05000260/LER-1980-029-03, /03L-0:on 800722,while Performing Surveillance Insp 4.1.A-7,reactor Low Level Switch LIS-3-203C Did Not Operate within Tech Spec Limits.Caused by Instrument Drift. Switch Inspected & Recalibr

From kanterella
(Redirected from ML18025B046)
Jump to navigation Jump to search
/03L-0:on 800722,while Performing Surveillance Insp 4.1.A-7,reactor Low Level Switch LIS-3-203C Did Not Operate within Tech Spec Limits.Caused by Instrument Drift. Switch Inspected & Recalibr
ML18025B046
Person / Time
Site: Browns Ferry Tennessee Valley Authority icon.png
Issue date: 08/20/1980
From:
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML18025B045 List:
References
LER-80-029-03L-01, LER-80-29-3L-1, NUDOCS 8008260537
Download: ML18025B046 (3)


LER-1980-029, /03L-0:on 800722,while Performing Surveillance Insp 4.1.A-7,reactor Low Level Switch LIS-3-203C Did Not Operate within Tech Spec Limits.Caused by Instrument Drift. Switch Inspected & Recalibr
Event date:
Report date:
2601980029R03 - NRC Website

text

U. 5, LEAR REOULAYlttrlsY CVIY)lbll~luw

{PLEASE PRINT OR TYPE ALLREQUIRED INFORMATION) 0 '~I 75 26 LICENSE TYPE 30 57 CAT 58 LICENSE NIIMBEA M 3(36 I

ENSEE EVeNY REPt2--

9 coNTRQL BLQGK:~~01 I

6

~0!j A

L B

R F

2 Q2 0

0 8

9 LICENSEE CODE 14 15 CON'T

~0i soURCE ~LQ6 0

5 0

0 0

2 7

s 0

8 2

0 8

OJQB 7

8 60 BI DOCKET NUMBER 69 EVENT DATE 74 75 AEPOAT DATE FVENT DESCRIPTION ANO PROBABLE CONSEQUENCES QIO L007j ~Durin normal o eration while erformin SI 4.1.A-7 reactor low water level switch ELIS-3-203C did not operate within T.S. Table 3.1.A limits.

There was no effect on the public health or safety.

Redundant switches in the same trip channel and

~0! 9 f OOBJ

~a redundant trip channel were operable.

Previous events:

260-804, 259-7824,

~259-741 and 259/7333.

. CZ3 GZQ I

7 8

4,)

SYSTEM

CAUSE

CAUSE COMP VALVE CODE CODE SUBCODE

'ahIPUNENT CODE SUHCOOE SUBCODE KH

~zA 0>>

~xO>>

~zOls z

s s r R

o 04

~sOls

~z Ols 7

II 9

10 11 12 13 18 19 20 SEOUENTIAL OCCURRENCE fiEPOflT AEVI!ION LEA.AO FVENT YEAR REPORT NO, CODE TYPE III) 0 o,

~so

~

~oz s

~

~os

~

! OJ 21 27 23 24 26 2) 28 29 30 31 37 llCTION FUTUflE EFFECT SHUTDOWN ATTACHMENT'PAD4 PRlhIE COSIP CCI.'PONE4'I TAKEId ACTION ON PLANT hIETHOD HOURS Q22 SUBMITTED'OAMSUB.

SUPPLIER MANITFACTUi.f,

~

01. ~9

~Q20 MZQ" 0

0 <<MQ>>

~NQ2" MNQ>>

3'.I 34 35 36 37 40 41 42 43 44 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 Q

Barton Model 288 switch set oint had drifted 1.48 in.

H 0 out of limits. The I switch was inspected, recalfbrated and fcnctionall tested for re eata~bilit To prevent recurrence the switch will be replaced with an analog trip system in accordance with Design Change Request 1398.

44 7

8 9FACI'TY'30 hiETHOD OF STATUS

!4 POWEA OTHER S'fATUS Q DISCOVERY

~l!

s 039 ~5039 sd

~s03l 7

II 9

10 12 I'I 44 45 46 ACTIVI'fY CONTENT RELEASED OF RELEASE AMOUNTOF ACTIVITYQB 0

~Z Q33

~ZQ34 NA 7

8 9

10 I I 45 PERSONNEL F)CPOSUAES 7

8 9

I I 17 13 PEflSONNEl, INJURIES D!SCOVERY DESCRiPTION 042 SI Testing LOCATION OF RELEASE QB NA I

~

.I 89, 9 EX'j ii EH 9

11 12 lOSS OF OA I)AMAGF. To FACIII'fY Q43 TYPE

DESCRIPTION

LZJQn2 NA 9

10 PUII( !CITY 14549)ra l)LSCAIPTIUN~4 LNJQnn NA 9

8 <<886'O8'3 T NAME OF PREPARER PHONE:

68 69 9

rK I

NRC USI I)I'llY

~ Tennessee Valley Authority Browns Ferry Nuclear Plant Form BF-17 BF I,"i.2 I/10/79 LER SUPPLEMENTAL INFORMATION BFRO 260 /

8029 Technical Specification Involved Reported Under Technical Specification 6.7 2.b(1)

Date of Occurrence 7/SS/SO Time of Occurrence 44 Unit Identification and Descri tion of'Occurrence:

Reactor low water level switch LIS-3-203C operated 1.48 in H20 below the T.S. limits when tested in accordance with SI 4.1;A-7 Conditions Prior to Occurrence:

PEr1$

Unit 2 at 97%

MWe Unit 3 at 98%

MWe Action specified in the Technical Specification Surveilldnce Requirements met duo~to ino arabia e4tui~mant.

Describe.

None Apparent Cause of Occurrence:

Setpoint drift Analysis of Occurrence:

There was no damage to plant equipment.

There was no activity release, no personnel exposure or injury and no danger to the health or safety of the public.

Corrective'ct,ion:

The swi,tch was inspected, recalibrated and functionally tested for operability.

The switch will be replaced with an analog system in accordance with Design Change Request 1398.

Failure Data:

260/804, 259/7824, 259/741 and 259/7333.

~Retention:

eriod - Lifetime; Responsibility - Administrative Supervisor

  • Revision: