Unit 2 associated

with the

installation of new furniture.

The unit operator

and

ASOS desks

were removed

and

new modular style furniture was installed.

The

ASOS desk design

was chosen to facilitate use of the

new

EOI

flowcharts.

The negative

impact

on the control

room personnel

has

been limited.

The i'nstallation processes

were conducted

to reduce

the noise,

adhesive

fumes, limited space,

etc..

Discussions

with

various operations staff indicated that while the activities

associated

with this job were disruptive,

they were not distracted

from performing their assigned

duties.

One

NCV was identified in the Operational

Safety Verification area.

4.

Measuring

5 Test

Equipment

Program

The inspector

reviewed the licensee's

METE program, specifically in the

, area of out of tolerance

investigations

as outlined in SSP-6.7,

Control

of Measuring

and Test Equipment, revision

1.

Within this area

several

weaknesses

were identified which collectively resulted in an inadequate

HKTE program with respect

to investigating

and dispositioning

nonconforming

MME.

The licensee

transports

most of its MME to the

CLSD, located in

Chattanooga,

Tennessee,

for calibration.

Following calibration the MDE

is returned to

BFNP with a calibration report documenting

items

such

as

"as-found"

and "as-left" data,

procedures

used to perform the

calibrations,

calibration tolerance

requirements,

dates of previous,

present,

and next calibration, etc..

If HKTE is found out of tolerance

or damaged

the licensee

is notified and

a nonconformance

evaluation is

issued

which investigates

the prior uses of the

HKTE back to the

previous calibration.

This nonconformance

package

includes the

7

initiating document that designates

appropriate

signatures

needed,

a

copy of the usage log,

and

a copy of the calibration form from CLSD.

The inspector

noted that

when

M&TE was found out of tolerance,

three to

five weeks would pass

before the licensee

was

made

aware of the

condition.

This untimeliness

resulted

in unnecessary

delay in

performing required investigation.

Each group that used the

H&TE during

the period in question will investigate

the uses to determine

system

impact, if any,

and identify corrective action.

This in turn is

reviewed for technical

adequacy

by

a technical

reviewer.

This process

is to be completed in 30 calendar

days but may be extended

to 40

calendar

days with an approved extension.

The inspector

reviewed fourteen

nonconformance

packages

and rioted the

following discrepancies:

SSP-6.7

states

that investigation shall

be completed

30

calendar

days. from the date of initiation and not exceed

40

calendar

.days with approved extensions.

Six packages

were

greater

than

30 days late without approved

extensions

with

four of these

packages

being later than the

maximum allowed

40 days.

Package

no. 91-00504. 1, generated

due to an out of

tolerance digital multimeter,

was completed

February

10,

1992,

and took 59 days to complete.

2.

SSP-6.7

states

that each

instance of use shall

be

investigated

and dispositioned.

Seven

packages

did not

contain documentation of investigating all previous

uses of

the

M&TE during the period in question.

As an example,

package

no.

91-00486. 1, concerning

an out of tolerance

flowmeter transducer

assembly,

listed ten uses of the

instrument to be dispositioned,

all of which were

on

CSSC.

Only one of the uses

could

be verified as dispositioned.

Package

no. 91-00332.1 listed work order 90-23710

on the

usage

log and therefore required investigation to determine

the impact of using out of tolerance

H&TE during its

performance,

however,

work order 90-23718

was investigated

instead.

3.

'SP-6.7

states

that activities associated

with H&TE found to

be nonconforming shall

be investigated

subsequent

to the

previous calibration.

Package

no. 91-00355.3 did not

investigate

the entire period in question

subsequent

to the

previous calibration.

4.

Eight packages

contained various administrative errors

including missing signatures

and dates.

For example,

package

no. 92-00002.2 did not have the investigators

signature

and package

no. 92-00104.

1 had the investigators

'signature

but it was not dated.

'

It was also noted that the controlling document

advised that

a program

status

report

be generated

each

month documenting the number of

calibrations

performed,

the number of nonconforming conditions,

average

number of days required to complete

nonconformance

evaluations,

and

any

other data which might indicate

M&TE reliability problems

and program

performance.

The inspector requested

a copy of the most recent report

and was informed that the report

has never

been generated.

Discussion

was held with licensee

management

on this subject

and

included highlighting the previous

SALP report,

90-02, which also

identified

a weakness

in this area.

One nonconformance

package,

91-00486. 1, concerning

an out of tolerance

flowmeter transducer

assembly,

was also discussed

with licensee

management

concerning

the

operability of systems

that used this instrument for the performance

of

surveillances

required

by TS.

Subsequent

evaluation

by the licensee

determined that surveillances

for the affected

systems

have

been

satisfactorily

completed

since that time.

The licensee will continue

to evaluate this area

as part of a corrective action plan for M&TE

program deficiencies

the licensee

generated

as result of this

inspection.

Additional objectives of this plan are

as follows:

2.

3.

4.

5.

6.

7.

8,

9.

10.

Ensure

each out of tolerance

H&TE usage

is properly

investigated.

Reduce

out of tolerance

review cycle time..

Establish

an escalation

process.

Consolidate

M&TE responsibility into

a single group.

Establish

an automated

H&TE traceability process.

Create

a centralized

H&TE issue

process.

Establish

goals to eliminate administrative errors, late

reports,

and

H&TE damage

and loss.

Ensure proper/prompt operability determination.

Ensure routine reporting to the Plant Manager.

Increase

the scope of both onsite

H&TE calibration

and post

use checks.

This corrective action plan developed

a short term plan to correct these

and other

known deficiencies

in the existing

M&TE program

and

a long

term plan to enhance

the program to meet or exceed

TVA, regulatory,

and

industry standards.

While there were

many individual root causes

for the discrepancies

noted

by the inspector,

the overall root cause

appears

to be

an inadequate

program

and management

oversight in the area of M&TE nonconformance

investigation.

Management

and leadership of the

METE organization

has

changed

several

times in the last year that resulted

in

a lack of

structure

and ownership

and led to these

program deficiencies.

Failure to have methods established

to adequately disposition

nonconforming

H&TE is

a violation of 10 CFR 50, Appendix B, Criteria XII

delineated

in the

TVA Nuclear Quality Assurance

Plan

(TVA-NQA-PLN89-A)

'section 9.5.2.B.3

and

implemented

by SSP 6.7 Control of Measuring

and

Test Equipment.

This constitutes

Violation 259,

260,

296/92-21-03,

Failure to Adequately Disposition Nonconforming

MLTE.

One violation was identified in the Measuring

and Test Equipment area.

Unit 3 Restart Activities

(30702)

The inspector

reviewed

and observed

the licensee's

activities involved

with the Unit 3 restart.

This included reviews of procedures,

post-job

activities,

and completed field work; observation of pre-job field work,

in-progress field work,

and gA/gC activities;

attendance

at restart

craft level, progress

meetings,

restart

program meetings,

and

management

meetings;

and periodic discussions

with both

TVA and contractor

personnel,

skilled craftsmen,

supervisors,

managers

and executives.

Pilot/Prototypical

Program

The inspector

completed

reviews of the

new proceduralized

SPOC/SPAE

process

as planned for the cooling towers.

Discussions

were held with various

managers for the different departments

at

BFNP.

The inspector

noted that each

department

manager

indicated

an understanding

of the cooling towers

SPOC/SPAE prototypical

program including the

Phase

I and

Phase II approaches.

The

inspector

concluded

from these

reviews

and discussions

-that the

licensee's

management

were

aware of the

new SPOC/SPAE

process

and

were ready to support its implementation.

b.

Design Activities

The inspector continued to monitor and review the design

activities associated

with the pilot/prototypical program involved

with the cooling towers

RTO.

DCN 17771,

Remove

Fan Control

Circuits, Automatic Operation

Function

and Indicating Lights From

Control

Room Panel

9-56/9-57

was field completed to the point

where post modification test procedure

O-PMT-BF-027.005,

Cooling

Towers I, 5,

and

6 Logic Functional

and Lift Pump Bearing

Lube

Water Annunciation Test,

was started.

When the fans were test run

and the spring loaded start switch was actuated,

the fans would

start,

but would stop

as

soon

as the switch was released.

The

test engineers

started

a troubleshooting

process

that indicated

that the implementation'f

a section of DCN 17771,

removal of the

reverse

mode of fans,

also affected the start seal-in function.

The inspector

reviewed

BTRD 2/3-BFN-BTRD-027,

Condenser

Circulating Water System

027.

The document defined the tests

required to demonstrate

that the

CCW system

027 can meet the

functional requirements

for safe

shutdown

from all abnormal

operational

transients,

accidents,

and special

events identified

in the

SSA and the

CCW system

027,

Requirements

Calculation.

The

scope of the document

was to identify all functional tests

required for the

CCW system that will determine its capability to

meet safe

shutdown requirements.

This included

any detailed

10

component testing or partial

system testing to ensure

the

functional ability of the system to meet its intended

design

function to support

shutdown of BFNP Unit 2 and/or Unit 3.

The

scope

was specifically aimed at cooling towers

1, 2, 3, 5,

and 6.

The

BTRD listed the required tests

as followed:

Descri tion of Test

Provide

warm water channel

level

indication in the main control

room.

Provide forebay level indication in the

main control

room for manual

actions to

reduce

power or if necessary

initiate

scram.

Mode Number

027-01

027-02

Provide cooling tower lift pump discharge

water high temperature

signal to 4-KV power

distribution system

(57-5) for tripping of

the corresponding

cooling tower lift pump.

Provide manual

vacuum breaking capability

to prevent backflow of cooling tower warm

water discharge

into the forebay

upon trip

of the

CCW pumps.

027-03

027-04

Provide forebay/warm water channel differential 027-05

level indication in the main control

room.

Provide cooling tower lift pump trip on

receipt of a condenser circulating water

system

(27) cooling tower lift pump discharge

water high temperature

signal.

57-5-05

Also contained

in the

BTRD as attachments

were the Test Scoping

Document for each

mode number

and

a testing matrix for'ach

cooling tower.

The inspector

concluded

from this monitoring and

these

reviews that the design activities for the cooling towers

pilot/prototypical program were being performed in

a controlled

manner

and in accordance

with approved

procedures.

c.

Construction Activities

Secondary

Containment

Penetration

A specific

WP for the drywell chiller modification was

monitored

and reviewed which involved the opening of a 36"

secondary

containment penetration.

WP 3107-92. was written

to implement the

DCAs of DCN W17695 associated

with the 36"

penetration

through the Unit 3 reactor building, south wall,

located at elevation 585'"

and 10'" from R16.

The

I

11

inspector

reviewed

DCAs W17695-009,

010,

060,

and 061,

observed

the craft personnel. in the field and monitored the

, gC inspectors activities.

The

DCAs and the

WP instructions

required that the outside cover of the penetration

be

removed;

the

new plate. with one

14" hole

and four 6" holes

be bolted over the penetration;

and the four capped

6"

OD

pipes

and the capped

14"

OD pipe

be pushed

through the plate

up to the inside penetration

cover; all five pipes to be

secured

using U-clamps; the inside penetration

cover

be

removed;

the five capped

pipes

U-clamps

be relaxed

one at

a

time, the pipes

be pushed further into the Unit reactor

building,

and the U-clamps secured;

and the inside

penetration

work than completed.

The craftsmen

performing

the work activities in this manner will maintain secondary

containment

throughout the process.

The inspector will

continue to monitor and review the penetration

work.

Work Plan Library

During the monitoring and review of the construction

activities,

the inspector

noted that the contractor

had not

instituted

a

WP library.

The process

of keeping

WPs

when

not in the field being actively worked in a library is the

method that Unit 2 modifications personnel

use.

This item

was discussed

with Unit 3 management

personnel.

Restart

management

agreed to establish

a Unit 3 Work Plan Library.

Pipe Replacement

On May 18,

1992,

the inspector toured the Unit 3 warehouse

containing the mockups for welding the recirculation

system

piping.

Full size

mockups

are being

used to train and

qualify welders for the pipe replacement

job.

The

recirculation

system safe-end,

risers,

and ring header

are

being replaced.

The licensee

is planning to temporarily

support

and lock into position the various spring cans prior

to draining

and cutting the pipe.

On May 19,

1992,

the inspector toured the Unit 3 drywell to

observe

work activities

and preparations

for the pipe

replacement.

The drywell coordinator briefed the inspector

on activities

and preparations

for pipe cutting.

The

activities in progress

were removing grating

and erection of

scaffolding.

UT

personnel

were using

a test block for

calibration of UT equipment

in preparation for conducting

a

UT of the safe-ends

weld area.

Preparations

were

on

schedule for the first pipe cut on June

1,

1992.

On June

1,

1992,

pipe cuts were

made for replacement

of the

piping.

These activities were reviewed

by

a regional

based

inspector during the weeks of June

1 -

5 and June

15 - 19,

1992.

These activities are documented

in IR 92-22.

12

Maintenance Activities

The inspector

monitored

and reviewed the maintenance activities

associated

with the pilot/prototypical program

on the

numbers

1,

5,

and

6 cooling towers.

The specific work activities observed

were those

involved with.the pre-operational

testing.

This

included troubleshooting,

meggaring of motors

and electrical

cables

and replacement

of failed oil seals

on fan gear drive

mechanisms.

The inspector noted that approximately

260

WOs were

generated

to restore

towers

1, 5,

and

6 and that

122 had

been

closed

and

43 were in the closure

process.

The inspector will

continue to monitor and review maintenance activities

and the

WO

closure process.

Pre-Operational

Testing/Return to Service Activities

1.)

Testing

The inspector monitored

and reviewed the pre-operational

testing for the pilot/prototypical program

on cooling towers

1,

5,

and 6.

The reviews involved test procedures

0-PMT-BF-

027.001,

Cooling Towers

1,

5,

and

6 Discharge

Temperature

Trip Logic and

Bypass

Switch Test;

O-PMT-BF-027.005,

Cooling

Towers

1,

5,

and

6 Logic Functional

and Lift Pump Bearing

Lube Water Annunciation Test;

and O-PMT-BF-027.007,

Cooling

Towers

5 and

6

Pump Discharge

Flow Control Valve and

Bypass

Valve Interlock Test.

Test 27.001

was initiated to verify

implementation of ECN

L 2057

and

DCN 1249, Test 27.005,

was

initiated to verify implementation of DCNs-W17703A and

W17771A;

and test

27.007

was initiated to verify

implementation of ECNs L-1929 and L-1960.

Each procedure

'tated the test objectives,

outlined the prerequisites,

discussed

the precautions,

limitations and actions, listed

the tested

equipment

as necessary,

and clearly indicated the

acceptance

criteria with the applicable

procedure

step's that

satisfied the acceptance

criteria.

The inspector

noted

two concerns.

One involved the cooling

tower

1 fan testing

when test

personnel

attached

a lanyard

to each

fan to ensure that each fan, fan gear box,

and fan

motor would not rotate

due to wind action prior to testing.

Due to lack of communication

and

second party verification

a

fan was inadvertently started with the fan blades

secured

with the lanyard.

This resulted

in a broken fan blade,

The

inspector discussed

this item with licensee

management

concerning test control.

The second

problem involved the test procedures.

While

reviewing the procedure it was noted that

a signature

was

required of the Modification Representative.

Throughout the

test procedures

the steps

are signed

by the Test Director.

The qualifications

and designations

for a Test Director are

0

13

clearly stated

in the licensee's

program.

The inspector

could. not determine

who the modifications representatives

were,

what their job titles were, or what their

qualifications were.

The inspector discussed

this concern

with licensee

personnel.

The inspector

observed

the performance of Section 5.3,

Cooling Tower

6 Fan Control Functional Test, of procedure

0-

PMT-BF-027.005.

All steps

were performed

as directed

by the

test,

communications

were adequately

established

and

controlled,

and all independent verification requirements

were met.

The inspector

concluded

from the field observations

and

reviews that the licensee

started

a pre-operational

type

testing

program for the cooling towers

1, 5,

and 6, using

approved

procedures

and were conducting the tests

in a

controlled manner.

Testing Neetings

The inspector

attended

the Unit 3, 7:00 a.m. testing

program

meetings.

This meeting

was being held on

a daily basis.

and

was patterned after the Unit 2 testing

program meeting.

The

personnel

discussed

the status

of various tests

involving

cooling towers

1, 5,

and 6, the expected testing for that

day,

any problems affecting test completion or delaying the

start of testing,

any specific group that stated

a subsystem

and/or system

was ready for test

when in fact it was not,

and

any group that did not support testing in an adequate

manner.

The inspector

noted

one difference

between

the Unit

2 testing

program meetings

and the Unit 3 meeting.

The .Unit

2 meetings

were attended

by representatives,

usually

supervisors,

from various organizations

on site,

such

as

operations,

maintenance,

technical

support, testing

program,

TVA gA, design engineering,, work planning

and scheduling,

and customer services.

The Unit 3 meetings,

were attended

by representatives

from system engineering,

testing

program,

TVA gA,

and scheduling:

The meeting did not have

a

conference

room and

was poorly attended.

The inspector

discussed

this meeting with various group supervisors

and

managers.

Several

were not aware. that the meeting

was being

held.

One significant item was discussed

and it involved

a

stop testing, similar to

a stop work situation in

construction,

on the cooling towers.

This occurred

when

during testing, wiring problems,

due to original

construction

and recently installed modifications,

were

identified.

Testing

was stopped

on June

12,

1992,

and

had

not resumed

as of June

16,

1992.

In

a previous inspection report,

the inspector

documented

several

ineffective meetings

and discussed

this occurrence

0

14

with licensee

personnel.

The inspector will continue to

attend

and monitor the pre-operational

testing meetings.

Unit-3 Safe

Shutdown Analysis

The inspector

reviewed the Unit 3 SSA.

This was issued

as

TVA

calculation

ND-(0999-910033,

dated

February

28,

1992.

The

SSA

provides

a systematic

analysis of the requirements for safe

shutdown 'for transients,

accidents,

and special

events.

The

analysis

was developed

from revision six of the Unit 2

SSA and

incorporated

open= items from the licensee's

commitment tracking

system.

It assumes

operation of Units

2 and/or

3 with Unit

1 shut

down and defueled.

Key differences

were noted

between

the Unit 3

SSA and Unit 2 SSA.

First, the Unit 3

SSA did not use

a phased

approach.

There

was

no

distinction between

equipment required for restart of the unit and

equipment that could be modified after restart.

Next, unit

interactions

were considered

with respect

to the required actions

that the shared

or common systems

take to support the event..

The list of assumptions

was reviewed

and found to be reasonable.

The Unit

1 and shared

equipment interactions

were reviewed.

The

SSA assumed

that the Unit

1 inter-unit

LOCA accident

signals

are

blocked.

This modification has already

been

performed

on Units

1

and

3 to support Unit 2 operation.

Other modifications required

on Unit 3 such

as

ATWS and

PASS are already being tracked

by other

regulatory requirements

and will not require special

tracking.

The

SSA is

a two volume document containing the analysis for

several

events.

For example,

Appendix 28, contains

the review for

shutdown

from outside the control

room,

The unit interactions

section discusses

that this special

event could affect the site

as

a whole since the loss of habitability of the control

room may

require

shutdown of all units from outside their control

rooms.

The shared

systems

were fuel oil,

RHRSW,

HVAC, ffCW, DG,

DG

starting air,

and

4K VAC distribution.

This list was consistent

with the systems

required to bring the unit of a safe hot shutdown

condition.

The inspector

concluded that the licensee

had performed

a detailed

SSA similar to Unit 2 with the differences

discussed.

From an

analytical viewpoint this provides the basis for Unit 3 to safely

be shutdown for transients,

accidents,

and special

events,

The inspector discussed

with the plant licensing staff the

need to

docket the

SSA.

The Unit 2

SSA was not placed

on the docket

and

it was concluded

a similar approach

would be used for Unit 3.

0

15

6.

Unit

1 Activities

The inspector

reviewed

and observed

the licensee's

activities involved

'ith the Unit

1 reactor vessel.

This included reviews of procedures

and

records;

observations

of field work,

QA/QC, operations

and contractor

personnel

activities;

and discussions

with licensee

and contractor

supervisors,

engineers,

and skilled craft personnel.

The IVVI of the

reactor vessel

and

steam dryer was completed.

Additional activities

included: reactor pressure

vessel

inspectability study,

and retrieval of

loose material.

The inspector will continue to monitor the Unit

1

reactor vessel activities.

a

~

Unit

1 Construction

0

On Hay 27,

1992,

the inspector toured the Unit

1 reactor building

and observed significant scaffolding erection in progress.

This

was

a concern

because

no unit separation

program exists for Unit

1

construction activities.

This program is defined in Site Standard

Practice,

SSP-12.50,

Unit Separation for Recovery Activities.

This procedure

states

Unit

1 is in layup.

Further, it explains

that the procedure will require, revision

when it becomes

necessary

to support Unit

1 recovery activities.

This concern

was discussed

with the Restart

V.P.

on Hay 28,

1992.

The work activities in Unit

1 were stated

as within the scope of

Unit 3 work.

This was explained

as all work required to support

multi-unit operation.

The physical

work was being planned for the

Unit 2 Cycle

6 outage,

since this was the last scheduled

three

unit defueling outage.

An example of this work was electrical

distribution work such

as deferred Unit

1

EQ cables

necessary

to.

support

both Unit

1

and Unit 2 operations.

The inspector

concluded that the work in Unit

1 was for Unit

1 recovery.

The

activities were being driven by schedule

convenience.

If Unit

1

were not to operate

then the work was not necessary

for Unit 2 or

Unit 3 operation.

The inspector discussed

that by controlling Unit

1 construction

work as part of Unit 2 operating

space this was in effect

integrating the operating unit and construction unit.

The

inspector stated that

some Unit 2 modifications were being worked

in advance for the Unit 2 outage to reduce

the scope of the Unit 2

outage

work.

.The Unit 3 construction activities

had sharply

increased

since

some design

change

DCNs had

been

issued.

These

coupled with construction activities

on Unit

1 would increase

the

chance for construction activities to affect the operating unit.

The Restart

VS P. stated that the Unit

1 activities would be

stopped until the issue

was reviewed.

This was also discussed

with the V.P. of Operations.

A meeting

was held in the Region II office in Atlanta,

Georgia

on

June

11,

1992 to discuss

these

issues.

As discussed

at this

16

meeting,

the activities

on Unit

1 would be limited to walkdown

activities required to prevent

a three unit defueling outage in

the future.

The walkdowns would be performed

by a dedicated

crew

of 30 people with the activities treated

as

a Unit 2 operating

space

work.

The activities will be listed in the plan of the day

handout.

Any departure

from the activities discussed

would be

reviewed with the

NRC.

Additional Activities

The licensee. provided the inspector with a list of modifications

resulting from multiple unit operation

mechanical

studies,

multiple unit operation electrical studies,

and evaluation of

future multiple unit outages.

Some of the modifications involved

the following:

DCN W17792,

Shutdown

Board

Room HVAC.

This modification is similar to the Ellis & Watts air

conditioners installed

on top of electrical

board

room 2A.

The

new

HVAC units will be located

in Unit

1 reactor

building,

and will provide qualified

HVAC to 4160V Shutdown

Boards

A and

B,

480 volt shutdown

boards

IA and

1B,

480V

RNOV Boards

1A and

1B,

and

250V

DC

RMOV board

1A and

1B.

DCN W18230,

EECW/RCW Valve Actuator Change.

This modification will change

out water actuated

valves

1-

FCV-67-50 and

51

and replace

them with pneumatic

operated

valves.

These

valves provide

EECW cooling to the two Unit

1

RBCCW heat exchangers

and the spare

heat exchanger

in case

of a loss of RCW.

The valves

are located in the Unit

1

reactor building.

Unit

1 Equipment

Impacting Unit 2 and

3 Operations.

These

items involve equipment,

electrical

cables,

and

end

devices,

that are located in Unit

1 spaces

and could impact

operation of Unit 2 and/or 3.

The latest information

received

from the licensee

indicated that

19 cables

could

impact Unit 3.

No information had

been received

as to the

identified impact

on Unit 2 operations.

DCN W17725, Unit

1 Non-1E Battery Addition - Unit Battery

and Battery Board 5.

This modification will install

a new battery room, battery,

battery charger,

DC electrical

switch board

and associated

ventilation system in the Unit

1 turbine building.

DCN W17721,

Replacement

of 4KV/480V Transformers

TSIA and

TS1B.

17

This modification will replace

two 750

KVA transformers

located in the Unit

1 reactor building, with two 1000

KVA EQ

transformers.

DCNs W17620

and

WXXXX, Reinstall Unit

1

RHRSW to

RHR Heat

Exchangers.

The second

DCN had not been

numbered

as of this reporting

period.

These

two modifications will reinstall

the. present-

ly cut and capped

RHRSW piping,

make the piping seismically

qualified and possibly rework or remove dresser

couplings.

The piping is located in the Unit

1 reactor building and

RHRSW tunnels.

Additional modifications involved the control air system,

Unit 1/2 control

bay

HVAC ductwork,

CREVS, Unit

1

HWWV,

off-gas

and standby

gas stack,

load tap changers

for the

CSSTs

and

USSTs, Unit

1 turbine building crane,

NFPA upgrade

for the cable spreading

A, and Unit

1 generator rotor

rebuild.

C.

Reactor

Vessel

The inspector

reviewed

and observed

the licensee's

activities

involved with the Unit

1 reactor vessel.

This included reviews of

procedures

and records;

observations

of field work,

QA/QC,

operations

and contractor

personnel

activities;

and discussions

with licensee

and contractor supervisors,

engineers,

and skilled

craft personnel.

The followup reviews of indicators identified by

UT of the in-vessel

manways

were discussed.

This involved

unexpected

indications

on one of the

manways that will require

additional

inspection

and evaluations.

The licensee

discussed

these indications with Region II senior

management.

The inspector

will continue to monitor the Unit

1 vessel activities.

Licensing Activities

The inspector

noted

a declining trend in complete

and accurate

licensing

submittals to the

NRC.

First, several

LERs had to be resubmitted.

This

is discussed

in 'the paragraph

on reportable

occurrences

in this IR.

Second,

the response

to

a violation in IR 92-03 contained

inaccurate

information and

a revised

response

was requested.

Third, the response

to'

violation in 'IR 92-12 did not address

the management

controls

specifically requested

in the IR.

Collectively, these

examples

represent

a negative trend in adequate

licensing submittals.

Each of

these

items

was discussed

with licensee

management

and the revised or

supplemental

responses.

1 8

8.

Reportable

Occurrences

(92700)

The

LERs listed below were reviewed to determine if the information

provided met

NRC requirements.

The determinations

included the

verification of compliance with TS and regulatory requirements,

and

addressed

the adequacy of the event description,

the corrective actions

taken,

the existence

of potential generic problems,

compliance with

reporting requirements,

and the relative safety significance of each

event.

Additional in-plant reviews

and discussions

with plant

personnel,

as appropriate,

were conducted.

Several

discrepancies

were noted

by the inspector that indicated

a lack

of attention to detail

by the writer'.

This was discussed

with the

compliance

manager;

.and

he indicated that the

LER's would be corrected

and resubmitted

to the

NRC.

1.

259/92002,

Unplanned

Engineered

Safety Features

Actuation Because

of an Unexpected

Reactor Protection

System Failure.

The event date

was incorrect in several

blocks throughout

the report.

The

LER sequential

number located in block 6 was incorrect

on several

pages.

This

LER stated

there were

no previous

LER's on similar.

events.

2.

260/92003,

Inadvertent

Group

4 Isolation During Performance

of the

High Pressure

Coolant High Temperature

Functional Test.

The report date in block 7 was blank.

The description of the event indicated the isolation

occurred at 0400 instead of the correct time of 0440.

0

9.

3.

260/92004,

Automatic Reactor Scram

on

Low Reactor

Water Level

Due

to Failure of the Feedwater

Level Control

System.

Block 8 did not list Unit's

1

and

3 as other facilities

involved even though the control

room emergency ventilation

and standby

gas treatment

system

are

common to all unit's.

Action on Previous

Inspection

Findings

(92701,

92702)

(CLOSED)

URI 259,260,296/92-11-02,-Hissing

Independent Verification

Steps.

During the performance of 0-SI-4. 11.B.2.a,

Diesel Fire

Pump Operability

Test,

the inspectors

noted

two steps that did not require

independent

verification.

Step 7.3.8.9. placed the Diesel

Driven Fire

Pump Strainer

Backwash Control Switch to Auto but did not independently verify its

position.

The licensee

stated

the independent verification was not

required,

based

on satisfactory

performance of a test conducted

in June

1989,

which operated

the

pump for two hours without allowing the

19

strainer to backwash.

The licensee further stated

the strainer is

backwashed

weekly during the performance of the SI and that

based

on

previous experience,

the strainers

are not likely to clog in such

a

manner

as to affect the operability of the

pump or prevent the system

from performing its design function.

Step 7.3.12.5

placed the Diesel

Fire

Pump Controller Selector

Switch to Auto following performance of

the SI, but did not independently verify its position.

The licensee

stated that independent verification of this step

was not required in

that step 7.3. 12.8 verifies correct positioning of this switch by

observing that annunciator

I-XA-'5-8E, Window 44,

DIESEL

PUMP

LOCAL CONT

IN MNL OR OFF, is not in alarm.

Regional Office Notice

2201,

dated

August 18,

1983 maintains this method of independent verification is

acceptable.

Based

on the above information this item is considered

closed.

Exit Interview (30703)

The inspection

scope

and findings were summarized

on June

19,

1992 with

those

persons

indicated in paragraph

1 above,

The inspectors

described

the areas

inspected

and discussed

in detail the inspection findings

listed below.

The licensee

did not identify as proprietary

any of the

material

provided to or reviewed

by the inspectors

during this

inspection.

Dissenting

comments

were not received

from the licensee.

Item Number

Descri tion and Reference

260/92-21-01

260/92-21-02

259,

260,

296/92-21-03

NCV,

RWCU Drawing Error, paragraph

three.

IFI, Adequacy of Scaffolding Review, para-

graph three.

VIO, Failure to Adequately Disposition

Nonconforming MME, paragraph

four.

Licensee

management

was informed that

1

URI was closed.

Acronyms

and Initialisms

ASOS

ATWS

AUO

BFNP

BTRD

CCW

CFM

CFR

CLSD

CRDR

CREVS

CSSC

CSST

DCA

Assistant Shift Operations

Supervisor

Anticipated Transient Without Scram

Auxiliary Unit Operators

Browns Ferry Nuclear

Power Plant

Baseline

Test Requirements

Document

Condenser

Cooling Water

Cubic Feet

Per Minute

Code of Federal

Regulations

Central

Laboratories

Services

Department

Control

Room Design

Review

Control

Room Emergency Ventilation System

Critical Structures,

Systems,

and

Components

Common Station Transformers

Drawing Change Authorization

DCN

DD

DG

ECN

EECW

EOI

EQ

FCV

HVAC

HWWV

IFI

IR

IVVI

KV

LCO

LER

LOP/LOCA

MOV

MR

M&TE

NCV

NFPA

NQA

NRC

PCIS

PMT

POI

QA

QC

Radcon

RBCCW

RCW

RHR

RHRSW

RMOV

RTO

RWCU

SALP

SI

SPAE

SPOC

SSA

SSP

URI

USST

VIO

VP

WO

WP

WR 20

Design

Change Notice

Drawing Discrepancy

Diesel

Generator

Engineering

Change Notice

Emergency

Equipment Cooling Water

Emergency Operating Instruction

Environmental Qualification

Flow Control Valve

Heating, Ventilation,

& Air Conditioning

Hardened

Wet Well Vent

Inspector

Followup Item

Inspection

Report

In Vessel

Visual Inspection

Kilo-volt

Limiting Condition for Operation

Licensee

Event Report

Loss of Power/Loss of Coolant Accident.

Motor Operated

Valve

Maintenance

Request

Measuring

and Test Equipment

Non-Cited Violation

National Fire Protection Association

Nuclear Quality Assurance

Nuclear Regulatory

Commission

Primary Containment Isolation System

Post Maintenance/Modification

Test

Plant Operating Instruction

Quality Assurance

Quality Control

Radiological

Controls

Reactor Building Closed Cooling Water

Raw Cooling Water

Residual

Heat

Removal

Residual

Heat

Removal

Service

Water

Reactor Motor Operated

Valve

Return to Operation

Reactor

Water Cleanup

Systematic

Assessment

of Licensee

Performance

Surveillance Instruction

System Plant Acceptance

Evaluation

System Pre-Operation

Checklist

Safe

Shutdown Analysis

Site Standard

Practice

Unresolved

Item

Unit Service Station Transformer

Violation

Vice President

Work Order

Work Plan

Work Request

0

0