05000260/LER-1980-023-03, /03L-0:on 800607,during Normal operation,2A Reactor Recirculation Motor Generator Set Tripped Due to Generator Stator Temp High Relay Actuation.Probable Cause Was Loose Wire Caused by Vibration

From kanterella
(Redirected from ML18025A944)
Jump to navigation Jump to search
/03L-0:on 800607,during Normal operation,2A Reactor Recirculation Motor Generator Set Tripped Due to Generator Stator Temp High Relay Actuation.Probable Cause Was Loose Wire Caused by Vibration
ML18025A944
Person / Time
Site: Browns Ferry 
Issue date: 06/27/1980
From:
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML18025A943 List:
References
LER-80-023-03L-02, LER-80-23-3L-2, NUDOCS 8007080399
Download: ML18025A944 (3)


LER-1980-023, /03L-0:on 800607,during Normal operation,2A Reactor Recirculation Motor Generator Set Tripped Due to Generator Stator Temp High Relay Actuation.Probable Cause Was Loose Wire Caused by Vibration
Event date:
Report date:
2601980023R03 - NRC Website

text

~J. '5 )> ~

> I.Z Aal )ILQIJLAI A)a f7 77)

~R CONTFIQL BLOCK: L I

A L

B R

F 2JQ2 9

LICENSEE CODE Licf=gg('PE F.'I/f'F>(; III DO8'f R

INT OR TYPE Al>L REQUIRED INFORMATIONI Q>

IPLEASE PR 6

0 0

0 0 lo

0 0

Qa 4

1 I

1 1 QR~J>Q 25

?G LICENSE TYPE 30 51 CAT'8 r

~01 1

CON'T

~D 1

8 0

LICENSE NUMBER

~LQR 0

5 0

0 0

2 6

0 Q>~06 0

7 8

0 s

0 6

'2 7

8 0

Qa GO 61 OOCKE r NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT OESCRIPTION ANO PROIIAOLE CONSEQUENCES QIO

~ ~DS stator temperature high relay actuation.

This resulted in single loop operation at reduced power.

Reference Technical Specification 3.6.F.

2B reactor recirculation MG set was operable.

There was no danger to health or safety of public.

Previous s

occurrence:

BFRO-50-260/80018rs

~DS 7

8 9

1 8

SYSTE>M

CAUSE

CAUSE COMP.

VAI.VE CODE CODE SUBCODE COAIPONENT CODE SUBCODE SUBCODE'

[~

0 88 Q LXXIQ

> 2 L2iJ Q

> 3 Z

Z 2

Z Z

Z Q,. ~ 0, LJ Q

>.s 9

10 11 12 13 16 19 20 SEO DEN AXIAL OCCVflRFNCI'IEPORT R 6 VISI0 N I I' Ro EVENT YEAR REPORT NO.

CODE TYPE h:().

Q>7 R>>OR>

~80

~

~02 3

i~W

~03J

~1, LJ

~0 21

??

23 24 26>

?8 29 30 31 ACTION FUTURE EFF ECT SHUIDO'LVN zr N ATTACHhlENT NPRD 4 PRIMP CohlP, Covi ONFNT

'MVE)4 ACTION QN PLAN1'ETIIOD HOVRS C?g SUBMITTFD FOHI,'U>>.

SUPPLIER hlANVNACTUREI~

[~XQ>s ~ZQ>s

~SQP>>

~ZQP>

O O

Zi 8

~YQ>a LNJQPR LZJQR i~>J 8 Z

33 34 35:IG 3/

.IO 41 43 44 CAUSE DESCRIPTION ANO CORFIECTIVE ACTIONS 02)

The RTD and rela were checked for ro ergo eration.'o malfunction was discovered.

Most probable

cause

was a loose wire caused by vibration.

The circuit was moved to a J

n 8

9 F AGILITY STATUS

'R POY)ER OTHER STATUS Q 8

Qz>> ~0~98 Qza [

NA 8

9 10 12 44 ACTIVITY CON TfN'f RELEASEO OF RELEASE ASIQUNT OF ACTIVITY s

z Qaa

~zQRR 7

8 9

10 44 PERSONNEL fXPOSURES NUMBER TYPr

DESCRIPTION

3 )

'LOO OJ OJQR z

Qaa NA 1

8 9

11 12 13 PERSONNEL INJURIES i

I'E HIQR OF DISCOVfHY L A>QR>

44 46 NA LOCA I)ON OF RELEASE~

80 f4\\

DISCOVERY DESCRIPT ION 32 Operator observed 2A recirc.. tri ped 8

9 11 12 eo LOSS or oR DAMAGE To FACILITYQ3

'I YPE l)ESCHIPIION 9

Z Qn2I 1

8 9 '0 PIJBLICITY ISR,>\\'ED l)ESCRIPTION R

~NQ<<

8 9

I

>R>> r>ran

>Pi TGR8R0 NA NA I:llF)NE~

NRC USE QNLV LlJJJJJJJJJJ J

GB 69 80

~%,

t

, - =~~ Tennessee Valle'y Author~

~., Groans Ferry Nuclear P~t primum QF-1V BF 15. 2 1/10/79 LER SUPPLEMFNTAL INFORMATION BFRO 260 /

80 23 Technical Specification Involved Reported Undei Technical Specification Date of Occurrence Time of Occurrence 0523

~

Unit Identification and Descri tion'of Occurrence:

Reactor recirculation MG set 2A drive motor tripped with resultant loss of 2A recirculation pump.

Unit operated at reduced load.

Conditions Prior to Occurrence:

Unit 1 8 85%

Unit 2 8

98%

Unit 3 8 75%

Action specified in the Technical Specification Surveillance Requirements met due to i~no erebie e ui nnent.

Describe.

EOI-1 was initiated.

~Ayarcnt Cause of Occurrence:

!Recirculation pump MG set 2A tripped when generator stator temp. relay picked up.

f There was no damage to plant equipment.

There was no activity release, no personnel exposure or injury and no danger to the health or safety of the public.

Corrective Action

Electrical tests were'un on the relay and RTD.

No problems were found and cause of relay actuation unknown.

A p6ssible loose wire caused by vibration was suspected.

Circuit was moved to a spare RTD.

4 Failure Data:

BFRO-50-260/80018

~Retention:

eriod - Lifetime; Responsibility

- Administrative Supervisor
  • Revision: