05000260/LER-1980-002-03, /03L-0:on 791222,w/unit in Cold Shutdown,Found That Flow Control Valve 2-FCV-68-79 on Recirculation Sys Would Not Operate.Caused by Motor Pinion Gear Being Installed Backwards.Installment Procedures Will Be Revised

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/03L-0:on 791222,w/unit in Cold Shutdown,Found That Flow Control Valve 2-FCV-68-79 on Recirculation Sys Would Not Operate.Caused by Motor Pinion Gear Being Installed Backwards.Installment Procedures Will Be Revised
ML18024B272
Person / Time
Site: Browns Ferry 
Issue date: 01/18/1980
From:
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML18024B271 List:
References
LER-80-002-03L, LER-80-2-3L, NUDOCS 8001240418
Download: ML18024B272 (4)


LER-1980-002, /03L-0:on 791222,w/unit in Cold Shutdown,Found That Flow Control Valve 2-FCV-68-79 on Recirculation Sys Would Not Operate.Caused by Motor Pinion Gear Being Installed Backwards.Installment Procedures Will Be Revised
Event date:
Report date:
2601980002R03 - NRC Website

text

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. 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES QIO With the unit in cold shutdown it was found that flow control valve 2-FCV-68-79 on the Recirculation System would not operate.

There was no dan er to the health or safet of the public, and'here have been no similar revious occurrences.

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2 02B 33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS 027 The motor pinion gear had.been LT1stalled backwards.

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shaft until the ears no ion er meshed and valve was rendered ino arable.

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0 Tennessee Valley Authority Bl'o'lvns Fel ry Nuclear Plant I.ER SUPPI.L'MFNTAL INFORMATION Form BF-17 BF 15.2 1/10/79 BFRO 260 / 802 'echnical Specification Involved T.8-3 5 ~ B.14 Reported Under Technical Specification Date of Occurrence 12-22-79 Time of Qccurrence 1142 Un><

2 Ittecirc flow control'alve 2. FCV.68-79 failed to operate from the. control room and fr~ the local pushbutton.

Conditions Prior to Occurrence:

Unit; 2 in cold shutdown, preparing to place 2B recirc pump in service following, outage for PCXS modification.

Unit 1 930 MRe Unit 3 950 MPe average during power ascension Action specified in the Technical Specification Surveillance Requirements met due to~inc crab~le ei ustment.

t)eacribe.

parent Cause of Occurrence:

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The p&ion gear was installed: backward in the valve operator.

This allowed the gear to move on the motor shaft and disengage its mating gear such that the valve would not operate.,

Anal sis of Occurrence:

No ganger to e

tE or safety of the public, no significant resulting occurrence or chain of events.

Corrective Action

Valve operator was replaced, MMX-88 implemented to have second person verification and inspect'ion.

Fatlure Data:

NA

+Retention:

I'eries<I - I.ifc l.!me; Irresponsibility - Administrative Supervisor e

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