ML18030A822

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Insp Repts 50-259/85-45,50-260/85-45 & 50-296/85-45 on 850820-0930.Noncompliance Noted:Failure to Take Corrective Action for Diesel Generator False Start & to Maintain Record of Diesel Generator Surveillance Instruction
ML18030A822
Person / Time
Site: Browns Ferry  Tennessee Valley Authority icon.png
Issue date: 10/23/1985
From: Brooks C, Cantrell F, Patterson C, Paulk G
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18030A820 List:
References
50-259-85-45, 50-260-85-45, 50-296-85-45, NUDOCS 8511040331
Download: ML18030A822 (28)


See also: IR 05000259/1985045

Text

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W.

ATLANTA,GEORGIA 30323

Report Nos.:

50-259/85-45,

50-260/85-45,

and 50-296/85-45

Licensee:

Tennessee

Valley Authority

500A Chestnut Street

Tower II

Chattanooga,

Tennessee

37401

. Docket Nos.:

50-259, 50-260,

and 50-296

License Nos.:

DPR-33,

DPR-52,

and

DPR-68

Facility Name:

Browns Ferry Nuclear Plant

Inspection

Conducted:

August

20 - September

30,

1985

Inspectors:

au

,

en1

e

ent

n

atterson,

s

t

roo s,

es

nt

Approved by:

F.

. Cantre

, Section

se

,

Division of Reactor Project

r

>2 ~$

ate

1gne

z3 z~

a e

sgne

gag gW

ate

igne

zing)

ate Signed

SUMMARY

Scope:

This routine inspection

involved

240 resident

inspector-hours

in

the

areas

of operational

safety,

maintenance

observation,

reportable

occurrences,

previous

enforcement

matters,

surveillance

testing,

regulatory

performance

improvement

program,

and refueling activities.

Results:

FOUR VIOLATIONS-

10 CFR 50, Appendix B, Criterion

XVI for failure to take corrective

action fer a diesel

generator false start.

2.

10 CFR 50, Appendix B, Criterion

V for multiple examples:

a.

Failure to maintain Reactor Protection

System circuitry per plant

drawing.

b.

Failure

to maintain

record of

a diesel

generator

surveillance

instruction.

851i0403~i

8/025'DR

ADOCK OM

@DR

c.

Failure to use

a

PORC approved

maintenance

request.

d.

Failure

to

have

an

adequate

operating

instruction for'he

containment

purge-system

charcoal

heaters'.

3.

10 CFR 50, Appendix B, Criterion VI for failure to maintain drawings of

the vacuum breaking system.

4.

10 CFR 50,

Appendix

B, Criterion

XVI, for failure to

preclude

repetition of violation

on failure to perform

vendor

recommended

maintenance

items.

REPORT DETAILS

Licensee

Employees

Persons

Contacted:

J.

A. Coffey, Site Director

R. L. Lewis, Plant Manager (Acting)

J.

E. Swindell, Superintendent

- Operations/Engineering

T.

D. Cosby, Superintendent

- Maintenance

(Acting)

J.

H. Rinne, Modifications Manager

J.

D. Garison, guality Engineering Supervisor

D.

C. Mims, Engineering

Group Supervt'sor

R. McKeon, Operations

Group Supervisor

C.

G.

Wages,

Mechanical

Maintenance

Supervisor

J.

C. Crowell, Electrical Maintenance

Supervisor

(Acting)

R.

E. Burns, Instrument Maintenance Supervisor

A. W. Sorrell, Health Physics

Supervisor

R.

E. Jackson,

Chief Public Safety

T. L. Chinn, Senior Shift Manager

T. F. Ziegler, Site Services

Manager

J.

R. Clark, Chemical Unit Supervisor

B. C. Morris, Plant Compliance Supervisor

A. L. Burnette, Assistant Operations

Group Supervisor

R.

R. Smallwood, Assistant Operations

Group Supervisor

S.

R. Maehr, Planning/Scheduling

Supervisor

G.

R. Hall, Design Services

Manager

W. C. Thomison, Engineering Section Supervisor

C.

E. Burke,

Radwaste

Group Controller

Other

licensee

employees

contacted

included

licensed

reactor

operators,

auxiliary operators,

craftsmen,

technicians,

public safety officers, quality

assurance,

design

and engineering

personnel.

Exit Interview

(30703)

The

inspection

scope

and

findings

were

summarized

September

20,

and

October I, 1985 with the Plant Manager and/or Assistant Plant Managers

and

other members of his staff.

The licensee

acknowledged

the findings and took no exceptions.

The licensee

did not identify as proprietary any of the materials

provided to or reviewed

by the inspectors

during this inspection.

Licensee Action on Previous

Enforcement Matters

(92702)

(Closed)

Unresolved

Item (259/83-27-05).

The licensee

has

established

a

program to certify hydrometers.

The hydrometers

in the tool

room were

inspected

and

each

contained

a current certification sticker.

This item is

closed.

(Closed) Violation (259,260,296/83-19-01).

The Pressure

Suppression

Chamber

(PSC)

System

has

been returned to an operable status.

Operating Instruction

OI-74,

Residual

Heat

Removal,

has

been

revised

to provide

a

method of

alignment of the

keep fill system

using

the

PSC

system or the condensate

transfer

system.

This item is closed.

(Closed) Violation (259,260,296/83-33-06).

Instrument Tabulation

Drawings

47B607-64-7R

and 47B607-64-8R were reviewed

and found to have

been correctly

revised.

This item is closed.

(Closed)

Open

Item (259/83-33-07).

This item has

been

inspected

during

other routine

inspections

since

Report

83-33

and

Unit

3 drywell

leak

detection

equipment is discussed

in paragraph five.

This item is closed.

(Closed)

Open

Item (259/83-33-08).

The licensee

has

completed

detailed

annunciator

procedures

for the control

room panels 9-3 and 9-4.

This item

is closed.

(Closed)

Open Item (259/83-52-01)..

The licensee

has

done

a detailed'review

of the control

and filing of temporary alterations.

Discussions

with

personnel

involved in the review indicated

the process

was sufficient to

correct deficiencies identified in the past.

This item'is closed.

(Closed)

Open

Item (259/83-33-05).

Technical

Instruction

38 has

undergone

a major revision to upgrade

the procedure.

This item is closed.

(Closed)

Violation (259/83-60-02).

Plant procedures

have

been

revised

in

this

area

to require notification of the chemistry

section

upon unit

startup.

This item is closed.

(Closed)

Unresolved

(260/81-09-01).

The

Pressure

Suppression

Chamber

System

has

been returned to an operating status.

This item is closed.

(Closed)

Open

Item (260/82-06-02).

Procedure

revisions

have

been

made to

designate

high worth control

rods

on the rod pull sheet.

This item is

closed.

(Closed)

Violation (260/82-15-06).

The response

to this violation was

reviewed

and the inspector

has

no further questions.

This item is closed.

(Closed)

Violation (260/82-12-03).

Procedure

revisions

to Surveillance

Instruction 4.6.H. 1, Visual Examination of Hydraulic and Mechanical

Snubbers

were reviewed

and found adequate.

This item is closed.

(Closed)

Violation (260/82-19-03).

The licensee

response

and corrective

action were reviewed.

The inspector

has

no further questions

in this area.

This item is closed.

(Closed)

Violation (260/82-24-01).

The licensee's

corrective action in

this

area

was

reviewed

and

recent

inspections

have

found

no

equipment

problems in this area.

This item is closed.

4.

5.

(Closed)

Open Item (260,296/82-34-04).

This item was previously closed for

Unit

1 and closed

now for the other units.

(Closed)

Violation (260/83-33-06).

The inspector

reviewed

the licensee

response

to this violation and the present

method of adjusting the

R factor.

This item is closed.

(Closed)

Violation (260/83-43-02).

The response

and corrective

steps

to

this violation were

reviewed

and the inspector

has

no further questions.

This item is closed.

(Remain

Open)

Open Item (259,260,296/81-35-05)

Licensee

Event Report 85-04

discusses

the

problems

with the

low pressure

coolant injection

(LPCI)

motor-generator

(MG) sets

and

the repair

program in process.

All Unit 2

LPCI

MG sets

have

been returned to the vendor for permanent repair.

Units

1

and

3 will be repaired after the return of Unit 2.

The

MG sets

continue to

be plagued with problems.

(Closed)

Violation (296/82-34-03).

Mechanical

Maintenance

Instruction

MMI-28 was

reviewed for post-maintenance

test requirements.

This item is

closed.

(Closed)

Violation (259/260/296/84-23=02).

Further tracking in this area-

concerning

diesel

generator will be under the deviation addressed

in this

report.

Unresolved

Items* (92701)

In paragraph

five there is

an unresolved

item about the

vacuum

breaking

system,

in paragraph

six there is

an unresolved

item concerning

fuses,

and

in paragraph

ten there is

an unresolved

item concerning reactor protection

system

panel discrepancies.

Operational

Safety

(71707,

71710)

The

inspectors

were kept informed

on

a daily basis

of the overall plant

status

and

any significant safety matters

related

to plant operations.

Daily discussions

were held

each

morning with plant management

and various

members of the plant operating staff.

The inspectors

made frequent visits to the'ontrol

rooms

such that each

was

visited at least daily when

an inspector

was

on site. Observations

included

instrument readings,

setpoints

and recordings;

status of operating

systems;

status

and

alignments

of emergency

standby

systems;

onsite

and offsite

emergency

power

sources

available for automatic

operation;

purpose

of

temporary tags

on equipment controls

and switches;

annunciator

alarm

t

n unreso

ve

tern

ss

a matter

a out w ich more information is required to

determine whether it is acceptable

or may involve a violation or deviation.

status;

adherence

to

procedures;

adherence

to limiting conditions for

operations;

nuclear

instruments

operable;

temporary alterations

in effect;

daily journals

and logs;

stack monitor recorder

traces;

and control

room

manning.

This

inspection

activity also

included

numerous

informal

discussions

with operators

and their supervisors.

General

plant tours

were conducted

on at least

a weekly basis.

Portions of

the turbine building, each reactor building and outside

areas

were visited.

Observations

included valve positions

and

system

alignment;

snubber

and

hanger

conditions;

containment

isolation alignments;

instrument

readings;

housekeeping;

proper

power supply

and

breaker

alignments;

radiation

area

controls;

tag controls

on equipment;

work activities in progress;

radiation

protection

controls

adequate;

vitaR

area controls;

personnel

search

and

escort;

and vehicle search

and escort.

Informal discussions

were held with

selected

plant

personnel

in their functional

areas

during these

tours.

Weekly verifications of system status

which included major flow path valve

alignment,

instrument

alignment,

and

switch

position

alignments

were

performed

on the primary containment

purge

system

and the circulating water

vacuum breaking

system.

A complete

walkdown of the accessible

portions of the primary containment

purge

system

and circulating water

vacuum breaking

system

was conducted

to

verify system operability.

Typical of- the items checked during the walkdown-

were: lineup procedures

match plant drawings

and the as-built configuration,

hangars

and

supports

operable,

housekeeping

adequate,

electrical

panel

interior conditions, calibration

dates

appropriate,

system

instrumentation

on-l.ine, valve position alignment correct,

valves locked

as appropriate

and

system indicators functioning properly.

a ~

Drywell Leak Detection

System

During

a routine tour of the unit three control

room on September

4,

1985, the inspector questioned

why both the drywell equipment

and floor

drain

sump level

abnormal

annunciators

were illuminated.

The system is

setup with high-high, high, low, and

low-low trip points.

The

sump

pumps cycle

between

the high

and

low points,

and the annunciator

is

actuated

by the high-high or low-low.

If the

system is operating

normal,

the annunciator

should not

be received

unless

a

problem

has

occurred with the

sump level.

The operator stated

the

sump levels were low which had been verified by

local

level transmitters.

Proper

operation

of the

sump

pumps

and

annunciators

was

understood.

One possible, explanation

for why the

drywell equipment drain

sump level abnormal

annunciator

had alarmed

was

that the

sump

pump had been manually cycled to try to stop

a continuous

upward drift of the

flow integrator.

Three

maintenance

request

stickers

were attached

to the integrator.

Although the integrator

was

providing

a meaningless

reading,

log readings

were still being taken

and

an average

value of greater

than

10 gallons per minute leakage

had

been

logged for several

days.

No leakage

was

suspected

for the plant

condition of cold shutdown.

The operator stated

the log readings

were

still being taken in hopes that

some action would be taken to correct

the equipment

problems.

The plant superintendent

for operations

was

informed of the inspector

concerns

in this area.

Primary Containment

Purge

System

During

a

walkdown of the

primary

containment

purge

system

on

September

12, 1985, the following deficiencies

were noted:

(1)

The charcoal

bed

heaters

on

each unit were

turned off for no

apparent

reason.

(2)

The high efficiency particulate filters were apparently installed

in the wrong units.

Each filter has

a manufacturer identification

label

which includes

the unit designation.

The unit designated

for unit one

was

found in unit three, unit two in unit one,

and

unit three in unit two.

(3)

The cover for unit two charcoal

bed temperature

sensor

(TI-64-125)

was missing.

(4)

The foundation bolts for unit two were found not secured.

These

concerns

were discussed

with plant

management

in

a meeting

on

September

12,

1985.

A review of the training departments

lesson

plan

(Lesson

Plan

16,

Primary

and

Seconda+

Containment

Systems)

found

little information concerning

the system.

The plan merely stated

the

system's

purpose

and

referenced

the plant operating

instructions.

Further review found that the charcoal

heaters

were not addressed

in

any plant operating instruction.

The charcoal

bed heaters

remove

any

accumulation of moisture to prevent degradation

of the system's

iodide

removal capability.

The iodide removal. efficiency for the charcoal

bed

is addressed

in Technical Specification 3.7.F.2.6.

Failure to have

a

procedure for operation of the containment

purge

system

charcoal

bed

heaters

is

a violation of 10 CFR 50 Appendix B, Criterion 5. (259, 260,

296/85-45-01).

This violation is similar to

a violation in last

month's report concerning

the standby

gas treatment

system charcoal

bed

heaters

(85-39).

The violation was

discussed

in an exit meeting

on

September

20, 1985, with plant management.

Vacuum Breaking System

The inspectors

performed

a walkdown

on the accessible

portions of the

Vacuum Breaking

System

(VBS) associated

with the Condenser Circulating

Mater System.

The

VBS is described

in Section 11.6.4 of the

FSAR as

a

redundant,

seismic

Class

I engineered

safeguard.

The

VBS pipe building

is located

outside

the protected

area.

The building is below grade

with an earth backfill over the top of the building.

Access is through

an unsecured

manhole.

The material condition was found to be generally

poor with an excessive

amount of dirt and cobwebs.

Rags,

old pressure

gauges

and various

other

loose

equipment

were laying about.

Three

check valves

(1-27-886,

2-27-886,

and 3-27-886)

were found removed

from

the

system

and

blank flanges

were installed in their place.

These

valves

were

removed

as part of

ECN L2002 performed in July 1978.

As

constructed

plant drawings

(47W831-3

Rev.

A) had not been

updated to

show the

removal

of the valves.

This work was closed

out without

proper verification of drawing revision.

This is

a violation of

10 CFR 50,

Appendix

B, Criterion VI.

(259,260,296/85-45-02).

The

following additional

concerns

were identified and will be tracked

as

an

unresolved

item

pending

evaluation

by

the

licensee.

(259,260,

296/85-45-03):

(1)

Critical System

and

Components List (CSSC).

(2)

Installed

instrumentation

is

not

on

a

program for periodic

functional

and calibration testing.

(3)

The operator

training

plan

does

not identify the

VBS

as

an

engineered

safeguard

and treats

the

basis for the

system

in

a

superficial

manner.

(4)

Radiological

Emergency

Procedures

(REP)

Implementing

Procedure,

IP-24,

Earthquake

Emergency

Procedure

identifies the location of

Breaker

1427

(power supply for the vacuum breaker valves)

as being

panel

14 of Battery Board 2.

Breaker

1427 is actually located

on

the Plant Non-Preferred

AC Panel

Board.

(5)

Although OI-27C, Condenser

Circulating Water System,

refers to the

Radiological

Emergency

Plan Implementing Procedures

for actions in

the event of

a breach of Wheeler

Dam,

no Implementing

Procedure

exists for'this situation.

6.

Maintenance

Observation

(62703)

Plant

maintenance

activities

of selected

safety-related

systems

and

components

were observed/reviewed

to ascertain

that they were conducted

in

accordance

with requirements.

The following items were considered

during

this review:

the limiting conditions for operations

were met; activities

were

accomplished

using

approved

procedures;

functional

testing

and/or

calibrations

were

performed prior to returning

components

or system

to

service;

quality

control

records

were

maintained;

activities

were

accomplished

by qualified personnel;

parts

and materials

used

were properly

certified; proper

tagout

clearance

procedures

were

adhered

to; Technical

Specification

adherence;

and radiological

controls

were

implemented

as

required.

Maintenance

requests

were reviewed to determine

status

of outstanding

jobs

and

to

assure

that priority was

assigned

to safety-related

equipment

maintenance

which might affect plant safety.

The inspectors

observed

the

below listed maintenance activities during this report period:

a.

MMI-29, RHRSW

Pump Maintenance

b.

Vacuum breaking

system

and off-gas building inspections

c.

Refuel floor activities

d.

LPCI

MG Set Maintenance

Requests

e.

Fuse

Problems

During

a review of recent

maintenance

requests

related to the

LPCI

MG sets,

numerous

requests

were written concerning

incorrect

fuse installations.

Further

inspections

in this

area

revealed

that

a

program for fuse

identification resulting

from

a previous violation (260/83-27-08),

where

several

control circuit

fuses

were

found incorrectly installed,

had

identified significant problems

in this area.

The inspector

thought that

all the fuse problems

had

been corrected

and the fuse identification program

was

a program consisting of operator training and labeling. of fuse holders.

Upon learning of the

magnitude

of the

problem the inspector told plant

management

on September

17,

1985 these

problems

needed

to be evaluated for

reportability.

Although all three units have not been operating since March

1985,

some of these

problems

were identified by the licensee while the units

were operating.

The following Table lists the

number of problems

found

during the labeling program:

Common

S stem

Unit

I

Unit

Ij

Unit

rrr

Fuse

Sets

Labeled

1340

No Fuse 'Block Found

12

Breaker Installed - No Fuse Block

0

Panel

Not Installed

9

Fuse Block Size - Incorrect

21

1970

5

2

6

5

2922

3411

13

33

6

2

12

4

8

6

Total

Number

Fuse

Sets

Percent

Complete

Requires

Maintenance

Request

Written

1382

44

688

1988

65

372

2961

3456

99

100

757

237

Requires

Design

Change

Request

Correction

42

25

38

154

Fifty percent

of the

maintenance

requests

written were

estimated

for

enhancement

items

and were not actual

problems.

The problems

were varied

and in all types of systems.

This area will remain unresolved for further

evaluation

(259,260,296/85-45-04).

a ~

Failure of a Diesel

Generator to Start

On August 27,

1985,

the licensee

made

a 4-hour report regarding

the

failure of the Units

1 and

2 (shared)

B Diesel

Generator

(hereinafter

referred to as the

1

B D/G) to start when required.

The residents

were

kept informed in

a general

way

on the status

of the troubleshooting

efforts

on

a daily basis.

Following return of the

1

B

D/G to an

operable

status,

the inspector weviewed the documentation

to determine

the initial failure indications,

root cause,

corrective action,

and

post-maintenance

testing.

The documentation

was inadequate

to support

the root cause

determination,

troubleshooting efforts,

and corrective

action

taken.

Interviews with operations

and maintenance

personnel

were initiated

to

supplement

the

documentation.

The following

Chronology

describes

the maintenance

efforts

from various

logs'nd'nterviews:

Aug. 27,

1985

1430

Commenced

SI 4.9.A.1.a,

Diesel

Generator

Monthly"Test,

on

1

B Diesel

Generator.

It is=

  • not

known if this was

a routine surveillance

or done,

due to

a problem noted during per-

formance

of

SI 4.9.A.3.a,

Common

Accident

Signal Logic Test (fuel pressure

problems).

1545

Licensee

Reportable

Event Determination

(LRED)

gives this

as

the

Event

Time

and Discovery

Time.

1

B D/G failed to start

when given

an

auto start signal during the performance of Sl

4.9.A.l.a.

NOTE:,

A copy of this SI 4.9.A.l.a cannot

be located;

no more details

on the failure of

1

B D/G are

known.

1600

1930

2030

1

B

D/G declared

inoperable

in

operators'ogs.

4-hour

ENS call-in made at 1744.

Running

1

B D/G, fuel filters appear

to need

changing - MR'd.

After running

1

B D/G which started

OK on slow

start, fuel oil system

8

1 pressure

was 0 when

diesel

was at idle speed; will try to change

filters.

Aug. 28,

1985

0105

SI 4.9.A.l.a in progress

on

1

B D/G.

0140

Stopped

1

B D/6 due to leak in fuel filter.

0145

SI 4.9.A.l.a

in progress

on

1

B

D/G blew

gasket

on fuel oil strainer.

DG shutdown.

NOTE:

A copy of this

SI 4.9.A. l.a cannot

be located;

interviews

indicated that the fuel filters were

changed

(although

no

MR has

been

located)

and that an "0" ring on the fuel filter cap retaining bolt was

either not reinstalled

or pinched

during assembly

since this

was the

source of the fuel leak.

0500

1

B D/G still inoperable,

will not idle at

450

RPM,

appears

not to

be getting

enough

fuel.

Starts to shutdown.

0820

1140

Started

SI 4.9.A.l.a on

1

B D/G.

SI 4.9.A. l.a

on

1

B D/G complete but D/G will

not start

on ¹

1 air start motor.

NOTE:

The

SI cover

sheet

indicates

that

the

reason

this

SI

was

performed

was that it was required

by the routine schedule

(a monthly

surveillance)

and

that

the

SI

acceptance

criteria

was satisfied.

Remarks

section

indicates

that the

D/G did not start

on the ¹

1 air

start motor and that

MR A 571512

was written to investigate.

An entry

was

made

on September

3,

1985 in the

remarks

section that

MR A 588874

was generated for additional work.

MR A 571512 - Work instructions

were to change

governor oil, replace

fuel filter retaining

nut gasket

and

inspect

the

engine air box.

Sample of old governor oil to be submitted to chemistry laboratory

(This

MR written

on August 28,

1985

and

completed

on September

29,

1985).

MR A 588874 - Work instructions

were to remove starting air motors to

be cleaned.

Replace after cleaning.

(This

MR written on August 29,

1985 and completed

on August 29, 1985).

NOTE:

Neither

MR satisfactorily documents

what conditions

were found

but interviews indicate that

no abnormal

conditions

were found and

no

cause for the previous

problems

could be determined.

Aug. 29,

1985

0735

Approved

MR to work

1

B D/G to change

out

governor oil.

1200

1458

Started

SI 4.9.A. l.a on

1

B D/G.

Completed

SI 4.9.A. l.a on

1

B D/G.

10

1500

1

8 D/G declared

operable.

This

breakdown

in corrective

action is

a violation of

10 CFR 50,

Appendix 8, Criterion XVI which requires strict control, documentation

and

reporting

of significant

conditions

adverse

to

quality

(259,260,296/85-45-05).

Browns

Ferry

Standard

Practice

1.3,

Definitions, describes

a significant condition adverse

to guality as

(in part)

any condition which is reportable

to the

NRC within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />

or within 30 days.

This condition

was

reported

as required

by the

4-hour reporting requirement of 10 CFR 50.72

on August 27,

1985.

The lost Surveillance Instruction test

data for SI 4.9.A. l.a which was

performed at

1430

on August 27; 1985

and again at 0105

on August 28,

1985 is

a violation for failure to adhere

to Standard

Practice

17.9,

Surveillance

Requirement

Program (259,260,296/85-45-01).

This Standard

Practice

requires

surveillance

instruction test data to be maintained

as

a quality assurance

record with a lifetime retention period.

RHRSW Relay Wiring

While observing

the

RHRSW

Suction pit cleaning

in progress

on

September

5,

1985,

the inspector

noted

the clearance

tag for the

B2

RHRSW

pump local control switch

was not attached

to the control switch"-

but was laying on

a workbench nearby.

Plant operations

personnel

were

informed of this discrepancy.

On September.10,

1985,

the inspector

once again toured the

RHRSW building and discovered that clearance

tags

for both

the

Cl and

C3

RHRSW

pump local control

switches

were not

attached

but were

found

on the

ground- in the vicinity of the

pump

motors.

The plant

manager

was

informed of the continuing lack of

control of clearance

tags

on control switches.

This deficiency will be

tracked

as

an inspector follow-up item for control of clearance

tags

on

local control switches

(259,260,296/85-45-06).

,1

Diesel

Generator

Maintenance

The licensee identified as part of their system operational

readiness

review that procedures

had not

been

prepared

for the standby

diesel

generators

scheduled

maintenance

as

recommended

by the manufacturer for

the six and twelve year intervals.

Procedures

were in place for the

annual

arRf three year inspections.

Technical Specification 4.9.A. l.d

requires

that

each

diesel, generator

be given

an annual

inspection in

accordance

with instructions

based

on the manufacturer's

recommen-

dations.

The manufacturer's

recommendations

of scheduled

maintenance

is given in Electro-Motive Division Maintenance

Instruction

(M.I. 1742)

for 999 system generating

plants.

The li'censee

performs Surveillance

Instruction'SI)

4.9.A. l.d

which

is

implemented

by

Mechanical

Maintenance

Instruction

MMI-6 and Electrical

Maintenance

Instruction

EMI-3 to comply with technical specifications.

11

The inspector

asked

to review. the licensee

event report

(LER) for this

discovery which occurred

on August 14, 1985,

on September

19,

1985, but

was told the

LER was still in draft form.

The

LER was being generated

for "informational purposes

only" and the 30 day reporting requirement

was not applicable.

This was questioned

as

a previous violation had

been

issued

concerning

diesel

maintenance

(259,260,296/84-23-02)

and

the inspections

were required

by technical specifications.

A review of the

licensee's

response

to

the

previous

violation

(84-23-02)

found that the licensee

stated that MMI-6 would be revised

to

include

the

maintenance

recommendations

made

in Electro-Motive

Division's

M.I. 1742,

Revision

E.

Full compliance

was to be achieved

October

5,

1984

when

MMI-6 was- revised to include the manufacturer's

recommendations.

A review of MMI-6 found that the

procedure

was

revised

not

on October 5,

but

on October 23,

1984,

to include the

recommendations.

The procedure

only included revisions

to the annual

and three year requirements.

Once the procedure

was

implemented

the

three year inspection

was not performed

and

has not been

performed for

any unit as of the date of this inspection.

The inspector

reviewed the package for preparation of the

LER and found

the following statement:

"Sequoyah

and Watts

Bar do not follow EMD's recommendations

word

for word,

but

have

used their judgement

to either eliminate,

reschedule

or modify EMD's program."

Not following the manufacturer's

recommendations

may be

a potentially

generic

problem at all

TVA sites.

According to the evaluation in the

LER package

by the cognizant

engineer

there

was

no justification for

deviation

from the

maintenance

schedule

for

some

items

based

on

conversations

with the vendor.

Listed as

most important

was the six

year replacement

of cylinder head

grommets, inlet and outlet seals

and

lower line seals.

The diesel

cooling water is maintained

heated for an

automatic start

and water continually flows by 'the seals

by natural

circulation.

A failure of the seals

could result in cooling water

entering

the piston cylinder area or the lubricating oil resulting in

failure of the engine.

Sufficient replacement

parts

were not available

to work even

one diesel.

Starting in 1972 for the units

one

and

two

diesels,

<he six year

items

are

over

seven

years

past

due

and since

1976

the

items

are

three

years

past

due

on unit three.

Other

maintenance

requirements

were additionally not completed

and are being

evaluated

by the licensee.

Additionally, some items

on the scheduled

maintenance

would normally be

performed

by the electrical

maintenance

section but a review found none

of the six year

items

were

being

performed.

Also, the electrical

section did not have the current revision of the vendor's

recommended

maintenance.

They

had

M.I.

1742 (original issue)

dated

August

1970.

12

This was part of the root cause for the previous violation 84-23-02

and

resulted

in the licensee

establishing

a vendor

manual

control

system.

A review of the vendor

manual

control

system

found that the diesel

manual

was not controlled

as yet but was

on

a priority list for later

control.

The

manual

assembled

to be established

as the control

copy

contained

not only M.I.

1742 dated

August

1970,

but also

M.I.'742,

revision

D dated April 1975.

The Mechanical

Maintenance

section

was

the only one which possessed

revision

E dated

June

1976.

Although the

vendor

manual

was not controlled

as yet, it is reasonable

to expect

that all sections

would be using revision

E since this was mentioned in

the licensee's

response

to violation 84-23-02 nearly

a year

ago.

The

root

cause

and corrective

action

to violation 84-23-02

were only

superficially

corrected.

This

is

in violation of

10 CFR 50,

Appendix 8, Criterion

XVI which requires

that

measures

shall

be

established

to assure

that conditions

adverse

to quality

such

as

failures,

malfunctions

and deficiencies

are

promptly identified

and

corrected.

In the .case of significant conditions

adverse

to quality,

the measures

shall

assure

that the cause of the condition is determined

and corrective

action

taken

to preclude repetition.

The licensee

failed

to

take

corrective

action

to

preclude

repetition

of

a

significant condition

adverse

to quality.

This is identified

as

Violation Item (259,260,296/85-45-08).

Also,

a review of the Final Safety Analysis Report

(FSAR) section 8.5,

Standby

A-C Power

Supply

and Distribution, found that section 8.5.5,

Inspection

and Testing,

addressed

the maintenance

on the diesels.

FSAR

page 8.5-19 states

that scheduled

maintenance

on the diesel

generators

is conducted

in accordance

with the manufacturer's

recommendations.

The licensee

reported

on September

24,

1985 that all the diesels

were

technically inoperable

since

the vendor required

inspections

for the

three,

six,

and

twelve year intervals

had not

been

performed.

The

diesels

would, however,

be maintained

in a standby

readiness

condition.

Simultaneously,

the diesels

were reported

inoperable

because

the diesel

battery

racks

were determined

to

be not seismically qualified.

This

was the subject of a previous violation (259,260,296/85-28-05)

in April

1985.

During correction of the April problem four studs

broke which

were welded to an

embedded

metal plate in the concrete

foundation.

The

battery

racks

are

secured

to the floor using

the studs.

The stud

material

was given

a metallurgical

evaluation

and found not acceptable

for welding.

The steel

contained

too high

a carbon content

and

upon

welding would

become brittle.

The studs

have

been installed for a

number of years

and the source of the error was

unknown.

The licensee

plans to systematically

repair

the diesel

battery rack

as quickly as

possible.

The inspector questioned

the timing of the information.

The

plant manager

reviewed the

sequence

of events with the inspector.

It

was stated

the first time the evaluation information was discussed

with

the plant

was

on September

20,

1985.

However, this

was

done

on the

13

telephone

and the information not understood fully.

The metallurgical

evaluation

was transmitted to the plant on September

24,

1985.

This is

the

second

example of violation 259,260,296/85-45-08

above,

in that

this condition was not promptly identified and corrected.

As

a result of the diesel

generators

being inoperable the licensee

was

unable

to meet three technical

specification

requirements.

These

are

summarized

as follows:

(1)

T.S.

3.9.C.1

requires

that

whenever

the

reactor

is in cold

shutdown with irradiated fuel in the reactor,

at least

two diesel

generators

shall

be operable.

This was not met for Units

1 and 3.

(2)

T.S.

3.5.A.4 requires

operable

core

spray

pumps

and associated

diesel

generators.

This

was

not

met for Unit three

with

irradiated fuel in the vessel

and the vessel

head installed.

(3)

T.S.

3.5.8.9

requires

operable

residual

heat

removal

pumps

and

associated

diesel

generators.

This

was not met for Unit three

with irradiated fuel in the vessel

and the vessel

head installed.

The licensee

initiated

a safety evaluation

to analyze

the unanalyzed

condition of the plant.

As a compensatory

measure

primary containmen't

was reestablished

on Unit three.

Additionally, all fuel

movement

was

suspended

due to timing problems

with some ventilation dampers.

FSAR section 5.3.4.2

discusses

a time

requirement of 2 seconds for the dampers.

The licensee

discovered that

some solenoid operated ventilation dampers

had not been given

a post maintenance

timing test after installation of

new solenoids for environmental

qualification purposes.

The timing in

question related to a fuel handling accident.

7.

Surveillance Testing Observation

(61726)

The

inspectors

observed

and/or

reviewed

the

below listed surveillance

procedures.

The inspection

consisted

of

a review of the

procedures

for

technical

adequacy,

conformance

to technical

specifications,

verification

of test

instrament

calibration,

observation

on the conduct of the test,

removal

from service

and return to service of the system,

a review of test

data,

limiting condition for operation

met,

testing

accomplished

by

qualified personnel,

and that the surveillance

was completed at the required

frequency.

a.

S. I. 4.9.A.3.A,

Common Accident Signal

Logic Test.

b.

S.I. 4.9.A.1.D, Diesel

Generator

Annual Inspection.

14

,

8

On August 28,

1985, while performing SI 4.9.A.3.A,

Common Accident Signal

Logic Test

on Unit 3, the licensee

discovered

that the Bl

RHRSW pump

was

inoperable

for

EECW service

since it failed to start

upon

an automatic

starting signal.

Subsequent

troubleshooting

by the licensee

discovered

a

wiring error associated

with time delay relay

TD2C in the Bl pump starting

circuitry.

This condition 'is believed to have

been in existence

since the

last surveillance test

was

performed

on the

RHRSW timers

on April 26,

1985.

A review of documentation

associated

with this event

indicated

that

a

similar time delay relay had failed in April 1985

on Unit 1 and was replaced

on April 26,

1985.

Maintenance

Request

(MR) A-170596 was written to verify

proper operation of the relay following the replacement.

This

MR contains

detailed step-by-step

work instructions with a temporary jumper installation

and independent verification sign-off steps.

Normally, MRs should refer to

PORC

reviewed

instructions

to assure

procedural

controls

are maintained.

Standard

Practice 7.6, Maintenance

Request

and Tracking, requires that

CSSC

MRs that

have

no

PORC reviewed instruction

and are

beyond the skill of the

craft shall

be sent to

PORC for review and to the plant superintendent

for

approval.

MR A-170596 was not reviewed

and approved

as required.

This is

a

violation for failure to adhere

to written instructions.

(259,260,296/85-45-01).

Reportable

Occurrences

(90712,

92700)

The below listed licensee

events

reports

(LERs) were reviewed to determine

if the

information

provided

met

NRC requirements.

The

determination

included:

adequacy

of event description, verification of compliance with

technical

specifications

and regulatory

requirements,

corrective

action

taken,

existence

of potential

generic

problems,

reporting

requirements

satisfied,

and

the relative safety significance of each

event.

Additional

in-plant reviews

and discussion

with plant personnel,

as appropriate,

were

conducted

for those reports indicated

by an asterisk.

The following licensee

event reports

are closed:

LER No.

  • 260/85-05
  • 260/85-06

Date

June

11,

1985

June

20,

1985

Event

Reactor Water Cleanup Isolation.

Secondary

Containment Isolation

Initiated from Refuel

Zone Radiation

Detector

  • 260/85-09
  • 260/85-08
  • 259/85-10

July 12,

1985

July ll, 1985

April 03,

1985

Containment Isolation

Because of

Improper Transfer

Reactor Water Cleanup Isolation

Because of Improper Transfer

Discontinuance of CAM Hourly

Sampling

Due to Personnel

Error.

Regulatory

Performance

Improvement

Program

(RPIP)

The responsible

section chief reviewed the status of RPIP and actions

taken

by TVA to implement specific items

as required

by

NRC Confirmatory Order

EA

84-34

dated

July

13,

1984.

TVA has

assigned

a senior

manager

as

RPIP

Coordinator at the site.

His responsibilities

include verifying that each

task

has

been

implemented

as described,

has

met objectives,

and that the

necessary

programs

are in place to insure that objectives will continue to

be met.

Host of the short term items

have

been indicated

as complete,

but

have

not

been

signed off as

completed

by the

RPIP Coordinator.

The

inspectors

,reviewed

implementation

of Short

Term Action

Item 4.11,

Establishment

of the Independent

Safety Engineering

Group

( ISEG)

and found

that contrary to the indicated status

on the RPIP, the

ISEG did not exist.

Follow-up discussions

with licensee

representative

led to a concern that the

proposed

ISEG functions

and responsibilities

did not satisfy the discussion

in NUREG-0737 regarding

ISEG.

Although the plant is not committed to this

THI action item, it was

expected

that the guidance

contained

in NUREG-0737

would be followed in the implementation of this

RPIP action item.

This item

will continue to be tracked

under the

RPIP program.

Long

Term

Item 9.7, Utilize outside

contractor

to evaluate

Technical

Specifications

was

reviewed.

The contractor's

report dated

September

27,

1984

was

reviewed

and

actions

initiated

by the

licensee

to resolve

identified technical

specification discrepancies

were followed up to verify

initiation of necessary

corrective action.

Refueling Activities (60710)

The inspector

observed activities associated

with fuel off-loading on Unit I

and

verified

that

technical

specification

requirements

related

to

containment

integrity,

neutron

monitoring instrumentation,

control

rods,

refueling interlocks,

and staffing were being satisfied.

An inspection of the Reactor

Protection

System Trip Panels

(panels 9-15 and

9-17)

was

performed to verify removal of SRH Shorting links per GOI-100-3,

Refueling Operations,

Step

B. l.p.

The inspector verified that the. links

were

removed

as required;

however,

several

apparent

discrepancies

regarding

the internal wiring of the

panels

prompted

a detailed

inspection.

The

as-constructed

drawing for panel 9-17

was obtained

(Drawing 791E247-2A)

and

the following problems

were identified on the Unit I panels:

a ~

The metallic jumper link connecting

terminals

79

and

80 of terminal

board

CC on panel 9-17

was not secured with terminal

screws.

The link

was merely resting

on the terminals

and the integrity of the electrical

connection

could

not

be

determined.

Plant

personnel

immediately

installed

appropriate

screws

when

informed.

This link was

in the

control rod timing test circuitry and was believed to have

no effect on

the

Reactor

Protection

System

(RPS)

should it have fallen off the

terminals.

16

b.

The insulation

on several

wires adjacent

to fuses '22, 23,

and

24

on

terminal

board

BB of panel 9-17 was discolored

from a previous overload

condition.

c.

On panels 9-15

and

9-17

diodes

CR2B

and

CR2O

were

observed

to

be

supported

only by the attached

wires

and were dangling, loose,

from the

plastic wire ways from which the wires emerged.

d.

The main

power supply wire from terminal

2 of the

RPS

NG set breaker

(CBIB) to terminal

1 of the hot bus

(CR) which supplies

power to all of

the

panel 9-17

components

shows

evidence

of an overloaded

condition.

The jacket is cracked,

discolored

and

sections

of the jacket

are

missing.

The cable insulation is also cracked in several

locations.

e.

The fire proof metallic enclosures

which house

fuses

F12,

F13, F16,

and

F17 in panel 9-17

had lost their fire proof integrity.

The hinged

enclosure

cover

plate

was

not

secured

to the

enclosure

with the

required

wing nuts

and

as

a result

a one-half inch opening to.the

enclosure

was observed.

e

f.

The one-half inch flex conduit from the fire proof metallic enclosures

housing fuses

F12,

F13,

F16,

and

F17 in panel 9-17 terminated

about

one

inch from the enclosure

and the w'ires emerged into an adjacent wire was

for a distance

up to 3 feet before the wires exited the bundle

and were

terminated

on terminal

block

CC.

Orawing

791E247-2A requires

the

conduit carrying these

wires to be'terminated

as close

as possible to

the terminal block.

g.

The wires

shown

on Orawing 791E247-2A from terminal

3 of fuse

F13 to

terminal

3 of fuse

F27 and from terminal

3 of fuse

F17 to terminal

3 of

fuse

F25 were not installed in panel 9-17.

Items a,

e, f and

g are

examples

of a violation for failure to have

equipment installed

per approved

plant drawings.

(259,

260, 296/85-

45-01).

Items b, c,

and

d will be further evaluated

by the licensee

and left as

an unresolved

item until evaluation

completion.

(259,

260, 296/85-45-07).

~

~