LER-1979-011, /01T-0 on 790526:while Pulling Control Rods,First Rod 26-27 in Group 3 Was Inadvertently Withdrawn Three Notches.Caused by Unexplained Factors.Procedures Were Revised |
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| 2601979011R01 - NRC Website |
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t4RC FORIFI 366 I7.77) "
LICENSEE EVENT REPORT CONTROL BLOCK:
0 (PLEASE PRINT OR TYPE ALLREQUIRED INFORMATION).
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LICENSEE CODE 14 15 LICENSE NUMBER 25 26 LICENSE TYPE 30 57 CAT 58 CON'T soURcE ~LQB 0
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09 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Q10
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While pulling control rods to achieve initial criticality for 'cycle 3, the first
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- rod, 26-27 in rou 3 was inadvertentl withdrawn three notches.
The rod moved from
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L osition 02 to osition 08 rather than from osition 02 to 04 as rescribed in the
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rod move sheets.
The reactor scrammed on hi-hi IRM flux.
Based on evaluation of
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rocess neutron monitorin instrumentation no safet limit was exceeded but is
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re orted in accordance with T.
ST 6 ' '.a 4
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No hazard existed to the health and
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safet of the ublic.
Previous occurrence:
259/7901.
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80 SYSTEh1
CAUSE
CAUSE COMP.
VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE t
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10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION LF RIRO EVENT YEAR REPORT NO.
CODE TYPE NO.
Ql7 AEPOIIT ~79
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ACTION FUTURE EFFECT SHUTDOWN ATl'ACHMENT NPROA PRIME COMP.
COMPONENT TAKEN ACTION ON PLANT METHOD HOURS Q22 SUBMITTED FORM SUB, SUPPLIER MANUFACTURER OIB ~Q9
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9 Q26 33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 o
The withdrawal of the rod from position 02 to position 08 is unexplained.
Functional testing of the rod after the event revealed that the rod would not travel three positions when given a notch withdraw signal.
Prior to restartz
& review of the 3
event was conducted and no safety limits were exceeded.
A subsequent rod pull, using the same
- sequence, resulted in a period of approximately 4'3 seconds.
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FACILITY STATUS
'YiPOWER OTHER STATUS Q I
6 B
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29 N/A METHOD OF DISCOVERY
~AQ3 45 46 45 N/A 7
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11 12 LOSS OF OR DAMAGETO FACIUTY Q43 TYPE
DESCRIPTION
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10 PUBLICITY ISSUED DESCRIPTION~
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8 N/A NAME OF PREPARER CC! LJO ~O ACTIVITY CONTENT RELE'ASED OF RELEASE AMOUNTOF ACTIVITYQS
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Q34 N A 7
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10 I I 44 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION Q39
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11 12 13 PERSONNEL INJURIES NUMBER OESCRIPTIONQ41
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Q44 DISCOVERY DESCRIPTION Q32 0 erator Observation LOCATIOTIOF RELEASE Q N/A NRC USE ONLY 68 69 PHONE:
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Tennessee Valley Authority Browns Ferry Nuclear Plant LER SUPPLEMENTAL INFORMATION Form BF-17 BF 15.2 1/10/79 BFRO 260 / 7911 Technical Specification Involved 6 7 2 a 4 Reported Under Technical Specification 6.7.2.a.4
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Identification and Descri tion of Occurrence:
BFNP unit 2 scrammed at 1928 on May 26, 1979,.while pulling control rod 26-27, l
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the first rod in RWM group 3, during an approach to critical,.
The cause of the scram was high neutron flux'on IRM's C, D, and F.
The reactor period was calculated to be 5.5 seconds.
Conditions 'Prior to Occurrence:
Normal startup procedure following the spring 1979 refueling 'outage.
This was the first approach to critical.
Action specified in the Technical Specification Surveillance Requirements met
'ue to ino erable e ui ment.
Describe.
N/A" A
arent Cause of Occurrence:
Movement of control rod 26-27 three positions.
Anal sis of Occurrence:
A reactivity insertion of approximately 0.287 percent delta K/K resulted when control rod 2o-27 was withdrawn from position 02 to position 08.
The resulting reactor period.by the SRH recorder was at3out one second.
Xt was calculated'o be 5.5 seconds.
Corrective Action
Prior to initial criticality follo<d.ng a.refueling outage, any control rod that has a single-notch worth wnich is capable of producing a period of equal to or less than 60 seconds, or any control rod that'has a double-notch worth capable of producing a period of equa'1 to or less than 30 seconds, will be wi<h-drawn"on a notch basis.
The nuclear engineer will be present in the control room during the period of time from initial rod pull until criticality is achieved.
During this period of time, he will confirm acceptable core behavior.
, Failure Data:
N/A
eriod - Lifetime; Responsibility - Administrative Supervisor
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| 05000296/LER-1979-001-03, /03L-0 on 790111:switch on LIS-3-56B Failed to Trip Reactor Recirculation Pump Motor Generator.Caused by Misadjusted Switch on Yarway Model 4418CE.Switch Recalibr & Tested Satisfactorily | /03L-0 on 790111:switch on LIS-3-56B Failed to Trip Reactor Recirculation Pump Motor Generator.Caused by Misadjusted Switch on Yarway Model 4418CE.Switch Recalibr & Tested Satisfactorily | | | 05000296/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000259/LER-1979-001, Forwards LER 79-001/01T-0 | Forwards LER 79-001/01T-0 | | | 05000259/LER-1979-001-01, /01T-0 on 790118:reactor Scrammed Due to High Flux Actuating Intermediate Range Monitor high-high Neutron Monitoring Circuit;Reactor Neared Criticality.Caused by Withdrawal of High Reactivity Worth Rod | /01T-0 on 790118:reactor Scrammed Due to High Flux Actuating Intermediate Range Monitor high-high Neutron Monitoring Circuit;Reactor Neared Criticality.Caused by Withdrawal of High Reactivity Worth Rod | | | 05000260/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000260/LER-1979-001-03, /03L-0 on 790113:during Test of high-pressure Injection Coolant Sys,Steam Supply Valve FCV-73-16 Failed to Open,Rendering Sys Inoperative.Caused by Failure of Limitorque Valve Operator Limit Switch | /03L-0 on 790113:during Test of high-pressure Injection Coolant Sys,Steam Supply Valve FCV-73-16 Failed to Open,Rendering Sys Inoperative.Caused by Failure of Limitorque Valve Operator Limit Switch | | | 05000296/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000259/LER-1979-002-03, /03L-0 on 790129:during Normal Operation While Performing Surveillance Test,Standby Liquid Control Pump 1B Relief Valve Opened Below Tech Spec Min.Caused by Valve Seat Surface Deterioration | /03L-0 on 790129:during Normal Operation While Performing Surveillance Test,Standby Liquid Control Pump 1B Relief Valve Opened Below Tech Spec Min.Caused by Valve Seat Surface Deterioration | | | 05000259/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000260/LER-1979-002-03, /03L-0 on 790203:alarm for Fire Protection Panel 25-236 Annunciated in Control Room.Panel Was Not Alarmed Condition.Caused by Normal End of Life Electrical Failure of Annunciator Point Card.Card Replaced & Sys Normalized | /03L-0 on 790203:alarm for Fire Protection Panel 25-236 Annunciated in Control Room.Panel Was Not Alarmed Condition.Caused by Normal End of Life Electrical Failure of Annunciator Point Card.Card Replaced & Sys Normalized | | | 05000260/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000296/LER-1979-002-03, /03L-0 on 790117:during Maintenance of Reset Switch,Short Circuit Damaged Power Supply & Sensor Circuit Board,Rendering Fixed Spray Automatic Initiation Circuit for Fire Protection Inoperable | /03L-0 on 790117:during Maintenance of Reset Switch,Short Circuit Damaged Power Supply & Sensor Circuit Board,Rendering Fixed Spray Automatic Initiation Circuit for Fire Protection Inoperable | | | 05000296/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000259/LER-1979-003-01, /01T-1 on 790120:during Cold Shutdown,Local Leak Rate Test Indicated Excessive Total Leakage.Caused by Leaking Valve Seating Surface in Eight Valves.Valves Repaired & Retested | /01T-1 on 790120:during Cold Shutdown,Local Leak Rate Test Indicated Excessive Total Leakage.Caused by Leaking Valve Seating Surface in Eight Valves.Valves Repaired & Retested | | | 05000259/LER-1979-003, Forwards LER 79-003/01T-1 | Forwards LER 79-003/01T-1 | | | 05000260/LER-1979-003-01, /01T-0 on 790214:rod Position Info Sys Power Supply Ps X-5 Failed,Causing Loss of Rod Position Indication in Bottom Half of Vertical Core Display.Caused by Failure of Cooling Fan in Trygon Model L5B6-70-OVS4989 | /01T-0 on 790214:rod Position Info Sys Power Supply Ps X-5 Failed,Causing Loss of Rod Position Indication in Bottom Half of Vertical Core Display.Caused by Failure of Cooling Fan in Trygon Model L5B6-70-OVS4989 | | | 05000259/LER-1979-003-03, /03L-2 on 790120:during Cold Shutdown,Local Leak Rate Test Revealed Total Leakage Exceeded Allowable 60% La Per 24-h.Caused by Excessive Leakage of Valve Seating Surface.Eight Leaking Valves Were Repaired & Retested | /03L-2 on 790120:during Cold Shutdown,Local Leak Rate Test Revealed Total Leakage Exceeded Allowable 60% La Per 24-h.Caused by Excessive Leakage of Valve Seating Surface.Eight Leaking Valves Were Repaired & Retested | | | 05000296/LER-1979-003-03, /03L-0 on 790202:linear Heat Generation Rate Out of Tech Spec Limits.Caused by Operation Close to Limiting Values & Increase in Reactivity Due to Gadolina Burnup. Greater Margin to Limiting Value Will Be Maintained | /03L-0 on 790202:linear Heat Generation Rate Out of Tech Spec Limits.Caused by Operation Close to Limiting Values & Increase in Reactivity Due to Gadolina Burnup. Greater Margin to Limiting Value Will Be Maintained | | | 05000260/LER-1979-003, Forwards LER 79-003/01T-0 | Forwards LER 79-003/01T-0 | | | 05000260/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000259/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000259/LER-1979-004-03, /03L-0 on 790227:during Normal Operation,Review of Surveillance Test Data Indicated Monthly Samples of Diesel Fuel Taken in Dec 1978 Have Not Been Analyzed.Caused by Loss of Samples in Transit.Will Try to Measure Samples on | /03L-0 on 790227:during Normal Operation,Review of Surveillance Test Data Indicated Monthly Samples of Diesel Fuel Taken in Dec 1978 Have Not Been Analyzed.Caused by Loss of Samples in Transit.Will Try to Measure Samples on Site | | | 05000296/LER-1979-004-03, /03L-0 on 790411:during Normal Operation,Heat Detector Alarmed & Would Not Clear.Alarm Would Have Masked Signals from Other Detector,Required to Be Operational.Caused by Personnel Damaging Detector | /03L-0 on 790411:during Normal Operation,Heat Detector Alarmed & Would Not Clear.Alarm Would Have Masked Signals from Other Detector,Required to Be Operational.Caused by Personnel Damaging Detector | | | 05000260/LER-1979-004-03, /03L-0 on 790414:reactor Bldg,Turbine Bldg & Refueling Zone Vent Exhaust Monitor RM-90-250 Failed Surveillance Test SI 4.8.B-4.3,Section 4e.Caused by Failure of Input Card for Radiation Monitor | /03L-0 on 790414:reactor Bldg,Turbine Bldg & Refueling Zone Vent Exhaust Monitor RM-90-250 Failed Surveillance Test SI 4.8.B-4.3,Section 4e.Caused by Failure of Input Card for Radiation Monitor | | | 05000296/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000296/LER-1979-005, Updated LER 79-005/01T-2:on 790506,RHR Svc Water Supply to RHR HX 2B Isolated Standby Coolant Supply.Caused by Lack of Administrative Control Over Sys Cross Connect Valves. 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Controls Improved | | | 05000296/LER-1979-005-01, /01T-1:on 790506,BHR Water Supply Isolation to 2B RHR Heat Exchanger Isolated Standby Coolant Supply to Unit 3.Caused by Lack of Administrative Control Over Sys Cross Connect Valves.Administrative Controls Have Been Improved | /01T-1:on 790506,BHR Water Supply Isolation to 2B RHR Heat Exchanger Isolated Standby Coolant Supply to Unit 3.Caused by Lack of Administrative Control Over Sys Cross Connect Valves.Administrative Controls Have Been Improved | | | 05000259/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000259/LER-1979-005-03, /03L-0 on 790225:reactor,turbine Bldg & Refueling Zone Vent Exhaust Monitor RM-90-250 Became Inoperable.Caused by Moisture Collection in Detector SC-2.-1.S.Detector Replaced & Moisture Removed | /03L-0 on 790225:reactor,turbine Bldg & Refueling Zone Vent Exhaust Monitor RM-90-250 Became Inoperable.Caused by Moisture Collection in Detector SC-2.-1.S.Detector Replaced & Moisture Removed | | | 05000260/LER-1979-005-03, /03L-0 on 790419:broken Terminal Discovered on Shutdown Board D Battery.Cause Unknown.Affected Cells Replaced & Personnel Instructed in Proper Tightening Methods | /03L-0 on 790419:broken Terminal Discovered on Shutdown Board D Battery.Cause Unknown.Affected Cells Replaced & Personnel Instructed in Proper Tightening Methods | | | 05000260/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000296/LER-1979-006-03, During Normal Operation, Erratic Indication of Torus Hydrogen Sensor Observed. 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Hydrogen Sensor Replaced & Tested Satisfactory.Design Change Request Initiated | | | 05000296/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000260/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000259/LER-1979-006-03, /03L-0 on 790228:reactor,turbine Bldg & Refueling Zone Ventilation Exhaust Monitor RM-90-250 Became Inoperable for 3.5-h.Caused by Moisture in SC-2B Detector & Leaking Flanges.Moisture Removed & Flanges Tightened | /03L-0 on 790228:reactor,turbine Bldg & Refueling Zone Ventilation Exhaust Monitor RM-90-250 Became Inoperable for 3.5-h.Caused by Moisture in SC-2B Detector & Leaking Flanges.Moisture Removed & Flanges Tightened | | | 05000259/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000260/LER-1979-006-03, /03L-0 on 790427:prior to Refueling Shutdown, Drywell Prepurge Tritium Sample Not Taken.Caused by Lack of Understanding Between Operational & Lab Personnel.Operating Instructions Amended to Prevent Recurrence | /03L-0 on 790427:prior to Refueling Shutdown, Drywell Prepurge Tritium Sample Not Taken.Caused by Lack of Understanding Between Operational & Lab Personnel.Operating Instructions Amended to Prevent Recurrence | | | 05000260/LER-1979-007, Forwards LER 79-007/03L-0 | Forwards LER 79-007/03L-0 | | | 05000296/LER-1979-007, Forwards LER 79-007/03L-0 | Forwards LER 79-007/03L-0 | | | 05000296/LER-1979-007-03, /03L-0 on 790612:during Performance of Procedure SI 4.1.A-14,turbine First Stage Permissive Pressure Switches PS-1-81A & B & PS-1-91A & B Setpoints Exceeded Tech Specs. Caused by Setpoint Drift.Switches Recalibr | /03L-0 on 790612:during Performance of Procedure SI 4.1.A-14,turbine First Stage Permissive Pressure Switches PS-1-81A & B & PS-1-91A & B Setpoints Exceeded Tech Specs. Caused by Setpoint Drift.Switches Recalibr | | | 05000260/LER-1979-007-03, /03L-0 on 790503:during Refueling Outage,Five MSIVs Exceeded Leakage Limits.Caused by Irregularities on Valve Seating Surfaces & Entrapment of Debris Under Seating Surfaces.Valves Will Be Repaired & Retested | /03L-0 on 790503:during Refueling Outage,Five MSIVs Exceeded Leakage Limits.Caused by Irregularities on Valve Seating Surfaces & Entrapment of Debris Under Seating Surfaces.Valves Will Be Repaired & Retested | | | 05000260/LER-1979-008-01, /01T-0 on 790504:while Preparing for Refueling Outage,Secondary Containment Integrity Was Not Conclusively Demonstrated Prior to Breaking Primary Containment.Test Improperly Performed Due to Personnel Error | /01T-0 on 790504:while Preparing for Refueling Outage,Secondary Containment Integrity Was Not Conclusively Demonstrated Prior to Breaking Primary Containment.Test Improperly Performed Due to Personnel Error | | | 05000259/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000259/LER-1979-008-03, /03L-0 on 790612:during Normal Operation, Pressure Switches PS-1-81 a & B & PS-1-91 a & B Setpoints Exceeded Tech Specs by 3-15 Psig. Caused by Model B2T-A12SS Switches Drifting | /03L-0 on 790612:during Normal Operation, Pressure Switches PS-1-81 a & B & PS-1-91 a & B Setpoints Exceeded Tech Specs by 3-15 Psig. Caused by Model B2T-A12SS Switches Drifting | | | 05000296/LER-1979-008-03, /03L-0 on 790627:no Speed Indication Noted on Reactor Core Isolation Coolant.Caused by Broken Wires to Magnetic Pickup EG-M Box.Wires Repaired | /03L-0 on 790627:no Speed Indication Noted on Reactor Core Isolation Coolant.Caused by Broken Wires to Magnetic Pickup EG-M Box.Wires Repaired | | | 05000260/LER-1979-008, Forwards LER 79-008/01T-0 | Forwards LER 79-008/01T-0 | | | 05000296/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000296/LER-1979-009-03, /03L-0 on 790717:hydrogen Ignition Damaged HEPA Filters.Caused by Improper Offgas Recombiner Preheater Operation.Sys HEPA Filters & Charcoal Bed Inspected.Three Filters Replaced.Procedures Will Be Revised | /03L-0 on 790717:hydrogen Ignition Damaged HEPA Filters.Caused by Improper Offgas Recombiner Preheater Operation.Sys HEPA Filters & Charcoal Bed Inspected.Three Filters Replaced.Procedures Will Be Revised | | | 05000260/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000296/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | |
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