ML18033B015

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Insp Repts 50-259/89-47,50-260/89-47 & 50-296/89-47 on 890925-29.Violations Noted.Major Areas Inspected:Disposition of Historical List of Tech Specs Problems,Tva Task Force Audit of Tech Specs & Comparison of Sys Design
ML18033B015
Person / Time
Site: Browns Ferry  Tennessee Valley Authority icon.png
Issue date: 10/20/1989
From: Little W, Patterson C
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18033B012 List:
References
50-259-89-47, 50-260-89-47, 50-296-89-47, NUDOCS 8911030133
Download: ML18033B015 (23)


See also: IR 05000259/1989047

Text

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W.

ATLANTA,GEORGIA 30323

Report Nos.:

50-259/89-47

50-260/89-47,

and 50-296/89-47

Licensee:

Tennessee

Valley Authority

6N 38A Lookout Place

1101 Market Street

Chattanooga,

TN

37402-2801

Docket Nos.:

50-,259,

50-260

and 50-296

License Nos.:

DPR-33,

DPR-52,

and

DPR-68

Facility Name:

Browns Ferry 1, 2,

and

3

Inspection

Conducted:

September

25-29,

1989

Inspecto

C. A.

a

son,

Team Leader

D te Si

ned

Team

mbers:

M. Marini

D. Nelson

Approved by

W.

S. Lit

e, Section Chief

Inspection

Programs

TVA Projects Division

Da

e Signed

SUMMARY

Scope:

This special

announced

inspection of Technical Specification

(TS) was conducted

to review the disposition of a historical list of TS problems,

TVA's task force

audit of TS,

a comparison

of system

design

basis

to

TS surveillance

require-

ments,

and

a corn'parison

of TS to the plant configuration.

Results:

Disposition of a historical list of TS problems

was nearly complete with most

of the restart

TS changes

completed.

Action taken to resolve

these

issues

was

good.

The disposition

of the

TS task

force

recommendations

needed

attention

to

resolve

the restart

TS issues

in

a timely manner.

Review by the

RRB using the

Restart Criteria

had

not

begun

during the week of the inspection.

Thirty-six

items were awaiting

PORC review.

Since the licensee

was still in the

process

9110301.

.S5'1021

PDFl

ADOCK 05I.I00259

9

PDC

of resolving

these

issues,

the

inspection

team

could

not confirm that all

restart

TS changes

were identified.

Review of the

TS amendment

concerning

TS 3.7.F

(item

061)

indicate

the

quality

of

reviews

could

be

improved,

paragraph

3.

A violation with three

examples

concerning

document

control of

a technical

specification

amendment

and

updating controlled copies

of TS

was identified.

These

examples

resulted

from inattention

to detail

and were not an indication

of a programmatic

problem.

The examples

are in paragraphs

2 and 4.

Two

IFIs

were

identified:

one

related

to

RHR

cross-tie

operability

(paragraph

5),

and the other related to

a failure to implement

a

TS Task Force

recommendation

in making

a

TS change

(paragraph 3.a.).

REPORT DETAILS

1.

Persons

Contacted

Licensee

Employees:

0. Zeringue,

Site Director

G. Campbell,

Plant Manager

"R. Smith, Project Engineer

J. Hutton, Operations

Superintendent

"A. Sorrell, Maintenance

Superintendent

G. Turner, Site Quality Assurance

Manager

  • P. Carier, Site Licensing Manager

"P. Salas,

Acting Compliance Supervisor

"J. Corey, Site Radi.ological

Control Superintendent

R. Tuttle, Site Security Manager

Other

licensee

employees

or

contractors

contacted

included

licensed

reactor operators,

auxiliary operators,

craftsmen,

technicians,

and public

safety officers;

and quality assurance,

design,

and engineering

personnel.

NRC Attendees

"M. Little, Section Chief

  • D. Carpenter,

Site Manager

"C. Patterson,

Restart

Coordinator

  • E. Christnot,

Resident

Inspector

  • M. Bearden,

Resident

Inspector

  • Attended exit interview

Acronyms used throughout this report are listed in the last paragraph.

2.

Historical List of TS Problems

During the period of time that

BFNP has

been

shut down,

a number of items

have

been identified which necessitated

revisions

or upgrades

to the

TS.

These

items were identified in a variety of ways, including

NRC Inspection

Reports,

LERs, Generic Letters,

and

10 CFR 50, Appendix

R.

As

a result of

several

meetings

and

conversations

between

licensee

personnel

and

NRC

staff,

a list of 54 such items

was compiled in March

1987.

Of these,

31

were determined to require submittal

and approval of the affected

TS prior

to restart of Unit 2.

The

team

reviewed

these

31 restart

items

and

two

nonrestart

items to determine

whether the affected

TS had been

revised

and

whether the revision adequately

addressed

the identified concern.

Below

is

an

item by item description identified by the

item number

from the

March,

1987 list of

TS revisions.

Unless

otherwise

noted,

the

team's

review found that the licensee's

actions

were appropriate

and acceptable.

~ >

(Note:

When

a series of three

amendment

numbers is listed, they represent

the applicable

amendments

for Unit 1, Unit 2,

and Unit 3, respectively)

ITEM 2)

Amendment

134,

130,

105, (7-17-87) revised

TS Table 3.1.A to

delete

the applicability of alternate

action 1.B. from APRM high

flux and

inoperative trip functions.

This

alternate

'action

could

have

erroneously

allowed the reactor

to

be placed

in

an

operational

condition where trip functions

were required to

be

operable,

but were not.

ITEM 3)

ITEM 5)

ITEM 6)

ITEM Ba)

Amendment. 133,

129,

104 (5-13-87) revised

TS

LCO 3.3.B. 3 to

clarify RWM operability

requirements.

Amendment

143,

139,

114 (2-12-88) revised

TS

LCOs 3.7.B.2.b,

3.7.E.2.b,

and

3.7.F.2.b

to

revise

the

methodology

and

acceptance

criteria for laboratory analysis

to verify charcoal

absorption

efficiency for SBGT,

CREV,

and

Primary Containment

Purge

systems,

as the previous methodology

was outdated.

Amendment

138,

134,

109 (9-11-87) revised

TS 6.0 to update

and

clarify minimum plant staffing levels

and onsite organizations

Amendment

158,

154,

129 (11-18-88) revised

Note 01 of TS

Definition 1.0

~ M to allow the

mode

switch to

be

temporarily

placed

in any position in order

to perform required tests

or

maintenance

when the reactor is in the

shutdown or refuel

modes.

ITEM 8b)

Amendment

158,

154,

129 (11-18-88) revised

TS Definitions 1.0.S

and

1.0.M to link more directly with mode

switch position

and

make

them applicable

only

when

there is fuel in the reactor

vessel.

ITEM 8c)

Amendment

158,

154,

129 (11-18-88) revised

TS Definition 1.0.J

to more clearly define the term startup.

ITEM 8d)

Amendment

158,

154,

129 (11-18-88) revised

TS Definition 1.0.K

to clarify the

term

COLD

SHUTDOWN

CONDITION to include

both

shutdown

and refuel

modes.

ITEM 9)

Amendment

135,

131,

106 (8-20-87) revised

TS Definition 1.0.C.2

to clarify its applicability during Cold Shutdown or Refueling.

The

team

determined

this clarification to

be

appropriate.

However,

an

additional

concern

was

identified.

Although

this

revision

was

approved

in

1987,

page

1.0-2

currently

located

in controlled

copies

of the

TS did not reflect

the

approved

and

issued

change.

Information

provided

by

the

licensee

revealed

that,

at the time the

change

was

approved,

the correct wording was incorporated into the controlled copies

of the

TS and

had not been

incorporated into the

TS master

copy.

In February

1989,

TS Amendment

158,

157,

129 revised different

information contained

on the

same

page.

Upon approval,

the

new

changes

were

made to the

TS master

copy

and distributed to the

controlled copies

of the

TS.

This resulted

in inadvertent

use

of

outdated

wording

in

TS

Definition

1.0.C.2.

This

is

considered

a failure to maintain

adequate

control of changes

to

approved

documents,

as

required

by

10 CFR 50,

Appendix

B

Criterion VI, Document Control,

as committed to by

NQAH Part I,

Section 2.6,

as

implemented

by

SDSP

2. 12,

and is identified

as

example

one

of Violation

259,

260,

296/89-47-01,

Document

Control of TS.

ITEM 10)

ITEM 12)

This item involved confusing information in TS 3/4.5.C

pertaining to the operability requirements

for RHRSW pumps.

The

licensee

had

submitted

proposed clarification of these require-

ments in TS-242,

which is currently under

review by

NRC staff.

This item involved incorrect information regarding

HPFPS

stations

3.A, 3.B,

and 3.C in

TS Table

3. 11.A.

Amendment

162,

159,

133 (12-12-88)

encompassed

a general

rewrite of TS 3/4.11

to eliminate ambiguity and bring

BFNP into conformance with

BWR

STS

and other current industry practices.

ITEM 13)

This item involved the discovery that, although

TS 4.11.D

required

the Safety Engineer to perform

a monthly inspection of

plant fire protection

systems,

TS 6.0 did not provide for

a

Safety

Engineer

in the site organization.

The administrative

and

technical

changes

referenced

in

items

6

and

12,

above,

provide

adequate

clarification

of

this

requirement

and

responsibility.

ITEM 14)

This item involved the observation

that

TS 6.0 did not

accurately

describe

the

current

onsite

organization.

The

administrative

changes

referenced

in item 6,

above,

adequately

resolve this observation.

ITEM 15)

Amendment

127,

122,

98 (2-26-86) provided for the establishment

of

a

procedure

to limit the

amount

of overtime

worked

by

personnel

performing

safety

related

functions,

in

accordance

with GL 82-12.

ITEM 17)

Amendment

139,

135,

110 (1-25-88) revised

TS 6.8.3.1 to clarify.

the access

requirements

to high radiation

areas

where the

dose

rate is greater

than

100 mr/hr but less

than

or equal to 1000

mr/hr.

ITEM 18)

This item involved the evaluation of TS Table 3.7.A, Primary

Containment

Isolation

Valves,

for

possible

additions

or

corrections.

The

licensee

had

completed

their

review

and'ubmitted

proposed

changes

via

TS-251

(8-2-88)

and

TS-251,

supplement

0'1 (7-13-89).

These

pro'posed

changes

are currently

under review by

NRC staff.

ITEM 22)

Amendment

140,

136, ill (1-19-88) revised

TS Table 3.2.A to

change

the trip level setting for SBGT Relative Humidity Heaters

to 2000 cfm to prevent

damage to the

SBGT filter banks.

ITEM 27)

ITEM 31)

Amendment

145,

141,

116 (2-29-88) revised

TS Definition

1.0.0;3,

TS 3.7.D. 1,

and

TS 3.7.D.2 in order to

make

Primary

Containment Integrity definition, operability requirements,

and

action statement

consistent with each other.

Amendment

150,

146,

121 (7-5-88) revised

TS

SRs 4.7.E. 1,

4.7.E.3,

4.7.F. 1, 4.9.A.2.c,

and

4. 11.A.5 to replace

the words

"not to exceed" with the words "at least

once every" in order to

provide

consistency

with surveillance

interval

requirements

contained in TS Definition 1.0.LL.

4

ITEM 36)'mendment

155,

151,

126 (9-23-88)

added

HPCI and

RCIC

functions to TS Tables 3.2.B and 4.2.B and to the

notes for TS

Table 3.7.A to complete

the lists of Groups

4 and

5 isolation

functions.

ITEM 37)

Amendment

147,

143,

118 (3-3-88) provided several

corrections

as follows:

Clarified Note 7.d for Table 3.2.C, pertaining to Rod Block

Monitor operability

Revised

TS 2. 1.A. l.d to show

SR 4.5.L as the correct

SR for

APRM Scram Setpoints

Deleted

Note

14

from Table

4.2.A,

as it is

no

longer

applicable to any instruments

in the table

Revised

TS 3.6.H to

show

SI 4.6.H-1

and 4.6 AH-2 as

being

the SIs that list safety related

snubbers

One additional

concern originally included within the

scope of

this

item

involved

confusing

notes

pertaining

to

Primary

Containment

and

Reactor

Building

Isolation

Instrumentation.

Note ll of Table 3.2.A stated that

an instrument

channel

may be

placed in an inoperable

status for up to four hours for required

surveillance,

while Note

22 of Table 4.2.A stated that certain

RMS channels

may be administratively bypassed for up to 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />

for functional testing

and calibration.

The licensee

did not

feel

a

TS clarification change

was desirable

at this time, since

an

upcoming

equipment modification to these

RMS channels will

ITEM 38)

ITEM 39)

ITEM 43)

ITEM 44)

necessitate

TS

changes

and the confusion

concerning

the

notes

can

be

resolved

at that

time.

This

concern

was originally

identified

by

NRC in

IR 86-05

as

IFI 86-05-07.

Additional

followup information

regarding

this IFI is contained

in

IR

89-19,

which identified this

as

an

issue

requiring resolution

prior to Unit 2 restart.

Amendment

137,

133,

108 (8-26-87) revised the drywell leakage

monitoring

requirements

in

TS 3.6.C. l.b, TS,4.6.C. 1,

and

TS 3.6.C.2 to reflect the guidance

contained

in GL 84-11.

Unit 2 Amendment

164 (5-16-89) revised

TS 3/4.1.B to add

'urveillance

requirements

and

correct

the

overvoltage,

undervoltage,

and underfrequency trip settings for the

RPS power

monitoring system.

Amendment

141,

137,

112 (2-3-88) revised

TS 4.7.A.2 and

TS 4.7.A.4 to correct

containment

leak rate

testing

requirements

and delete the option of'erforming

a reduced

pressure

test,

as

such

a test could yield nonconservative

results.

Amendment

142,

138,

113 (2-12-88) revised

TS 3.7.A.5 and

SR 4.7.A.5.c to limit the use of air for pneumatic

control inside

containment,

to reflect the guidance

contained

in GL 84-09.

ITEM 45)

Amendment

154,

150,

125 (9-2-88) revised

TS 3/4.4 to meet

SLC

shutdown requirements

for future fuel cycles,

and to comply with

ATWS requirements

of 10 CFR 50.62.

ITEM 46)

Amendment

153,

149,

124 (8-19-88) revised

TS 3/4.5, 3/4.9,

and

6.9.7 to improve

DG reliability by decreasing

the

number of fast

diesel starts,

to reflect the guidance

contained

in GL 84-15.

ITEM 47)

ITEM 48)

ITEM 50)

Unit 2 Amendment

162 (1-30-89) revised

TS Tables 3.2.B and

4.2.B to change

the trip setpoint for the existing

ADS timer,

and

add

surveillance

and

setpoint

requirements

for

a

high

drywell

bypass

timer,

in

accordance

with

NUREG-0737,

Item II.K.3.18.

I

This item involved

a proposed

TS change

to demonstrate

that ARI

equipment

can satisfy

the reliability requirements

of the

ATWS

Rule,

10 CFR 50.62.

Conversations

with licensee

personnel

and

NRC staff determined that such

a change

is not required at this

time.

NRC staff will provide

guidance

on

a

generic

basis

regarding

TS requirements

for ARI at

a future date.

Unit 2 Amendment

172 (9-13-89)

updated

the Unit 2 TS to reflect

the Reactor

Core Operating Limits for Cycle 6.

ITEM 52)

Amendment

152,

148,

123 (8-8-88) .revised

TS Table 3.7.A to

increase

the stroke time for LPCI injection valves

FCV-74-53 and

-67 from 30

seconds

to

40

seconds

due to valve motor operator

modi ficati on s requi red to meet

10 CFR 50. 49 criteri a.

ITEM 53)

Amendment

160,

157,

131 (11-28-88) revised

TS 1.1.C to delete

all references

to "top of active fuel" when measuring

reactor

water level,

and to describe all involved setpoints

as

"above

vessel

zero".

ITEM 54)

This item involves proposed

TS additions pertaining to testing

requirements

necessary

to

demonstrate

remote

shutdown

capability,

as required

by 10 CFR 50, Appendix

R.

The licensee

has

submitted its proposed

Appendix

R TS enhancements

via TS-.268

(4-14-89).

This

submittal

is currently

under

review

by

NRC

staff.

3.

TS Task Force'udit

To fulfill a commitment

made in

LER 260/89001,

Fuel

Load Without Adequate

Neutron

Monitoring

Due

to

Inadequate

Safety

Review

of

Technical

Specification

Amendments,

an assessment

was 'conducted

of the

BFNP Unit 2

TS.

The

licensee

established

a

TS

assessment

team

consisting

of ten

members with nuclear

work experience

ranging

from

8 to

27 years.

The

final report was issued

March 31,

1989.

The

team

developed

four major objectives

to perform the

assessment.

A

summary of the four objectives

and the licensee's,conclusion

follows:

Objective

A was

an evaluation

of the effectiveness

of the

TS change

control

program.

The task

force

concluded

that

the

process

was

effective in identifying necessary

changes

to

TS

and

implementing

procedures.

Objective

B

was

to

evaluate

the

current

TS

interpretations

to

determine their compatibility with the

intent of

TS

requirements.

The task force concluded that the

TS interpretation

manual

contained

four nonconservative

interpretations

and

nine

outdated

interpreta-

tions.

CAgRs were written to track resolution of these deficiencies.

Objective

C was to provide confidence

that

TS accurately

reflected

plant design

basis criteria.

The task force concluded that the

TS

consistently

reflect

plant

design

criteria.

Of the

18

issues

identified none were determined

to be significant by the task force.

Objective

D

was

to provide confidence that

TS contained

essential

requirements

to

ensure

safe

plant

operation.

The

task

force

concluded

that

BFNP

TS

contained

essential

requirements,

however,

significant issues

were identified which when resolved

would enhance

the ability to safely operate

Unit 2.

Of 99 issues

identified,

two

were

recommended

for Unit

2 restart

TS

changes.

Eighty-three

of

the

issues

were

recommended

for restart

administrative controls

and

evaluation.

The remaining

14 issues

were categorized

as post-restar't

action items.

From the

four objectives the

18 items in

C and

99 items in

D were placed

into several

categories

of action

items.

Each

item was designated

by

a

letter and

number

as Cl, C2, or the appropriate

designation for the item.

After the

TS

task

force

performed

the audit

a

group of

BFNP plant

personnel

were

assembled

consisting

of

licensing

engineers,

system

engineers,

and operations

personnel

and others

to answer

the

items

and

prepare

the action item.

The .action in

some

cases

was the preparation

of

procedure

revision for submittal to

PORC.

Several

more restart

TS changes

were identified by the plant group.

The inspector

questioned

whether

the Restart Criteria in Volume

3 of the

NPP were

being

used

to evaluate

whether

an

item was

a restart

TS change

or post restart

change.

At the

end of the inspection

none of the

items

had

been

reviewed

by the

RRB.

Additionally, 'the

RRB review would

come

after

a

PORC review of

some

items.

There

were

an

estimated

35

items

awaiting

PORC

approval.

Included

in this

were

10 items designated

as

post restart

TS changes.

The inspector

concluded that the licensee

was still in the decision

making

stage

for determination

of whether

items were restart

or not.

This

was

also supported

by the

TS task force recommendation

of 2 restart

TS changes

compared

to

a total of

6 after

the plant staff review.

Considerable

variation

of the

numbers

could result

following

PORC

review

and

RRB

review, with new items designated

as post restart

TS changes.

The inspector

determined this portion of the inspection

could not

be

a

confirmatory one

since

the actions

to address

the task force

items

were

still being reviewed.

The inspection

could only be

somewhat of a quality

check

on the items in progress.

The inspector briefly reviewed

the entire list of findings.

In general,

the

inspector

thought

the

task

force

items

were well thought out

and

conservative reflecting the experience

level of the task force.

Accordingly the

inspector

reviewed

in detail

a

sampling

of the

items

identified by the

TS task force.

The first two items

(D8 and

D61) were

identified by the

TS task force

as restart

items.

A discussion

of the

inspection of these

items

and other items follows:

a.

Audit Item

D 61

The task force

recommend

a

TS change prior to restart for TS 3.7.F,

Primary Containment

Purge

Vent and

Exhaust.

The present

TS states

that primary containment

shall

be normally vented

and purged through

the

primary

purge

system.

The

SBGT

may

be

used

when the primary

containment

purge

system is inoperable.

The task force concern

was

that for normal venting,

during

power operating conditions the

SBGT

was the

preferred

path

and

the technical

specification'hould

be

amended

accordingly.

The inspector. reviewed

the

BFNP

TS submittal

dated

August 4,

1989,

and

concluded

that

the

submittal

did not

address

the

task

force

concern.

No statement

was

added to allow the preferred

vent path.

The

second

sentence

of 3.7.F. 1 concerning

using

SBGT

when

primary

containment

purge

is

inoperable

was

eliminated

from

the

LCO

statement.

This part of the

LCO statement

was

moved to the

BASES.

This represents

a fundamental

mi sunderstanding

of

LCO statements

and

TS BASES.

10 .CFR 50.36 states

the

BASES are not part of TS.

The

statement

added

to the

BASES would

have better

described

the

operation

of the

purge

system.

The

statement

was that the primary

containment

purge

and ventilation system

may be

used

as part of the

inerting/deinerting

process

for 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> following placing the

mode

switch in the

RUN position or 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> prior to shutdown.

This is

the

purpose

of the

purge

system.

During

power

operation,

the

primary containment is isolated

by two isolation valves in series.

The licensee

decided

to revise

the submittal.

Inspector

Follow-up

Item

259,

260,

296/89-47-03

is

designated

to follow-up

on this

action.

b.

Audit Item

D8

The

task

force

recommended

a

TS

change

prior to restart

for

TS 3.2.A-1.0,

concerning

isolation of shutdown cooling.

BFNP TS action

1.0 in Tables 3.2.A notes that for inoperable isolation function that

shutdown. cooling

should

be

isolated.

The

task

force felt that

shutdown cooling should

be allowed to remain

in service

even if the

automatic

isolation capability

becomes

inoperable.

Other 'compensa-

ting action

could

be acceptable

and at

a

minimum

a" time should

be

allowed to establish alternate

decay

heat

removal capability prior to

isolation.

'I

The inspector

concurs with a

TS change

for establishing

an alternate

decay

heat

removal

prior to isolation.

In discussion

with the

licensee

consideration

was

being given to allowing six hours.

The

inspector

noted

that

STS

requires

the

affected

system

isolation

valves

be closed

and locked within one hour and declare

the affected

system

inoperable.

The

one

hour time period

seemed

adequate

for

establishing

an alternate

cooling

method.

Any deviation

from

STS

regarding this matter should

be fully explained

in TVA's submittal.

The licensee

stated

the time difference would be reviewed.

Audit Item C8

The task

force identified the

RPS

requirements

of 3. 1.A.

do not

require

the

IRM inoperative tr ip or the

APRM inoperative tr ip while

in shutdown.

These functions should

be required

OPERABLE anytime the

high flux trip is required.

The table

also

does

not require

APRM

high in shutdown,

however,

note

7 applied to the

REFUEL heading

seems

to indicate it should

be applicable.

The task force

recommended

that

controls

be established

prior to restart followed by TS changes.

The

plant staff

determined

this

item

as

acceptable

and correct

with no administrative

controls

needed

or

TS changes

required.

The

basis for this was stated that the exi sti ng plant design

and hardware

interlocks

make it impossible

for any control

rod to

be

at

any

position

other

than fully inserted

when

the

mode

switch is

in

shutdown.

Note

7 applied to

REFUEL only.

The inspector

reviewed

note

7,

and the table.

Note

7 was beside

the

column heading of the Table 3. 1

~ A for REFUEL only.

However,

Note

7

states

the following:

When

the

reactor

is

subcritical

and

the

reactor

water

temperature

is

less

212

degrees

F,

only the

following trip

functions

need to be operable:

A.

Mode switch in

SHUTDOWN

B.

Manual scram

C.

High flux IRM

D.

Scram discharge

volume level

E.

APRM 15 percent

scram

F.

Scram pilot air header

low pressure

The

inspector

reviewed

STS

and

found that the

RPS trip functions

were

required

for operating

mode

5

which is

both

Shutdown

or

Refuel.

Furthermore

in

BFNP

TS Section 1.0 for definitions it was

noted that definition M.,

Mode of Operation,

for

shutdown

mode

and

refuel

mode

has

a footnote

(1).

This footnote

allows

the

mode

switch to

be placed

in any position to

perform required

tests

or

maintenance

authorized

by the shift operations

supervisor,

provided

that the control

rods

are verified to remain fully inserted

by

a

second

licensed

operator

or other technically qualified

member

of

the unit technical staff.

Since

the

function of

RPS

is

to protect

the

core,

these trip

functions

might

be

applicable

in

the

shutdown

mode

also.

The

inspector

has

concern

with the

task

force finding

and

should

be

reviewed further prior to restart.

10

Also,

the

inspector

was

concerned

that

the

plant staff did not

evaluate

the difference

between

STS

from

a

standpoint

that

more

protection

might be

needed for. the reactor.

The evaluation

was .only

from the standpoint that the existing controls were justified.

The licensee

stated this item would receive further review.

d. 'udit Item D39

The task force identified that the value of "tau" which is

a factor

to account for scram

response

time in the calculation of the minimum

critical power ratio

should

be administratively controlled

as

equal

to

one until

scram

time

measurements

and

"tau" calculations

are

completed

at the beginning of each cycle.

TS 4.3.C requires

scram

time testing

be

completed prior to exceeding

40K. power after

each

refueling outage.

A TS change is to be submitted after restart.

TVA agreed

to the administrative

controls prior to restart

and to

.

keep the controls in effect until

a

TS

a change

was

made.

BFNP, TS 4.5.k.2.a

requires "tau" equal

to 0.0 prior to initial scram

time measurements

for the cycle.

STS

in surveillance

requirement

4.2.3 states

"tau" should

be

equal

to 1.0.

If BFNP implements

the

administrative controls,

they will be in violation of BFNP T.S.

The

inspector

concluded

that

as

a conservative

approach,

and to

be in

compliance with TS, the value of "tau" should

be changed.

The

licensee

agreed

that

to get "tau"

equal

to

1.0

would

be

a

noncompliance

item and that the surveillance

requirement

would remain

at

0.0 until the

TS

was

changed.

Administrative controls

would

review

a calculation

using 1.0 until the

TS was updated.

e.

Comparison of BFNP to Standard

TS

The licensee's

audit included

a comparison

of BFN TS to

STS for BMRs.

Recognizing

numerous

minor differences,

the

licensee

established

an

undefined

level

of significance

for

documenting

differences.

The

inspector

selected

one

system,

SLC,

and

conducted

an

independent

comparison

between

BFNP TS and

STS in order to determine

the depth of

comparison

conducted

by the

licensee.

The

following differences

noted

by the inspector

were not documented

by the licensee.

Also,

only differences

where the

BFN TS are less conservative

than

STS are

identified:

Pump Operability:

Verified by BFN TS 4.4.A. 1 quarterly

vs

STS 4. 1.5.b. 1 monthly.

System Valve Lineup:

Not verified by

BFN /TS vs

STS

4. 1. 5.b. 4 monthly.

11

Explosive Charge:

Continuity not verified by BFN TS vs

STS

4. 1.5.b.2

monthly.

Replacement

required to be

no older than

5 years

by

BFN

TS 4.4.A.2.c

vs

STS 4.1.5.c.l

required

to

be

from

same

manufactured

batch

as

one tested.

Infrequent Surveillances:

Once per cycle,

no operational

condi tion

speci fi ed

by

BFN

TS vs

STS

4. 1.5.c

once per

18 months,

shutdown.

These difference

were discussed

with the licensee

as observations

and

do

not represent

a concern

about

the quality of the task force audit which

was good.

4.

TS Comparison to Plant Configuration

a

~

TS Tables

The

inspector

compared

selected

TS tables

of instrumentation

and

components

to actual plant configuration.

The tables

selected

were:

3.2.F

Surveillance

Instrumentation

3.7.A

Primary Containment Isolation Valves

3. 11.A

Fire Detection Instrumentation

3. 11.B

Spray/Sprinkler

Systems

3. 11.C

Hose Stations

Information

contained

in the

tables

was verified,

on

a

sampling

basis,

to

be consistent

with actual

plant configuration.

Included

was verification of nomenclature,

location, function,

and in the case

of instrumentation,

the parameter

measured

and type of indication and

range.

A typographical

error

was

identified

in

Table

3.2.F,

Surveillance

Instrumentation.

Drywell

Temperature

Indicator

TI-64-52AB

was

listed

with

other

instrumentation

for

Drywell

Pressure.

The licensee

acknowledged

this error

and stated

that it

would be corrected

in a future

TS amendment.

No safety significance

is connected

with this error.

Also

in

Table

3.2.F,

The

wide

range

Gaseous

Effluent Radiation

Monitor and Recorder

was incorrectly identified as Instrument

Number

RR-90-322A.

The correct identification is

RM-90-306

and

RR-90-360,

respectively

for

the

monitor

and

recorder.

The

licensee

had

previously identified this

discrepancy

and

produced

a

copy of

an

12

intended

TS revision to,correct the error.

This is

new instrumenta-

tion and is still in the, process of being installed.

b.

TS Comparison to

FSAR

The- inspector verified that all references

to the

FSAR contained

in

TS Section 5.0, Major Design Features,

were consistent with the

FSAR.

No discrepancies

were identified.

C.

TS Controlled

Copy Review

The inspector

reviewed

two copies

of Unit 2

TS to ensure

that all

pages

were present

and

were of the appropriate

amendment.

The

two

copies

reviewed were

numbers

52 and

40 assigned

to the

NRC Resident

Inspector's office and the Unit 2 control

room, respectively.

Pages

1. 1/2. 1-2 through

1. 1/2. 1-4 of copy

52 were of the incorrect

amendment.

The

pages

present

were considered

"Original", having

an

effective

date

of 3-19-87.

According

to

the

TS Effective

Page

Listing,

these

pages

should

have

an

Effective

Revision

Date

of

3-3-88,

reflecting

Amendment

No.

143.

This indicates

that these

pages

were not -properly revised

upon

Issuance

of Amendment

No.

143.

Numerous, other

pages

also affected

by Amendment

143 were properly

revised.

The

presence

of

superseded

pages

in copy

52

represents

example

two of the violation 259,

260,, 296/89-47-01,

discussed

in

paragraph

2 above.

Two copies of pages

3.7/4.7-15

and

16 (front and back of one sheet)

were present

in

TS copy

40 located in the Unit 2 control

room.

One

of these

pages

(3.7/4.7-16)

contained

a

licensee

added

annotation

adjacent

to

paragraph

4.7.c. l.a,

a

surveillance

requi rement

for

secondary

containment.

The

annotation

referred

to

CM-88-64-2-007.

This

CM identifies

a

known

in-leakage

source

from temporary air

compressors

that accounts for

a portion of the allowable

in-leakage

of 12,000 cfm.

Since

two copies of page 3/7/4 '-16 were present,

the

CM would not have

been identified if the non-annotated

page

had

been

used.

SDSP

12. 11,

"Special

Requirements

and

Compensatory

Measures,"

requires

that

when

TS

are

annotated

with

SRs

on

CMs,

that

the

annotated

pages

replace

the

existing

pages.

This

precludes

duplicated

pages,

and thus eliminates

the possibility of missing

a

CM

or

SR.

The inspector verified that all other

pages

annotated

with

SRs or

CMs (two existed) in the control

room copy of Unit 2

TS were

not duplicated.

The inspector also verified that

no other

SRs or

CMs

existed ,that

should

be

annotated

in Unit

2

TS according

to the

requirements

in

SDSP

12. 11.

The presence

of two conflicting pages

in

the Unit 2 copy of TS represents

example three of Violation 259,

260,

296/89-47-01

discussed

in paragraph

2.

The inspector discussed

with

the licensee

the practice of annotating official copies

of

TS with

13

non-NRC

revi ewed

informati on,

whi ch presents

the

opportuni ty for

unauthorized

changes

to TS.

5.

System Design'asis

Comparison to TS Surveillance

Requirements

In order

to verify that

TS surveillance

requirements

accurately verify

system operability,

the inspector

compared

surveillance

requirement

flow

rates

for the

RHR system to the design basis flow rate requirements.

FSAR

Table 6.4-1 lists minimum

RHR pump flow of 10,800

gpm

and

20,000

gpm for

one

and

two

pump operation,

respectively,

at

0 psid

between

the reactor

and drywell for adequate

ECCS response.

TS surveillance

4.5.B. 1 .requires

that

each

LPCI

(RHR)

pump deliver 9000

gpm at

125 psig

and two pumps in

the

same

loop deliver

12,000

gpm at

250

psig.

The

licensee

provided

calculations that demonstrated

the surveillance

requi rement flow rates

are

conservative

in verifying

RHR operability with respect

to design

basis

flow rate requirements.

RHR

TS 3.5.B. 11

requires

that

the

RHR unit to unit

cross

connect

capability be operable

whenever irradiated fuel is in the reactor

and when

pressure

is

greater

than

atmospheric.

When

questioned

about

this

requirement

pertaining

to Unit

2 restart,

the licensee

stated

that the

Unit

1

RHR cross

connect would be utilized to meet the requirement.

It is

unclear what licensee

intentions are regarding Unit

1

RHR operability for

seismic,

environmental

qualification,

and fire protection

requirements.

Additionally,

the

NRC

has

questions

with

regard

to

satisfying

TS

surveillance

requirements

for Unit

1

RHR and control

room staffing for

Unit

1 with Unit

1

RHR required for Unit 2 operation.

These

concerns will

be tracked

as IFI 259,260,296/89-47-02,

Unit 1

RHR Cross-Tie Operability.

6.

- Exit Interview (30703)

The inspection

scope

and findings were

summarized

on

September

29,

1989

with

those

persons

indicated

in

paragraph

1 'above.

The

. inspectors

described

the

areas

inspected

and

discussed

in detail

the

inspection

findings listed below.

The licensee

did not identify as proprietary

any

of the material

provided

to or reviewed

by the inspectors

during this

inspection.

Dissenting

comments

were not received

from the licensee.

Item

259,

260, 296/89-47-01

Descri tion

VIO, Document Control of TS,

example

1 in

paragraph

2,

and

examples

2

and

3

in

paragraph

4.

259,

260,

296/89-47-02

IFI, Unit

1

RHR Cross-Tie Operability,

paragraph

5.

259,

260, 296/89-47-03

IFI, Failure of TS

Change

to

implement

SI

Task Force

Recommendation,

paragraph

3.a.

14

7.

Acr onyms

ADS

APRM

ARI

ATWS

BFNP

BWR

CAQR

CFM

CFR

CM

CREV

DG

FSAR

GL

GPM

HPCI

HPFPS

IFI

IR

IRM

LER

LCO

LPCI

MR/HR

NPP

NRC

NSRB

PORC

RCIC

RHR

RHRSW

RMS

RPS

RRB

RWM

SBGT

SDSP

SI

,SLC

SR

SRs

STS

TS

TVA

VIO

Automati c Depr essui izati on System

Average

Power

Range Monitor

Alternate

Rod Insertion

Anticipated Transient Without Scram

Browns Ferry Nuclear Plant

Boiling Water Reactor

Condition Adverse to Quality Report

Cubic Feet

Per Minute

Code of Federal

Regulations

Compensatory

Measure

Control

Room Emergency Ventilation

Diesel Generator

Final Safety Analysis

Repor t

Generic Letter

Gallon Per Minute

High Pressure

Coolant Injection

High Pressure

Fire Protection

System

Inspector

Followup Item

Inspection

Report

Intermediate

Range Monitor

Licensee

Event Report

Limiting Condition for Operation

Low Pressure

Coolant Injection

Millirems Per Hour

Nuclear Performance

Plan

Nuclear Regulatory

Commission

Nuclear Safety

Review Board

Plant Operations

Review Committee

Reactor

Core Isolation Cooling

Residual

Heat

Removal

Residual

Heat

Removal

Service Water

Radiation Monitoring System

Reactor Protection

System

Restart

Review Board

Rod Worth Minimizer

Standby

Gas Treatment

System

Site Directors Standard

Practice

Surveillance Instruction

Standby Liquid Control

System

Surveillance

Requirements

Special

Requirements

Standard

Technical Specification

. Technical Specification

Tennessee

Valley Authority

Violation